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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141A5021997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Oyster Creek Nuclear Generating Station ML20141H7441997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Oyster Creek Nuclear Generating Station ML20137X8231997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Oyster Creek Nuclear Generating Station ML20137C3771997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Ocnpp ML20134P6151997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Oyster Creek Nuclear Generating Station ML20133M1751996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Oyster Creek Nuclear Generating Station ML20132D1011996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Oyster Creek Nuclear Generating Station ML20134M9761996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Oyster Creek Nuclear Generating Station ML20129B1631996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Oyster Creek Nuclear Generating Station ML20117M7561996-08-31031 August 1996 Monthly Operating Rept for Aug 1996 for Oyster Creek Nuclear Generating Station ML20116M6761996-07-31031 July 1996 Monthly Operating Rept for Jul 1996 for Oyster Creek Nuclear Generating Station ML20115F8561996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Oyster Creek Nuclear Generating Station ML20112J7431996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Oyster Creek Nuclear Generating Station ML20112A6891996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Oyster Creek Nuclear Generating Station ML20101R0401996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for Oyster Creek Station ML20101D7701996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for Ocnpp ML20100G5101996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for Oyster Creek Nuclear Generating Station ML20096E8071995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Oyster Creek Nuclear Generating Station ML20099L7571995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Oyster Creek Nuclear Generating Station ML20094P8431995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Oyster Creek Nuclear Generating Station ML20093H3571995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Oyster Creek Nuclear Generating Station ML20092H7741995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for Oyster Creek Nuclear Generating Station 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
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AVERAGE DAILY POWER LEVEL DOCKET ?...... 50-219
' UNIT.......... O. C. ?1 REPORT DATE... March 12, 1979 COMPILED BY... C.M. MCCLAIN TELEPHONE..... 201-455-8748 MONTH February 1979 DAY MW DAY MW
- 1. 649. 17. 649.
- 2. 649. 18. 649.
- 3. 649. 19. 647.
- 4. 649. 20. 648.
- 5. 648. 21. 648.
- 6. 299. 22. 649.
- 7. 328. - 2 3 ., 640.
O. 629, 24. 649.
9 604. 25, 649.
- 10. 647. 26. 649.
ii, 640, 27 649.
- 12. 649. 20. 649.
- 13. 642.
- 14. 531.
- 15. 650.
- 16. 647.
7903210102_
OPERATING DATA REPORT OPERATING STATUS UNIT NAME.. 0YSTER CREEK DOCKET NUMBER.. 50-219 UTILITY DATA PREPARED BY...C.M. MCCLAIN 201-455-8748 REPORTING PERIOD... February 1979 LICENSED THERtiAL POWER (MWT)...i930 NAMEPLATE RATING (GROSS MWE).. 650 DESIGN ELECTRICAL RATING (NET MWE).. 650 MAXIMUM DEPENDADLE CAPACITY (GROSS MWE).. 650 MAXIhUN DEPENDABLE CAPACITY (NET MWE).. 620 IF CHANGES OCCUR IN CAPACITY RATING SINCE LAST REPORT, GIVE REASON...
NONE POWER LEVEL TO WHICH RESTRICTED, IF ANY< NET MUE)... NO RESTRICTION REASON FOR RESTRICTION, IF ANY...
NO RESTRICTION MONTH YEAR CUnULATIVE HOURT IN PERIOD 672.0 1 4 1 6 ., 0 80520.0 HOUR ' FW CRITICAL 660.7 1330.0 6235i.9 R RE!ERVE SHUTDOMN HRS. 0.0 0.0 168.2 HR . GEN ON LINE 655,5 ,6i3.4 61094 ~7 UT RESERVE SHUTDOUN HRS 0.6 00 0.0 GROSS T HERMAL Et!ERGY 1238169.0 2478875.5 102514870.5 GROSS ELEC ENERGY 431000.0 860390.0 35000395.0 NET ELEC ENERGY 4163(?1.0 8291Si.0 3374694i.0 UT SERVICE F' ACTOR 97.5 (?2.8 75.9 UT AVAILADILITY FACTOR (77.5 92.0 '75.9 UT CAPACITY FACTOR tiDC 99.9 o4.4 69.5 UT CAPACITY FACTOR DER 95.3 90.1 64.5 FORCED OUTAGE FACTOR 2.5 7.2 5.4 NO OUTAGE IS SCHEDULED OVER THE NEYT l' I X MONTHS
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DOCK ET NO.
50-219 UNIT SilUTDOWNS AND POWER REDUCTIONS UNIT N AME Oyster Creek #1 DATE Mar'ch 12, 1979 -
COMPLETED BY C. H. McClain REPORT MONTII February 1979 TELEPl!ONE 201-455-8748 9.
No . Dat e g
.5E 3g 3
@ jg5 E Licensee Esent 5-r,
- g h
o- 3 Cause & Corrective Action to H
$E 5 j@g Report : NU h' Prevent Recurrence 6
2 790206 F 16.5 G 3 NA CH RELAYX "C" feedwater pump tripped when the breaker cubicle door was closed, shaking the "C" di f ferential relay.
The scram occurred from a low water level after the pump trip.
I 2 3 4 F: Forced Reason: Method: Exhibit G . Instructions S: Scheduled A. Equipment Failure (Explain) 1 Manual for Preparation of Data B-Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee C Refueling 3 Automatic Scram. Event Report (LE R) File (NUREG-D Regulatory Restriction 4 Other (Explain) 0161)
E-Operator Training & License Exannnation F Administralise 5 G-Operational I.i ror ( E xplain ) Exhibit I- Same Source 19/77) Il-Ot he r ( E xplain)
Oyster Creek Station #1 -
Docket No. 50-219 OPERATIONS Sl WARY - FEBRUARY 1979 The unit was operating at full load at the beginning of this report period.
On February 6,1979, "C" feedwater pump tripped when the breaker cubicle door was closed, shaking the "C" differential relay. A reactor scram occurred at 11:15 a.m. frcm low water level following the feedwater pump trip. All systems functioned normally. The unit was returned to service at 3:41 a.m. on February 7.
On February 9, poaer level was reduced frca rated load to approximately 35% when condenser vacuum rapidly decreased. Steam jet air ejector 1C1 was shutdown and IC2 was started. Ioad was increased to rated.
On February 13, power was reduced to approximately 65% to insert control rod 34-39 and replace a leaking scram pilot solenoid valve. Power was increased to rated following withdrawal of rod 34-39.
Two (2) reportable occurrences were identified during the tronth:
RO 79-2 occurred on Febnary 6 when one (1) reactor high pressure switch for isolation condenser initiation tripped above the allowable setpoint during routine surveillaire testing.
RO 79-3 occurred on Febnary 26, 1979 when the drywell to torus differential pressure dropped below the technical specification limit for 10 minutes during a reactor building closed cooling water tenperature transient.
Oyster Creek Station #1 Docket No. 50-219 ,,
CORIiECTIVE INSTRUIEETF MAltIIDIANCE ON OASL ITEMS FOR THE MotTI11 OF FEBICARY 1979 Item # Equipnent Malfunction Corrective Action 1 APal Ch. 6 Upscale spiking causing half- Bypassed 12-41B in APIN scrams drawer and aux, drawer 2 CRD 34-39 Scram solenoid air leak Rebuilt scram pilot valves with new parts and tested 3 APM1 Ch. 4 Rod block from faulty diode Replaced diode and conducted APIN surveillance test & cal.
4 SIN Front Panel ICR meter out of spec Mjusted trip module and zeroed DC amp for 10-1 on zero position 5 'D' Recirc Pump AP trans Icaking water at RK03 Tlghtened pacidng on root val 6 Core Spray Sys I Alarms did not flash Peplaced "B" acknowledge butt 7 AIX)G Front Panel Potential faulty indications Mjusted zero and set alann on recorder and checked recirc. valves
Oyster Creek Station #1 '
Docket No. 50-219 ,
ODRRDCTIVE ILDCTRICAL PAINTENANCE ON GASL ITENS 10R TIIE BOtml OF FEBRUATE 1979 Itan # Equipnent' Malfunction Corrective Action 1 Service Water Pump #1 Breaker trip unable to reclose Changed undervoltage coil and perfo. M PM on breaker l
e
Oyster Creek Statation #1 .
Docket No. 50-219 CORRECTIVE MECIIRJICAL MM!7IEWJCE CN OASL ITD1S EUR TIE FOTIll OF FEBRUARY 1979 . .
Itan # Equipment Malfunction Cbrrective Action 1 CRD 46-27 IICU Nipple on fill connection Ramved connector & retapped leaking around threads 2 Core Spray System V-20-41 leaking Mjusted packing to stop leakage 3 Condensate Transfer V-ll-41 leaking Tightened bonnet bolts as necessary Isolation to Isol. Cond. , to stop leak 4 Fire Protection System Packing leak on the pond pump Repacked the pump as necessary at the fire pump house to stop leak 5 CRD accumulator 14-11 V-lll valva nulfunction Replaced valve bonnet with a rebuilt spare 6 1-1 RDCCW Pump Leak from inboard seal Replaced seals
Oyster Creek Station #I Docket No. 50-219 REFUELING INFORMATION-- FEBRUARY 1979 Name of facility: Oyster Creek Station #1 Scheduled date for next refueling shutdown: September 15, 1979 Scheduled date for restart following refueling: November 10, 1979 Vill refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?
No Technical Specification change relative to the refueling is anticipated.
Scheduled date(s) for submitting proposed licensing action and supporting In fo rmat ion :
- 1. July 1979 - Cycle independent General Electric fuel design information and safety analysis for future use.
- 2. No submittal is scheduled for the use of Exxon fuel.
Important licensing considerations associated with refueling, e.g., new or different fuel design or supplier, unrevi~ewed design or performance analysis methods, significant changes in fuel design, new operating procedures:
- 1. General Electric Fuel Assemblies - Fuel design and performance analysit methods have been approved by NRC. New operating procedures, if necessary, will be subnitted at a later date.
- 2. Exxon Fuel Assemblies - No major changes have been made, nor are there any anticipated.
The number of fuel assemblies (a) in the core - 560 (b) in the spent fuel storage pool - 620 The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:
1,800 The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:
The Fall 1986 Outage.