ML19209C973

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LER 79-061/03L-0:on 790917,various Snubbers on safety- Related Sys Found Inoperable.Caused by Low Fluid Level & Loose Pipe Clamps Leading to Snubber Clippage.Snubbers Positioned Per Plant Drawings & Tightened
ML19209C973
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 10/03/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19209C970 List:
References
LER-79-061-03L-01, LER-79-61-3L-1, NUDOCS 7910180534
Download: ML19209C973 (1)


Text

(7 77)LICENSEE EVENT REPORT CONTROL BLOCK: l llllllh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 M lN l C 1Bk' P l 1 l@15l 0l 0l -l 0l O! 0l O! O ~l0l0l@l4l1 1l 1l 1l@l ll@7 8 9*lTCENSJE ODE 14 LICENSE NUMBER 25 26 LICEs SE TYPE JO

$7 CAT $8 CON'T EnN l L l@l 0 l 5 l0 l- 10 l 3 l 2 l5 @l Ol 91 il 7l 7 9hl1l0 l0 l3 [7 l9 lg O 1 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 FtEPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l O 121 lWhile performing PT 19.6.0.2, Visual Inspection of Accessible Snubbers on Safety l@ l Related Systems, the following were found inoperable:

1) ISW-173SS175, service water l lTITl to discharge canal; 2) 1E11-18SS47, line from RHR heat exchanger to vessel; 3) 1C41-ll0lsl 9SS27, line from SLC pumps to vessel; 4) 1G41-1SS22, fuel pool cooling line to RHR; l0 sl5) IG41-20SS76, fuel pool cooling recirculation line.

I I O I 7 I lTechnical Specifications 3.7.5, 6.9.1.9b l0 all7 8 9 80 DE CODE SU8C E COMPONENT CODE SU8 CODE SU ElS lH l@ Q@

l@ l S l U l P l 0 l R l T l@ W@ y @

B O 9 7 8 9 10 11 12 13 18 19 20., SEQUENTI AL OCCURRENCE REPORT REVISION LER/RO EVENT YEAR R EPOR7 NO.

CODE TYPE N O.@ REPOyl217l 9ll_ll 0l 6l 1l y 0l3llL g W 22 23 24 26 27 28 29 30 31 32 KN A O O PLANT M HOURS 22 58 i FOR 8.SUP Lt R MANUFACTURER lB l@34Zl@

Zl@l Zl@l 0l 0; 0l lNlglY[g A lgl B 2l0l9lg 33 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AP..> CORRECTIVE ACTIONS h i Ol Snubbers ISW-173SS175, and IE11-18SS47 had a low fluid level. These snubbers were li li l l rebuilt with new seals and functionally tested. Snubbers IC41-9SS27. and IG41-ISS?C ITT q and 1G41-20SS76 had loose pipe clamps which allowed the snubbers to slip on their i g pipes. The snubbers were positioned per plant drawings and tightened. Testing of I g l snubbers will continue per Technical Specifications.

7 8 9 80 ST S% POWER OTHER STATUS DIS RY DISCOVERY DESCRIPTION y W@ l 0l 0l 0l@lNA ll B l@l Periodic Test lA TIVITY CO TENT RELEASS.D OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE R W @ lZ l@l NA llNAlPERSONNEL EXPOS ES NUMBER TYPF.DESCRIPTION ITTil l O l 0 l 0 l@l z l@l NA l'* " PERSONN E t iNauNiES

-~" , NUMBER DESCRIPTION ll0l0 0l@lNAlt s 7 8 9 11 12 80'#;5 ESC %^fy'J,C'"'@7910180' " ^E Zl@lNAl1 9 7 8 9 10* ' ' '80 iSSuEf@lDISCRiPr!ON O

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l, N_NA 2 o'8 9 10 68 69 80 g o NAME OF PREPARER

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