ML19210D352

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LER 79-096/01T-0:on 791110,nonisolable Weld on Pump a Suction Line Test Connection Discovered Leaking.Cause Unknown.Line Cut,Plugged & Capped.Affected Weld Connections Will Be Metallurgically Evaluated
ML19210D352
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 11/21/1979
From:
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19210D351 List:
References
LER-79-096-01T, LER-79-96-1T, NUDOCS 7911260338
Download: ML19210D352 (1)


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t.lCENSEE EVENT REPORT CONTROL BLOCK: l l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 GTl 8I 9Nl ClLICENSEE P l El Pl 1[gl50 j 0 ] -l 0 l 0 ] 0 ] 0 l 0 l - l 0 l250 lgl l lg 14 LICENSE NUMBER 26 4 LICENSE l 1 l l j TYPE1l JOl jgl$7 CA T 58 7 CODE 1 CON'T E "

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68 69 EVENT CATE 74 REPORT DATE 7 8 60 61 DOCK ET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h I o l 2 I lWhile work was progressing on the seal replacement of the "A" reactor recirculation o a l pump, a mechanic noted that a nonisolable weld on pump "A" suction line test con- l o 4 Inection was leaking. The 3/4-inch line is about 2-1/2 feet in length and contains a

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90* elbow, two 3/4-inch valves, and a cap. The crack was associated with the pipe to l o s o e telbow weld away from the recirculation loop. I O 7 i Technical Specifications 6.9.1.8c l I

o a i 80 7 8 9 DE CODE SLBC E COMPONENT CODE SU8 CODE S E 7

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18 19 20 SEOUENTIAL OCCURRENCE REPORT REVISION

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EVENT YE AR REPORT No. CODE TYPE N O.

LE R/RO OO RE RT yUQE l7l9l l-l 0l9l6l l/l l0l1l l Tl l-l l0 l 21 22 23 24 26 27 N 3 30 31 32 T KN ACT ON ON PLANT TE hours S8 i O FOR 8. SUPPLIE MANUFACTURER lFl@lXl@

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42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h i o lThe line*was cut upstream of the 90* elbow, plugged, and capped per an approved plant lTTTl [ modification. A similar modification was performed on the "B" pump during this period.i g JThe Unit No. 2 "B" pump was modified in 1977 and the Unit No. 2 "A" pump will be modi-l g , l 31 lfied at the next scheduled cold shutdown (presently December 1979). Affected welds on[

L' L4J Iboth Unit No. 1 connections will be metallurgically evaluated to determine the cause [

7 8 9 80 STA S  % POWER oTHER STA TUS is O RY DISCOVERY DESCRIPTION W l,_Gj @ l0l 0 l 0l h l N/A l l A l@l Mechanic Surveillance 0 l

ACTIVITY CO TENT

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RETE ASEo CF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE i c {_gj @ W@l N/A 44 l N/A 45 80 l

7 8 9 10 11 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION

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LOSS OF On DAMAGE TO F ACILITY TYPE DE SCniP TION j h l

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  1. MU 10 79112603 9/3 iititiiiiiiiil) 68 69 80 5;

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NAME Of PREPAHEli PHONE:

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LER CONTINUATION--RO #1-79-96 FACILITY: BSEP Unit No. 1 EVENT DATE: 11-10-79 of failure.

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