ML19207B124

From kanterella
Revision as of 21:24, 15 August 2019 by StriderTol (talk | contribs) (Created page by program invented by StriderTol)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
LER 79-059/03L-0 on 790718:discovered Low Fluid Level on Snubber 2E51-40SS87,RCIC Pump Suction.Caused by Leaking Seals.Snubber Replaced
ML19207B124
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 08/15/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19207B121 List:
References
LER-79-059-03L, LER-79-59-3L, NUDOCS 7908230404
Download: ML19207B124 (1)


Text

' '(7 77)LICENSEE EVENT REPORT , , , , , CONTROL BLOCK: l llllllh (PLEASE PRINF OR TYPE ALL REQUIRED INFORMATION) 1 O_N l C BlElPl2l@l0 0l-l0l0 0 0 0 -l0 0 l@l 4 1 1 l1 1 @ll@o 1 7 8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TY PE JQ 5 7 C A T 58 CON'T 5$RC lLl@l0l5 0l-l0 3 l 2 l 4 @l 0 l 7 ( 1 l 8 l 7 l 9 lg 0 l 8 l 1 l 5 l 7 l 9 l@

"" o 1 7 8 60 61 DOCKET NUMBER 68 69 EVE'JT D ATE 14 75 REPORT D ATE 80 EVENT GESCRIPTION AND PROBABLE CONSEQUENCES h o 2 bitriw normal plant operation, snubber 2E51-40SS87, RCIC Pump Suction, was noticed to I o a have a low fluid level by plant personnel. Tha snubber was functionally tested, and itl Ifailed the test.

lo 4 sj gechnical Specfication 3.7.5, 6.9.1.9b l0 Lo ' 6 1 I O.'7 I I O 8l!7 8 9 80 SYSTE\1 CAUSE CAUSE COYP.VA LV E CODE CODE SUBCODE COVPON ENT CODE SUSCODE SUSCODE o 9lClE @ l E l@ l X [@ lS lU lP l0 R lT l@ l D @ l Z l @

7 8 9 10 11 12*3 18 19 20_SEQUENTI AL OCCURRENCE REPORT REVISION LER RO EVENT YE AR REPORT NO.

CODE TYPE NO.@ REPl7 l9 l_ll 0l 5l 9l j ,,, -l 0l 3[lLll_ll 0l_ 21 22 23 24 26 27 28 29 Ju 31 32 T K ACT ON O PLANT 4 HOURS S B IT FOR 8.SUPPLIE MANUFACTURER

[I_j@l 7 l@

W@d@l 0l 0l Ol 0 lNl@l Yl@lA@lB l2 l0 l9 l@

J3 J4 35 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l The low fluid level was due to leaking seals. The snubber was replaced with one from l i ol stock. This snubber will be counted as inoperable on the next visual inspection of

, 3;; accessible snubbers per Technical Specifications., ,, , t 1 lllt 1 4 7 3 9 80 ST S". POWER OTHER STATUS IS OV RY DISCOVERY OE%RIPTION

[Ej @ l0l9 5 l@l NAll A l@l NA l1 5 A TIVITY CO TENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATION OF RE' EASE RM [_Zj @ l Z l@l NA lNAl7 d 9 10 11 44 45 80 PERSON %E L E kPOSURES NUMBER TYPF OESCRIPTION d d l 0l 0l 0l@ lZ l@l NAlPERSONNEL INJURIES NUV8ER DESCRIPTION

y. b'1 b 4 l0l 0 l 0 l@l NA I a (/1 3 9 11 12 80 LOSS OF OR DAVAGE TO FACILITY ggi r"' '790823 MM , s F 8 9 10 80 DE CRIPTION

'*<!$UUEL 81 NA lllllllllllll lI 2 o'a 9 10 68 69 80 5 o M son, R.

~NAME OF PREP ARER

..PHONE: