Semantic search

Jump to navigation Jump to search
Condition
Printout selection
Options
Parameters [
limit:

The maximum number of results to return
offset:

The offset of the first result
link:

Show values as links
headers:

Display the headers/property names
mainlabel:

The label to give to the main page name
intro:

The text to display before the query results, if there are any
outro:

The text to display after the query results, if there are any
searchlabel:

Text for continuing the search
default:

The text to display if there are no query results
class:

An additional CSS class to set for the table
transpose:

Display table headers vertically and results horizontally
sep:

The separator between results
prefix:

Control display of namespace in printouts
Sort options
Delete
Add sorting condition
 Issue dateTitleTopic
PNO-III-80-032, on 800219,correspondents from ABC 20/20 Program Will Interview Regional Director & Other Members Re NRC Investigation Into Allegations of Falsification of Qualification Records of Personnel Doing Design Work19 February 1980PNO-III-80-032:on 800219,correspondents from ABC 20/20 Program Will Interview Regional Director & Other Members Re NRC Investigation Into Allegations of Falsification of Qualification Records of Personnel Doing Design Work
PNO-III-80-054, on 800318,licensee Informed Region 3 That Channel 7 News in Detroit,Mi Plans to Televise 800321 Interview W/Site Contractor Employees Re Allegations of Improper Receipt Insp of Small Bore Pipe19 March 1980PNO-III-80-054 :on 800318,licensee Informed Region 3 That Channel 7 News in Detroit,Mi Plans to Televise 800321 Interview W/Site Contractor Employees Re Allegations of Improper Receipt Insp of Small Bore Pipe
PNO-III-85-050, on 850621,initial Criticality Achieved within Two Steps of Estimated Critical Position.Control Rods Withdrawn to Criticality21 June 1985PNO-III-85-050:on 850621,initial Criticality Achieved within Two Steps of Estimated Critical Position.Control Rods Withdrawn to Criticality
PNO-III-85-055, on 850709,reactor Tripped on Low Water Level. Caused by Operator Inattentiveness to Level Indicator.No ECCS Injection Occurred10 July 1985PNO-III-85-055:on 850709,reactor Tripped on Low Water Level. Caused by Operator Inattentiveness to Level Indicator.No ECCS Injection OccurredReactor Vessel Water Level
PNO-III-85-058, on 850702,reactor Brought to Criticality W/O Shift Supervisor Realizing Incident.Caused by Reactor Operator Failing to Follow Proper Procedures for Moving Control Rods in Full Out Position.Incident Being Reviewed15 July 1985PNO-III-85-058:on 850702,reactor Brought to Criticality W/O Shift Supervisor Realizing Incident.Caused by Reactor Operator Failing to Follow Proper Procedures for Moving Control Rods in Full Out Position.Incident Being Reviewed
PNO-III-85-058A, on 850716,confirmatory Action Ltr Issued Documenting Util Commitment to Restrict Power Level to 5%, Pending Completion of Evaluation of 850702 Inadvertent Criticality Incident.Investigation Continuing17 July 1985PNO-III-85-058A:on 850716,confirmatory Action Ltr Issued Documenting Util Commitment to Restrict Power Level to 5%, Pending Completion of Evaluation of 850702 Inadvertent Criticality Incident.Investigation Continuing
PNO-III-85-063, on 850723,reactor Shut Down to Repair Thrust Bearing Housing on Feedwater Pump,Damaged During 850722 Demonstration Testing.Further Exam Underway24 July 1985PNO-III-85-063:on 850723,reactor Shut Down to Repair Thrust Bearing Housing on Feedwater Pump,Damaged During 850722 Demonstration Testing.Further Exam Underway
PNO-III-85-063A, investigation Concluded That Vibration in South Reactor Feeder Pump Turbine,Plus Inadequate Securing of Outboard Bearing Cap Caused Turbine Failure.Study of Problem Continuing5 August 1985PNO-III-85-063A:investigation Concluded That Vibration in South Reactor Feeder Pump Turbine,Plus Inadequate Securing of Outboard Bearing Cap Caused Turbine Failure.Study of Problem Continuing
PNO-III-85-066, on 850729,low Svc Water Flow Alarm Received During Surveillance Testing of Div I Diesel Generator. Generator Manually Tripped.Caused by Closed Bypass Valve in Line Returning Water to Reservoir.Investigation Underway30 July 1985PNO-III-85-066:on 850729,low Svc Water Flow Alarm Received During Surveillance Testing of Div I Diesel Generator. Generator Manually Tripped.Caused by Closed Bypass Valve in Line Returning Water to Reservoir.Investigation Underway
PNO-III-85-067, on 850730,licensee Announced That Low Power Testing Would Not Resume Until Various Equipment & Procedural Difficulties Resolved.Shutdown Caused by Premature Criticality on 85070231 July 1985PNO-III-85-067:on 850730,licensee Announced That Low Power Testing Would Not Resume Until Various Equipment & Procedural Difficulties Resolved.Shutdown Caused by Premature Criticality on 850702
PNO-III-85-067A, on 850809,licensee Will Resume Low Power Testing.Region III Approved Util Corrective Action Program Submitted on 850807,in Response to 850702 Premature Criticality.Plant Still Restricted to 5% Power9 August 1985PNO-III-85-067A:on 850809,licensee Will Resume Low Power Testing.Region III Approved Util Corrective Action Program Submitted on 850807,in Response to 850702 Premature Criticality.Plant Still Restricted to 5% Power
PNO-III-85-070, on 850806,Monroe County Board of Commissioners Requested Full Investigation of Operational Procedures & Employee Credentials Due to 850702 Unplanned Criticality Not Reported to NRC Until 8507158 August 1985PNO-III-85-070:on 850806,Monroe County Board of Commissioners Requested Full Investigation of Operational Procedures & Employee Credentials Due to 850702 Unplanned Criticality Not Reported to NRC Until 850715
PNO-III-85-076, on 850825,recirculation Pump B Problem Resulted in Brief Power Increase from 2.9 to 8.8%.Reactor Operators Tripped Pump After Failing to Reduce Pump Speed. Testing Disclosed No Problems W/Speed Control Circuitry26 August 1985PNO-III-85-076:on 850825,recirculation Pump B Problem Resulted in Brief Power Increase from 2.9 to 8.8%.Reactor Operators Tripped Pump After Failing to Reduce Pump Speed. Testing Disclosed No Problems W/Speed Control Circuitry
PNO-III-85-077, on 850904,leak Rate Test Connection Valve Installed on 850620 in Containment Sampling Sys Found Open & Attached Line Uncapped,Due to Unrevised Containment Valve Lineup Procedure.Valve Closed5 September 1985PNO-III-85-077:on 850904,leak Rate Test Connection Valve Installed on 850620 in Containment Sampling Sys Found Open & Attached Line Uncapped,Due to Unrevised Containment Valve Lineup Procedure.Valve Closed
PNO-III-85-083, on 850917,leak Observed in East Steam Bypass Line.Transient Power Spike Observed While Attempting to Isolate Line & Open Valve.Cause of Transient Not Determined. Cracked Piping Around Valve Under Investigation19 September 1985PNO-III-85-083:on 850917,leak Observed in East Steam Bypass Line.Transient Power Spike Observed While Attempting to Isolate Line & Open Valve.Cause of Transient Not Determined. Cracked Piping Around Valve Under Investigation
PNO-III-85-095, on 851113,unusual Noise & Vibration Observed in Emergency Diesel Generator.Operator Manually Tripped Diesel.Preliminary Evaluation Indicates Damage to Connecting Rod Bearing for Upper Crankshaft & Upper Piston Skirt14 November 1985PNO-III-85-095:on 851113,unusual Noise & Vibration Observed in Emergency Diesel Generator.Operator Manually Tripped Diesel.Preliminary Evaluation Indicates Damage to Connecting Rod Bearing for Upper Crankshaft & Upper Piston Skirt
PNO-III-85-095A, on 851201,during Reassembly of Steam Generator 13,discontinuities Observed on Three Connecting Rod Journals.Vendor Will Supply Documentation.Investigation Continuing.Startup Projected for 8512113 December 1985PNO-III-85-095A:on 851201,during Reassembly of Steam Generator 13,discontinuities Observed on Three Connecting Rod Journals.Vendor Will Supply Documentation.Investigation Continuing.Startup Projected for 851211
PNO-III-85-095B, during Insp of Emergency Diesel Generator 11,degradation of Six Upper Crankshaft Bearings Noted.Cause Undetermined.Findings & Relation of Findings to Other Diesel Generators Being Evaluated4 December 1985PNO-III-85-095B:during Insp of Emergency Diesel Generator 11,degradation of Six Upper Crankshaft Bearings Noted.Cause Undetermined.Findings & Relation of Findings to Other Diesel Generators Being Evaluated
PNO-III-85-095C, on 851212,diesel Generator 14 Tripped on Low Lube Oil Pressure During Test Run.Bearing Failure & Erratic Behavior of Svc Water Pump Under Investigation as Possible Causes.Generator Will Be Monitored12 December 1985PNO-III-85-095C:on 851212,diesel Generator 14 Tripped on Low Lube Oil Pressure During Test Run.Bearing Failure & Erratic Behavior of Svc Water Pump Under Investigation as Possible Causes.Generator Will Be Monitored
PNO-III-85-095D, on 851113,bearing Damage Occurred to Diesel Generators 13,11 & 14.Caused by Insufficient break-in Period.Bearing Replacement Required for Diesel Generator 11. Decrease in Lubricating Oil Viscosity Noted for 12 & 1424 December 1985PNO-III-85-095D:on 851113,bearing Damage Occurred to Diesel Generators 13,11 & 14.Caused by Insufficient break-in Period.Bearing Replacement Required for Diesel Generator 11. Decrease in Lubricating Oil Viscosity Noted for 12 & 14
PNO-III-85-098, on 851117,between 17,000 & 35,000 Gallons of Radioactive Water Released from Ruptured Seam in Condensate Storage Tank.Water Radioactivity Less than 0.4% of Regulatory Limit for Offsite Release18 November 1985PNO-III-85-098:on 851117,between 17,000 & 35,000 Gallons of Radioactive Water Released from Ruptured Seam in Condensate Storage Tank.Water Radioactivity Less than 0.4% of Regulatory Limit for Offsite Release
PNO-III-86-004, RHR Pump Motor Removed Offsite for Testing & Insp Following 851125 Failure Due to Mfg Defect.Pump Replaced.Generic Implications Under Investigation23 January 1986PNO-III-86-004:RHR Pump Motor Removed Offsite for Testing & Insp Following 851125 Failure Due to Mfg Defect.Pump Replaced.Generic Implications Under Investigation
PNO-III-86-008, on 860125,roving Fire Watch Discovered Burning Insulation on Exhaust Line of Emergency Diesel Generator 13.Caused by Oil Soaking Insulation During Prior Disassembly & Oil Flushing.Fire Extinguished.Leak Repaired27 January 1986PNO-III-86-008:on 860125,roving Fire Watch Discovered Burning Insulation on Exhaust Line of Emergency Diesel Generator 13.Caused by Oil Soaking Insulation During Prior Disassembly & Oil Flushing.Fire Extinguished.Leak RepairedFire Watch
PNO-III-86-024, on 860317,backup Reactor Protection Sys Trip Breaker Failed to Trip During Bus a Transfer from Primary Electrical Supply.Caused by Repeated Testing.Manual Scram Inserted.Investigation Underway17 March 1986PNO-III-86-024:on 860317,backup Reactor Protection Sys Trip Breaker Failed to Trip During Bus a Transfer from Primary Electrical Supply.Caused by Repeated Testing.Manual Scram Inserted.Investigation Underway
PNO-III-86-037, on 860418,util Announced Extension of Outage to mid-Jul 1986.Licensee Review of Reevaluation of Design Work Performed on Concrete Embedments & Pipe Supports Will Be Completed by 86050118 April 1986PNO-III-86-037:on 860418,util Announced Extension of Outage to mid-Jul 1986.Licensee Review of Reevaluation of Design Work Performed on Concrete Embedments & Pipe Supports Will Be Completed by 860501
PNO-III-86-067, on 860708,Monroe County Board of Commissioners Adopted Resolution,By 5 to 3 Vote,Requesting Congressman Dingell to Hold Hearings on Adequacy of GE Mark 1 Containment9 July 1986PNO-III-86-067:on 860708,Monroe County Board of Commissioners Adopted Resolution,By 5 to 3 Vote,Requesting Congressman Dingell to Hold Hearings on Adequacy of GE Mark 1 Containment
PNO-III-86-069, on 860715,full Scram & ECCS Actuation Occurred During Heatup of Reactor Pressure Vessel.Approx 10 Gallons of Water Injected Into Vessel.Caused by Pressure Spike from Flow Perturbation.State of Mi Informed16 July 1986PNO-III-86-069:on 860715,full Scram & ECCS Actuation Occurred During Heatup of Reactor Pressure Vessel.Approx 10 Gallons of Water Injected Into Vessel.Caused by Pressure Spike from Flow Perturbation.State of Mi InformedHydrostatic
PNO-III-86-074, on 860731,licensee Authorized to Resume Operation Up to 5% Power.Further NRC Authorization Required for Higher Power Levels.Startup Will Begin on 8608011 August 1986PNO-III-86-074:on 860731,licensee Authorized to Resume Operation Up to 5% Power.Further NRC Authorization Required for Higher Power Levels.Startup Will Begin on 860801
PNO-III-86-074A, on 860804,start Up Initiated W/Removal of Control Rods.Activities Postponed from 860801 for Repair of Bypass Valve.Problem W/Position Indicators for MSIVs Also Corrected4 August 1986PNO-III-86-074A:on 860804,start Up Initiated W/Removal of Control Rods.Activities Postponed from 860801 for Repair of Bypass Valve.Problem W/Position Indicators for MSIVs Also Corrected
PNO-III-86-077, on 860806,fire & Electric Overload Alarm Received.Fire Located in Cubicle Containing Power Supply Breaker.Cause Unknown.Fire Extinguished.Power Supply Breaker & Affected Motor Control Ctr Inspected7 August 1986PNO-III-86-077:on 860806,fire & Electric Overload Alarm Received.Fire Located in Cubicle Containing Power Supply Breaker.Cause Unknown.Fire Extinguished.Power Supply Breaker & Affected Motor Control Ctr Inspected
PNO-III-86-083A, on 860828,nine NRC Licensing Examiners Completed Simulator Portion of Requalification Exams.All Nine Passed Exams.Licensee Requalification Program for Licensed Operators Acceptable29 August 1986PNO-III-86-083A:on 860828,nine NRC Licensing Examiners Completed Simulator Portion of Requalification Exams.All Nine Passed Exams.Licensee Requalification Program for Licensed Operators Acceptable
PNO-III-86-088, on 860902,normal Plant Shutdown Began for Repair of Malfunctioning torus-to-reactor Bldg Vacuum Breaker Isolation Valve.Repair Effort Expected to Take More than 48 H.Addl Maint Will Be Conducted During Shutdown3 September 1986PNO-III-86-088:on 860902,normal Plant Shutdown Began for Repair of Malfunctioning torus-to-reactor Bldg Vacuum Breaker Isolation Valve.Repair Effort Expected to Take More than 48 H.Addl Maint Will Be Conducted During Shutdown
PNO-III-86-097, on 860912,authorization Granted to Increase Power Level to 20%.Power Escalation Expected This Wk.Power Increase Previously Recommended for 86091015 September 1986PNO-III-86-097:on 860912,authorization Granted to Increase Power Level to 20%.Power Escalation Expected This Wk.Power Increase Previously Recommended for 860910
PNO-III-86-106, on 860926,suspicious Device Found on Hatch Cover on Fourth Floor of Auxiliary Bldg.Bomb Disposal Specialists Investigated Device & Found Device Empty.Device Was Piece of Pipe Placed on Hatch by Maint Personnel26 September 1986PNO-III-86-106:on 860926,suspicious Device Found on Hatch Cover on Fourth Floor of Auxiliary Bldg.Bomb Disposal Specialists Investigated Device & Found Device Empty.Device Was Piece of Pipe Placed on Hatch by Maint Personnel
PNO-III-86-111, on 861005,reactor Manually Scrammed from 15% Power Due to Partial Loss of Vacuum in Condenser Causing Temp Increase.Also,On 861005,during Test of Water Level Transmitters,Pressure Spike Inadvertently Introduced8 October 1986PNO-III-86-111:on 861005,reactor Manually Scrammed from 15% Power Due to Partial Loss of Vacuum in Condenser Causing Temp Increase.Also,On 861005,during Test of Water Level Transmitters,Pressure Spike Inadvertently Introduced
PNO-III-86-112, on 861009,problem Occurred W/Rod Sequence Control Sys,Hindering Normal Manual Insertion of Control Rods.Caused by Low Voltage in Normal Power Supply.Evaluation of Problem Underway10 October 1986PNO-III-86-112:on 861009,problem Occurred W/Rod Sequence Control Sys,Hindering Normal Manual Insertion of Control Rods.Caused by Low Voltage in Normal Power Supply.Evaluation of Problem Underway
PNO-III-86-118, on 861023,licensee Demonstrated Remote Shutdown Capability.Demonstration Successful W/All Equipment Operating as Designed.Plant Control Returned to Control Room After 45 Minutes.Plant in Cold Shutdown for Scheduled Maint24 October 1986PNO-III-86-118:on 861023,licensee Demonstrated Remote Shutdown Capability.Demonstration Successful W/All Equipment Operating as Designed.Plant Control Returned to Control Room After 45 Minutes.Plant in Cold Shutdown for Scheduled Maint
PNO-III-86-125, on 861031,operator Inadvertently Skipped Step in Rod Withdrawal Procedure & Pulled Next Rod in Sequence Out One Notch (6 Inches).Rod Reinserted to Proper Position & Correct Rod Sequence Restored31 October 1986PNO-III-86-125:on 861031,operator Inadvertently Skipped Step in Rod Withdrawal Procedure & Pulled Next Rod in Sequence Out One Notch (6 Inches).Rod Reinserted to Proper Position & Correct Rod Sequence Restored
PNO-III-86-131, on 861107,unit Shut Down Due to Air Leakage Into Main Condenser.Caused by Leakage in Thermal Expansion Joint Between One Low Pressure Turbine & Main Condenser. Licensee Plans to Inspect Remaining Joints10 November 1986PNO-III-86-131:on 861107,unit Shut Down Due to Air Leakage Into Main Condenser.Caused by Leakage in Thermal Expansion Joint Between One Low Pressure Turbine & Main Condenser. Licensee Plans to Inspect Remaining Joints
PNO-III-86-131A, 4-ft Tear Identified in North Condenser Boot During Repairs to Condenser Thermal Expansion Boots.Caused by Structural Damage to Condenser Supports.North & Ctr Condenser Thermal Expansion Boots Replaced14 November 1986PNO-III-86-131A:4-ft Tear Identified in North Condenser Boot During Repairs to Condenser Thermal Expansion Boots.Caused by Structural Damage to Condenser Supports.North & Ctr Condenser Thermal Expansion Boots Replaced
PNO-III-86-136, on 861117,283,000 Gallons of Water Lost from Condensate Storage Tank Following Maint on Valve.Caused by Breaking of Weld to HPCI Test Return Pipe.Radwaste Spill Occurred During Transfer of Spilled Water18 November 1986PNO-III-86-136:on 861117,283,000 Gallons of Water Lost from Condensate Storage Tank Following Maint on Valve.Caused by Breaking of Weld to HPCI Test Return Pipe.Radwaste Spill Occurred During Transfer of Spilled Water
PNO-III-86-148, on 861217,guns,knives,ammunition & Marijuana Found in Possession of Truck Driver Seeking Entrance to Protected Area.Driver Denied Access & Arrested by State Police.Driver Involved W/Paramilitary Organization for Hire17 December 1986PNO-III-86-148:on 861217,guns,knives,ammunition & Marijuana Found in Possession of Truck Driver Seeking Entrance to Protected Area.Driver Denied Access & Arrested by State Police.Driver Involved W/Paramilitary Organization for Hire
PNO-III-87-001, on 870102,three Small Steam Leaks Discovered on Two of Four Main Steam Lines.During Power Reduction for Shutdown,Main Turbine Tripped on 18% Power.Cause Under Investigation.Instrument Lines Will Be Temporarily Plugged2 January 1987PNO-III-87-001:on 870102,three Small Steam Leaks Discovered on Two of Four Main Steam Lines.During Power Reduction for Shutdown,Main Turbine Tripped on 18% Power.Cause Under Investigation.Instrument Lines Will Be Temporarily Plugged
PNO-III-87-001A, on 870102,licensee Discovered Three Small Steam Leaks on Two of Four Main Steam Lines & on 870105, Following Repairs & Return of Steam Lines to Svc,Cracked Weld on Instrument Line/Valve Connection Found6 January 1987PNO-III-87-001A:on 870102,licensee Discovered Three Small Steam Leaks on Two of Four Main Steam Lines & on 870105, Following Repairs & Return of Steam Lines to Svc,Cracked Weld on Instrument Line/Valve Connection Found
PNO-III-87-001B, on 870108,normal Plant Shutdown Commenced to Repair Series of Small Steam Leaks on Main Steam Piping Attachments.Leak Located on Main Turbine Stop Valve 3 & Can Only Be Isolated by Closing MSIVs8 January 1987PNO-III-87-001B:on 870108,normal Plant Shutdown Commenced to Repair Series of Small Steam Leaks on Main Steam Piping Attachments.Leak Located on Main Turbine Stop Valve 3 & Can Only Be Isolated by Closing MSIVs
PNO-III-87-009, on 870114,Safe Energy Commission of Michigan (Sec) Announced Results of Investigation Into Licensee Safeteam Program.Rept Contends Safeteam Program Failure.Sec Plans to File 2.206 Petition W/Nrc14 January 1987PNO-III-87-009:on 870114,Safe Energy Commission of Michigan (Sec) Announced Results of Investigation Into Licensee Safeteam Program.Rept Contends Safeteam Program Failure.Sec Plans to File 2.206 Petition W/Nrc
PNO-III-87-012, on 870123,licensee Informed Region That NRC- Licensed Nuclear Supervising Operator Suspended on 870122 Due to Positive Testing in Random Drug Screening on 870115. No Evidence of Error Found in Performance26 January 1987PNO-III-87-012:on 870123,licensee Informed Region That NRC- Licensed Nuclear Supervising Operator Suspended on 870122 Due to Positive Testing in Random Drug Screening on 870115. No Evidence of Error Found in PerformanceFitness for Duty
PNO-III-87-016, on 870129,small Steam Leak Discovered in Spare Instrument Line Attached to Body of West Main Steam Bypass Valve.Caused by Crack in Weld Attaching Valve to Instrument Line.Valves Cut Off & Instrument Lines Plugged30 January 1987PNO-III-87-016:on 870129,small Steam Leak Discovered in Spare Instrument Line Attached to Body of West Main Steam Bypass Valve.Caused by Crack in Weld Attaching Valve to Instrument Line.Valves Cut Off & Instrument Lines PluggedFlow Induced Vibration
PNO-III-87-022, on 870216,Region III Authorized Facility to Exceed Previous 20% Power Limitation & Continue Testing Activities Up to 50% Power.Power Escalation Expected Pending Restoration of HPCI to Operable Status17 February 1987PNO-III-87-022:on 870216,Region III Authorized Facility to Exceed Previous 20% Power Limitation & Continue Testing Activities Up to 50% Power.Power Escalation Expected Pending Restoration of HPCI to Operable Status
PNO-III-87-022A, on 870308,plant Reached NRC Imposed Limit of 50% Power.Licensee Will Operate Plant at Approx 50% While Conducting Test on HPCI Sys,Rwcu Sys & Safety Relief Valves. Util Also Plans to Conduct Loss of Offsite Power Test9 March 1987PNO-III-87-022A:on 870308,plant Reached NRC Imposed Limit of 50% Power.Licensee Will Operate Plant at Approx 50% While Conducting Test on HPCI Sys,Rwcu Sys & Safety Relief Valves. Util Also Plans to Conduct Loss of Offsite Power Test