ML19209B975

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LER 79-068/01T-0:on 790927,cables for HPCI Inboard Isolation Valve G41-F002 Discovered in Sections of Cable Tray W/Automatic Depressurization Sys Cables.Cause Not Stated. Mods Being Prepared
ML19209B975
Person / Time
Site: Brunswick Duke Energy icon.png
Issue date: 10/09/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19209B974 List:
References
LER-79-068-01T, LER-79-68-1T, NUDOCS 7910110338
Download: ML19209B975 (2)


Text

{{#Wiki_filter:. ...,.(777)LICENSEE EVENT REPORT CONTROL BLOCK: l llllllh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6lN lC lB lE lP l1 [@15l 0l 0l -l 0 0 0 0 0-l 0l 0l@[ 4l 1l 1l 1 1l@ll@o 1 UCENSE NUMHLH 25 26 LICENSE T)PE Jo $1 CAT $8 7 8 9 LICENSEE CODE 14 CON'T[n"c' l X}@l 0l 5 0]-l0l3l2l5@l0 9l 2 7l 7] 9l@1 0 0 l9 7 l9 @o i 1 8 60 61 OOCKET NUMBER M 69 EVENT DATE 24 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h o 2 lDuring a review of ECCS division separation, it was determined that Division TI cables l i for the llPCI inbcard isolation valve (C41-F002), a Division II valve, was run in sec- l o a ltions of cable tray containing Division II ADS system cables. Subsequent analysis of l o 4 o s [those cables revealed that if the isolation valve was in the wrong position, then a lo s failure at a trav section containing thes'e cables might result in a cou sinatien of al'0 7l cable failures which could impair the operability of the HPCI (Division 1) and ADS lo sl(Division II) systems. This is common to both units. Technical Specifications 6.9.1.$1 SYSTEM CAUSE C A US E C O .' P.VALVE CODE COGE SUBCODE COVPONENT CODE SU8 CODE SUECODElS lF lh lB h Wh l E l Ll E l C l 0l N l@ l Z l@ y @ o 9 F 8 9 10 11 12 13 16 19 20 ,_SEGUENTI AL OCCURRENCE REFORT REVISION LER RO EVENT YEAR R EPOHT NO. CODE TYPE N O.O RgPl7l9l-ll 0l 6l 8l ]/ll0l1lTl-0lRT_ 21 22 23 24 26 21 28 29 JJ 31 32 TAKEN ACTO CN PL AP T P TH HOURS S 8 IT D F R UB 5 P LI E MAP FACT RER lF lglJ4X@ l Z lgl Zl@l0l0l0l0l[ YlQl Y lg NlglG l0 8 l 0lg 33 35 Jo 3/40 41 42 43 44 41 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l United Engineers and Constructors is preparing plant modifications to " spare" cables li o LLL'_J land install new cables in isolated conduit to provide sufficient isolation. A review jof ECCS and their primary containment isolation valves in being performed to verify i 7 i 3 that no other cable separation problems existed. The cable seperation criterion for l the IIPCI and ADS systems will be redefined in the appropriate cabic seperation (CON'T} i.7 8 9 80 ST$% PO.'.E R OTHER STATUS D50 Y DISCOVE HY DESCR.PTION W@ l 0l 9l 1l@l NA ll D l@l NSSS Notification li 5 ACTIVITY LO TENT RE LE ASE D OF RELE ASE AVOUNT CF ACTIVITY LOCAT'ON OF RELEASE Z l @ l Zl@l NA lNAl1 6 7 8 9 10 11 44 45 80 PERSO*.NE L E XPOSun ES NUMBE R TYPE DESCRIPTION 37 l 0 l 0 l 0 l@l Z l@l NA li 7 PERSONNEL NJU ES NUYRER CESCH.P TION l 0 l 0 l 0 l@l NA i a 1 8 9 11 12 go LOSS OF OR D AV AGE TO FACILITY TYPE D;SC RIP TION W@l NA 9 7 8 9 to 60 12 l c l l N f@l DESCRIPTION 910110 3 2, > Nw m mn ISSUE , NAlll[[lllllllllj '1 8 9 10 68 69 80 ;s. C. Tollison, Jr. 919 457-9521 2 NAME OF PRFDARER payy . ..LER CONTINUATION - RO# 1-79-068 Facility: BSEP Unit No. 1 Event Date: 9-27-79 specifications in such a manner as to prevent any future recurrence of this event. .$1129 249}}