ML061000598

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E-mail from D. Croulet of Entergy to J. Noggle of USNRC, Regarding H-3 Sources IPEC-RL-Comments-1
ML061000598
Person / Time
Site: Indian Point  Entergy icon.png
Issue date: 12/20/2005
From: Croulet D
Entergy Nuclear Operations
To: Noggle J
Division of Reactor Safety I
References
FOIA/PA-2006-0081
Download: ML061000598 (10)


Text

James Noggle -FW: H-3 sources iPECRL Comments 1.xls _Page1JJ From: "Croulet, Donald" <dcroule@entergy.com>

To: "'James Noggle"' <JDN~nrc.gov>

Date: 12/20/05 3:30PM

Subject:

FW: H-3 sources IPEC_RL_Comments_1.xls Jim, At todays Spent Fuel Pool status meeting I inquired about our plans to verify that the Unit 1 south curtain drain was unblocked and functioning and also the Unit 2 containment footer drain system and segregation of its outfall for sampling at manhole 5. I was told that a feasibility study is in progress to determine robotics entry points.From: Croulet, Donald Sent: Tuesday, December 20, 2005 9:46 AM To: 'James Noggle'

Subject:

FW: H-3 sources IPECRLComments_1.xls Jim, This is the last list I have. I will confirm with Bill Axelson. We will send you an updated version as changes occur to this list.From: Lavera, Ron Sent: Tl ursday, December 08, 2005 5:47 PM To: Solanto, Robert; Bob Evers; Christopher English; David Smith; Don Leach; Don Mayer; Donald Croulet; Dragos Nuta; Gary Hinrichs; Hank Santis; James Peters; Joe Kulaga; John Skonieczny; Kathy McMullin; Kenneth Morin; Michael Durfee; Michael Rutkoske; Paul Deeds; Richard Colville; Richard Drake; Flon Lavera; Ronald Sachatello; T. R. Jones

Subject:

H-3 sources IPEC_RLComments_1.xIs To all This is the known past leakage list that Dennis Quinn and I have compiled, so far. Please let me know about any addtions/deletions/changes.

Thanks Ron<<H-3 sources IPEC RL-Comments-1.xls>>

Js Nogge -FW: H-3 sourcesIPEC RL Comments 1.xls Pag1 From: "Croulet, Donald" <dcroule©entergy.com>

To: "'James Noggle"' <JDN~nrc.gov>

Date: 12/20/05 9:46AM

Subject:

FW: H-3 sources IPECRLComments_1.xls Jim, This is the last list I have. I will confirm with Bill Axelson. We will send you an updated version as changes occur to this list.From: Lavera, Ron Sent: Thursday, December 08, 2005 5:47 PM To: Solanto, Robert; Bob Evers; Christopher English; David Smith; Don Leach; Don Mayer; Donald Croulet; Dragos Nuta; Gary Hinrichs; Hank Santis; James Peters; Joe Kulaga; John Skonieczny; Kathy McMulli,;

Kenneth Morin; Michael Durfee; Michael Rutkoske; Paul Deeds; Richard Colville; Richard Drake; Ron Lavera; Ronald Sachatello; T. R. Jones

Subject:

H-3 sources IPEC_RLComments_1 .xls To all This is tne known past leakage list that Dennis Quinn and I have compiled, so far. Please let me knovi about any addtions/deletions/changes.

Thanks Ron<<H-3 sources IPEC_RL_Comments_1.xls>>

Potential Volume H-3 H-3 total for.U2 FSP 3.OOE+05 2.80E-02 3.18E+01 high 1990-1992, 2005 2000 leak from wall from skimmer U3 FSP 3.OOE+05 3.40E-02 3.86E+01 High pump leak onto concrete Noticed in 1990-1994 time frame. Initial leakage not contained/collected.

On going leakage. Containment process U1 West Pool 1.OOE+05 4.OOE-04 1.51 E-01 High implemented.

leakage not contained/collected.

On U1 Other Pools 0.00E+00 High going leakage. Containment process Anecdotal information that it over flowed to the ground on several U2 RWST 3.50E+05 1.68E-01 2.23E+02 occasions in the past No known significant leakage to the U3 RWST 3.50E+05 4.64E-02 6.15E+01 ground.Anecdotal information that the area was U2 CVCS Tanks 0.OOE+00 flooded in the past Anecdotal information that the area was U2 Waste Tanks 0.00E+00 flooded in the past Anecdotal information that the area was flooded by Waste Collection Tank U2 MOB 0.OOE+00 Med water, in the past Overflows of 31 Waste Tank into tank A .pit containing 31 WHUT, and 31-33 pitc cotIng 31r- WHUT+ -n', andl 31,-3.Ve- T- nnL -. m -LC IMe d III IL4LHTS I l 70' UL4c1a y V's.I.

._ 31 WHUT tank area flooded. 32 & 33 U3 Waste Tanks _.O0E+00 Tank areas never flooded.Potential for Tritium contamination of U2 SFP 1990 -1992 Leak [a] 1.83E+04 2.OOE-02 1.39E+0O High soil.U2 RWST Overflow (year?) 0.OOE+00 _ (U2 PAB Sump = 1.OOE-01 0.OOE+00 Med Sump is not lined with stainless steel.Floor was flooded to significant depth in U2 15 Ft. PAB 0.OOE+00 Med late 1970's early 1980's U3 PAB Sump = = 0.OOE+00 U3 to U2 underground waste line -Leaked in 1980s; it was abandoned in abandoned 0.OOE+00 place Known Contamination near the GT U3 to U2 Blowdown Transfer Line High between units.U2 Resin Spill in alleyway next to Resin spill with relative small volume of FSB 0.OOE+00 low water.%J.J- I IJWJI I WV ILI I LIAVI I IAUJ PD;7u-trench from PAB spilling into area Known leakage in the 1977-1985 time below cable tunnel 0.OOE+00 High frame.Known leakage in the 1977-1985 time U3- area between VC, FSB, PAB, frame. Extends to building curtain aka Pigeon Pit, unknown leakage _ 0.OOE+00 drains and storm sewer system.a- assume 25 gallons/day x 2 years= 18,300 gallons _0.E+00L south of U3 Command Post, had Cs 137, Co-60, others. Removed in -1 1980 and stored on hill past met tower O.OOE+Oo High U2 Blowdown (Past) atmospheric Known operation for years, with primary release O.OOE+O0 to secondary leaks.U2 Blowdown (current) atmospheric Known operation for years, with primary release 5.OOE-07 O.OOE+00 to secondary leaks.Contamination of secondary plant -U2 SG Tube Leak Feb 2000 O.OOE+00 drains U3 SG Tube Leak Oct 1989 =.OOE+00 Contamination of secondary plant U3 Operation of Main Steam supply Auxilary steam system drains go to to Auxilary Steam system. 5.OOE-07 O.OOE+Oo High plant drains and storm drain system.Anecdotal information that the area U2 PAB 15' Overflow/Pump to flooded or was pumpted into the transformer yard 1 .OOE-01 O.OOE+Oo High transformer yard, in the past On going -Also during years operating IP-2 Transformer Yard -Turbine hall with known primary to secondary condensate drainage High leakage.U3 RWST base of Hill contaminated Water stream High Source may have been IP-1 leakage IP-3 41' PAB Auxilary Condensate sump pump discharge was aligned to lP-3 41' PAB Sump Pump storm drain system in late 1970's to Dishcharge to storm drain Low early 1980's. Since locked closed.9 9 9 9.1 L £ I.,

1 7- I T-- -I -I-I II.I .. I_________

I __ I __ __ __ _________i i I 1i i i 4 .9 I I 4 8 A .1. A Unit- Site 2 3 tI 1 1 I-r 2 3 2 2 2 1 1 r 2 2 2 2 3 .1 3 -i 3 .4. i 2 3 3 3 2 2 2 3 3 3 2 3 3.I I