ML18142B875

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LER 1975-010-00 for R. E. Ginna, Personnel Error Which Could Prevent Fulfillment of Functional Requirements of Systems Required to Cope with Accidents Analyzed in the SAR
ML18142B875
Person / Time
Site: Ginna Constellation icon.png
Issue date: 06/25/1975
From: White L
Rochester Gas & Electric Corp
To: O'Reilly J
NRC/IE, NRC Region 1
References
LER 1975-010-00
Download: ML18142B875 (6)


Text

X'Ri AI.OGGUitPv.IMAGE AND OR XNGXDENX'R~STRIBUTION FOR PART 50 DOCk,, MATERIAL-(TEMPORARY FOBivl)CONl'0 0:~~FILE.XNCXDENZ REPOPT FXL I FROM.Rochester Gas 8o Electric Rochester N.Y-L D White Jr Mr.O'Reilly 6-25-75 ORIG none, signed.7-2-75 CC OTHER DATE OF DOC DATE R EC'D LTR TWX RPT SFNT AEC PDR SENT LOCAL PDR OTI-IE R CLASS UNC LASS XXXX PROP INFO tNPUT NO CYS REC'D 40 DOCKET NO: 50-2tttt DESCR IPTION Ltr trans the following:

'ACKNO vVLHDGED DO NOT HFMPVE PLANT NAME: RE Ginna ENCLOSURES:

Abnormal.Occurrence Report No.75-.10 on 6-11-75, during safeguard.

valve survei-nce testing the"C" SX pump discharge MOV's 873A and"871j3 were found closed.;.I 40 copies encl rec'd FOR ACTION/INFORMATION BUTLER (L)W/Copies CLARK (L)W/Conies PARR (L)YY/Copies KNI EL (L)W/Copies SCHYYENCEB (L)W/Copies STOLZ (L)W/Copies VASSALLO (L)W/Copies~pUnpi c (L)W/Copies Zl EMAI'JN (L)W/Copies DICKER (E)W/Copies KNIGHTON (E)W/Copies YOUNGBLOOD (E)W/Copies RCGAN (E)W/Copies LEAR (L)W/Copies SPELS W/Copies W/Copies INTEBNAI DIS1'R t BUTION OCNrON~~'G in I MES GAMivll I L KASTI',i E R BALLAf<D SPANGLER ENVI BO MULLER DICKER KNIG I ITQN YOUNG BLOOD BEGAN PROJECT LCB HAH LEss EXTEflrini ois TECH REVIEW~SCHBOEDEB OGC, ROQMi P-506A cAMACCABY GOSSI Cti/STAFF KNIGH1~CASE PAWLICKI GIAMBUSSO Sl-IAO BOYD"-"'~STE L LO MOO f<E (L)=""-~HOUS1'ON DF YOUNG (L)"~'~NOUAK SKOV HOL.I (L)~ROSS GOLLCB (L)(Ltr)~IPPQLITO P.COLLINS/TE OESCO OLNISE J.COL'LXNS RCG OPR LAI NAS<I-ll E K f;FGION (2)BENABOYA~.M>></>>(}~VOLLMEB Sl EELE LtC ASST R.DIGGS (L)H.GEABIN (L)E.GOULBOUBNE (L)P.KBEUTZER (E)J.LEE (L)M.MAIGBET (L)S.BEFD (E)A.sEnvicE (L)S.SHEPPARD{i)M.SLATER (E)H.SMITH (L)S.TEETS (L)G.WILLIAMS (E)V.WILSON (L)B.INGRAM (L)3Ul ION A/T tNO.BBAITiViAN SA LTzrvl AN rvtELTZ PLAN ViCOOix A LO CHAPMAN DUBR (Ltr)E.COUPrE PETE flSQN I.IARTFI C LD (2)w KLECIiEB EISENil IU I'ir I GG li~tTON~F.WXLlXA~IS 0 n1-~1~1 1-1-LOCAL POR Lyons~NY Rochester, NY TIC{ABEBNAI IIY)(l)(2)(10)

-NA~TIONAL LABS NSIC (BUCIIANAN) 1-W.PENNINGTON, Bm C.201 GT ASLB 1-CONSULTANTS Neivlon AA(tersotl NE'(Vie ARK/0 LUM C/AG BABI AN ACBS SE'"L'O LX ST SEND ONLY TEN DAY PZPOHTS qMJ 1-Pon.SAN/LA/r IY 1-BIEOOKIPAVEN NAT LAB 1-G.ULf<It<SON, OBNL.1-AGMED (RUTH GUSSMAN)Brn B-127 GT 1-'.D.liUNKLFS, Rm E.201 I GT 4 l<-~P I C, (p l (~l A l l*t 1'I'h t J Ap'1 J ql~~~t~to~pe'I a E c III'(/'/ŽlA'i~i~!3 Il~i/ur'I!lg ROCHESTER GAS AND ELECTRIC CORPORATION gg/Cj(e JI:.,~/r , 89 EAST AVENUE, ROCHES ER, N.Y.14649 I IAIC LEON D.WHITE, JB.VICE PRESIDENT TEEEI'HONE

'"*REA cooE Tue 546.2700 June 25, 1975 Mr.James P.O'Reilly, Director U.S.Nuclear Regulatory Commission Office of Inspection and Enforcement legion I 631 Park Avenue King of Prussia, Pennsylvania 19406$(.V@qQ s,'IO I~<<EIIt

Subject:

Abnormal Occurrence 75-10, Personnel error which could prevent the fulfillment of the functional requirements of systems required to cope with accidents analyzed in the SAR.R.E.Ginna Nuclear Power Plant, Unit No.1 Docket No.50-244

Dear Mr.O'Reilly:

In accordance with Technical Specifications, Article 6.6.2a, the attached report of Abnormal Occurrence 75-10 is hereby submitted.

Two additional copies of this letter and the attachment are enclosed.Very truly yours, L.D.White, Jr.Attachment cc: Mr.Donald F.Knuth (40)l./,y 8><It+45 iCP~~EE~'c a 1 4

'ON~lOL BLOCK: LICENSEE EVENT REPCPy (PLEASE PRII'4T ALL REQUIRED IMFORPJIATION3 7 89 LICENSEE NAME N Y R R G 1 14 15 LICENSE NUMSER 0 0-0'0 0 0 0-0 0 UCENSE EVENT TYPE TYPE 4 1 1 1 1~01 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMOER~01 cON>~DI~T~L 0 5 0-0 2 4 7 8 57 58 59 60 61 EVENT DATE REPORT DATE 4 0 6 1 1 7 5 0 6 2 5 7 5 68 69 74 75 80 EVENT DESCRIPTION Jog Durin safe uard valve surveillance testin the"C" SI um dischar e MOV's 871A and 7 8 9 80 tOD3]871B were found closed.The two other SI um s on se arate buses were ca able of 7 89 80 toOj4 performing their intended function.Valves were placed to correct open position.Sub-7 8,9 80 Qpg sequently a check was made to verify that all SIS valves were in the proper position.7 8 9[oO~J (Abnormal Occurrence 50-244/75-10)

COMPONENT MANUFACTURER 44 48 7 8 9 PRME SYSTEM CAUSE COMPONENT CODE CODE COMPONENT CODE SUPPUER VIOIATION[oarI~sF~A H 7 8 9 10 11 12 17 43 47 CAUSE DESCRIPTION l00m Incorrect position of the valves was due to operator error during safety injection pump 80 80 7 8 9 I 80~09 monthly surveillance testing.Measures to prevent recurrence are on attached page.7 8 9~10 7 89 FACIUTY STATUS POWER Qg~z~os o OTHER STATUS NA AMOUNT OF ACTIVITY 7 8 9 10 11 PERSONNEL EXPOSURES 7 8'10 12 13 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE gg H~p METHOD OF DISCOVERY b 44, 45 46 44 45 NA DISCOVERY DESCRIPTION NA LOCATION OF RELEASE 80 80 80 80 7 89 11 12 13 PERSONNEL IN JURIES NUMBER DESCRIPTION

~00 0 7 89 11 12 OFFSITE CONSEQUENCES NA 80 80 7 8 9 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION

~16 P, 7 89 10 PUBLICITY 7 8 9 NA NA 80 80 80 ADDITIONAL FACTORS Q~g In the event of safeguards actuation, all 3 50%capacity SI pumps are automatically 7 89 80~qg started in a timed sequence, and', in case one of the other (cont'd.on attached page)7 89 NAME.Bruce A.Snow 80 PHDNEI 716-546-2700, ext.291-214 GFO 881~667 Licgnsee Event Rep.50-244/'05-10 Measures to Prevent Recurrence:

The operator involved was reprimanded for his error.The procedure used during error committal was reviewed and no inadequacies were noted in the procedure.

However, a procedure change was reviewed by the Plant Operations Review Committee and was recommended for approval on June 23, 1975 to eliminate procedural options relative to the operation of MOV-.871A and MOV-871B.In addition, the Operations Engineer has issued a memorandum to all operators to once again impress upon them the importance.

of adhering to procedures, and stressed the importance of verification of status lights on safeguards equipment when assuming control board duties.Additional Factors cont'd.)2 SI pumps fails to start, one of the"C" SI pump discharge MOV's will automatically close to direct flow to the affected loop.Emergency Procedure E-1.1, Safety Injection Actuation, directs operators to observe measured variables and status indicators to verify proper automatic actions, and to perform any necessary actions manually.In doing so, if either"A" or"B" SI pump were to fail to start, the required manual action would be performed to provide flow to the affected loop from the"C" pump, namely to open the appropriate MOV.