ML19242A828

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LER 79-075/03L-0 on 790708:no Visible Oil Level in Outboard Bearing Oil Reservoir Sight Glass on Containment Spray Pump 1-2.Caused by Component Failure.Oil Added to Reservoir & Fittings Tightened
ML19242A828
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 08/02/1979
From: Hartigan J
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19242A826 List:
References
LER-79-075-03L, LER-79-75-3L, NUDOCS 7908060439
Download: ML19242A828 (2)


Text

U. S. NUCL E AR e _GUL ATORY COMMISSION N BC. F O H M 306 (7 77)

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EVENT DEsCni 110'l A .D PRCD L C . i .CES o , [On July 8, 1979, operations personnel naking routine rounds noticed that there was no j n ;3 l visible oil level in the outboard bearing oil reservoir sight glass on Containnent _j l Spray Punp 1-2. The prcsence of oil on the floor was also noted.

The pump was de- J n 3 gg [ clared inoperable at OJ30 hours on July 8, 1979, placing the unit in the ac tion state-l There was no danger to the health and safety) o e Ln er.t of Technical Specification 3.6.2.1.

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l of the public or station personnel. Containment Spray Pump 1-1 was operable through- l gg ; out ' hi s occurrence. (.P-33-79-83)

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CAUSE DESCHlPT!G'i m3 CO% E C Ti' CTIONS

, o l The cause is ccaponent failure; oil was leaking at a gasketed joint at the botton of l 3 3 [the sight glass and at a threaded plug in the bearing end cover. Oil was added to thel The

, l reservoir, and the fittings were tightened under Maintenance Work Order 79-2462. 1

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pump was declared operable removian the unit from the oction statement at 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> l 1979. j

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TOLEDO EDISON CG'!PA'iY DAVIS-BESSE NUCLEAR PO'!ER ETAT 105 UNIT ONE SUPPLEMENTAL INFOPJL\ TION For LER SP-33-79-S3 DATE OF EVENT: July 8, 1979 F ACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Containment Spray Ptrap 1-2 outboard bearing oil reser-voir leak Conditions Prior to Occurrence: The unit was in Mode 3, with Power (MWT) = 0, and Load (Cross MWE) = 0.

Description of Occurrence: On July 8,1979, while making routine rounds, op era t ion s personnel observed that there was no visible oil level in Containment Spray Punp 1-2 outboard bearing oil reservo ir sigh t glass, and oil was found en the floor. Mainten-ance personnel were contacted to investigate the oil leak and refill the il reservoir.

The pump was declared inoperable at 0130 hours0.0015 days <br />0.0361 hours <br />2.149471e-4 weeks <br />4.9465e-5 months <br /> on July 8,1979, placing t.ie unit in the action statement of Technical Specification 3.6.2.1 which requires the operability of tw> independent containment spray syst.ns in Modes 1, 2, 3, and 4.

c.,..,, ,, r occurrenc e: The apparent cause is componenr ttiinre.

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Investigation conducted under Maintenance Work Order 79-2462 found oil leaking it a gasketed joint at the bottom of the sight glass and at a threaded plug in the center of the hearing end cover. No maintenance had been done on this pump since .Tanuary, 1979. The leaks may have developed from vibration loosening the nut en top ot the sight glass and the plug in the center of the bearing end cover.

Analysis of Occurrence: There was no danger to the health and saf ety of the public or to station personnel. Containment Spray Pump 1-1 was operable and capabic of per-forming the intended safety function if required.

Corrective Action: Under Maintenant.e Work Order 79-2462, oil was added to the out-board bearing reservoir and the fittings were ti;;h t ene d . The pump was declared opera-ble at 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> on July 8, 1979, removing the unit from the action statement of Technical Specification 3.6. 2.1. "o further leaks have been observed. Maintenance Work Order 79-2529 was issued to lock the above mentioned fittings on both pumps with Loctite to prevent future loosening fron vibration.

Failure Data: No pr_.vious oil leaks have occurred on Containment Spray Pumps.

LER #79-075

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