ML18085B096

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LER 81-007/01X-1:on 810119,throttling Valves 14SJ16,11SJ138, 12SJ138 & 13SJ138 Found Out of Position.Caused by Procedure Inadequacy & Personnel Error.Valves Moved to Correct Positions & Procedures Changed
ML18085B096
Person / Time
Site: Salem PSEG icon.png
Issue date: 03/20/1981
From: STEELE W J
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18085B095 List:
References
LER-81-007-01X, LER-81-7-1X, NUDOCS 8103310632
Download: ML18085B096 (1)


Text

il-l 1 J ... 'f ... LICENSEE EVENT REPORT CONTROL BLOCK:

6 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION!

[iliJ IN !J Is I GI sl1 101 al al -I al al al al ol-1 al alG)l4I1l 1l 1l 1l©I I 10 7 :: 9 LICENSEE CODE 14 I& LICENSE NUMBER 2& 26 LICENSE TYPE JO &7 CAT SB *coN'T IillJ 7 B [ill] IIIIl [ill] ITIII ITID L1J© I a I s I a I a I a I 2 I 1 I 2 101 o I 1 I 1 I 9 I a I 1 I© I a I 60 61 DOCKE1' '.!UMBER . 66 :,!i9 EVE"IT DATE 74 75 EVENT DESCRIPTION AND PROBABLc CONSEQUENCES@

11 2 I al REPOR1' DATE a ,10 80 I While in the Hot Standby condition on 1/19/81 at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />,. the NRC Resident Inspect tor requested that the throttle valves which balance flow thru the Safety Injection I Loops be inspected to verify that they were all in their required positions.

va"lve4 14SJ16,11SJ138,12SJ138

& 13SJ138 were not in their correct positions.

The incor-rectly positioned valves may have prevented the fulfillment of the functional

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__ s_A_R_. ______ ___, ITTIJ 7 8 9 Jill] 7 B SYSTEM CODE Is IF I@ 9 10 CAUSE CAUSE CODE SUBCODE L!Ll@ UJ@ 11 12 COMPONENT CODE I v I A I LI v I E I x 1@ 13 18 SEQUENTIAL OCCURRENCE LE R RO LVEN1' YE.AR REPORT NO. CODE Is I i 1 I I I o I o I 11 I ......-1 Io 11 I 21 22 23 24 26 2 7 28 29 COMP. SUBCOOE L!J 19 RE FORT TYPE 30 VALVE SUBCOOE w@ 20 L=l 31 ACTION FUTURE EFFECT SHU1'00Wi'<

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ATTACHMENT NPRD-4 PRIME COMP. SUPPLIER REv1s1m. NC. L2:J 32 COMPONEN1' MANUFACTURER BO TAKEN ACTION ON PLANT METHOD HOURS SUBMITTED FORM :.UB. W@W@ UJ(§) W I 01010101 L!J@ W@) 33 34 35 36 37 40 41 42 , IR I 3 I 4 I 0 I@ l.EJ@ CAUSE DESCRIPTION AND CORRECTIVE ACTIONS @ 43 44 47 IJ::]]J I This event was the result of procedure inadequacy.

To insure that all the valves in this system are returned to their exact required positions following any IIIIJ evolution requiring a valve line-up, on-the-spot changes have been made to the IIIIJ LI a::.t=e...A.p;:;r.;;o..;:c;.;:e;.;:d:.;;u;.;r;.;e::.:s;;..;...

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_____________________ ...... 7 8 9 FACILITY IJQ\ STATUS % POWER OTHER STATUS \:::::; EJil W@ I ol ol ol@ .... I __ N..._/A __ _ 8 9 10 12 11 ACTIVITY CONTENT Q\ RELEASED OF RELEASE AMOUNT OF ACTIVITY IJJil l2J@ L!J@I N/A 7 8 9 10 11 7 80 METHOD OF DISCOVERY DESCRIPTION

@ DISCOVERY W@I Special Inspection 44 45 46 80 LOCATION OF RELEASE @ N/A 44 45 80 PERSONNEL EXPOSURES

  • r.:;::., NUMBER (':;':;\TYPE DESCRIPTION IITIJ I ol al
  • NA 7 8 9 . 11 121 PERSONNEL INJURIES t::;'\ NUMBER DESCRIPTION6 ITIIJ I 0 I a I 0 l@.___ ____

_____________________

..... 7 B 9 11 12 BO LOSS Of OR DAMAGE TO TYPE DESCRIPTION EE W@ NA 1 0 9 ___________

....:.;.'-=...;_---------------------------------------__.

9 0 PUBLICITY Q\ NAC USE ONLY ., ISSUEOC,;\

l1TIJ UU6 N A I I I I I I I I I I I 7 B 9 1 ..

69 I" I . ! NAME W. J. Steele OFPREPAREA--------------...,..---------

  • S"l 0 3 310'13-2 80 c; 0 Q. PHONE: __ 6_0_9_-_9_3_s_-_a_9_9s

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