IR 05000245/2008002

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May 8, 2008

Mr. David Christian Sr. Vice President and Chief Nuclear Officer Dominion Resources 5000 Dominion Boulevard Glenn Allen, VA 23060-6711

SUBJECT: MILLSTONE POWER STATION - NRC INTEGRATED INSPECTION REPORT 05000336/2008002 AND 05000423/2008002

Dear Mr. Christian:

On March 31, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Millstone Power Station Unit 2 and Unit 3. The enclosed inspection report documents the inspection results, which were discussed on April 8, 2008, with Mr. Alan Price and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations, and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

This report documents three NRC-identified findings of very low safety significance (Green).

Two of these findings were determined to involve violations of NRC requirements. However, because of the very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Millstone.

In accordance with Title 10 of the Code of Federal Regulations Part 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,/RA/ Raymond J. Powell, Chief Reactor Projects Branch 5 Division of Reactor Projects Docket No. 50-336, 50-423 License Nos. DPR-65, NPF-49

Enclosure:

Inspection Report No. 05000336/2008002 and 05000423/2008002 w/

Attachment:

Supplemental Information

cc w/encl: J. A. Price, Site Vice President, Millstone Station C. L. Funderburk, Director, Nuclear Licensing and Operations Support W. Bartron, Supervisor, Station Licensing J. Spence, Manager Nuclear Training L. M. Cuoco, Senior Counsel C. Brinkman, Manager, Washington Nuclear Operations J. Roy, Director of Operations, Massachusetts Municipal Wholesale Electric Company First Selectmen, Town of Waterford B. Sheehan, Co-Chair, NEAC E. Woollacott, Co-Chair, NEAC E. Wilds, Jr., Ph.D, Director, State of Connecticut SLO Designee J. Buckingham, Department of Public Utility Control C. Meek-Gallagher, Commissioner, Suffolk County, Department of Environment and Energy V. Minei, P.E., Director, Suffolk County Health Department, Division of Environmental Quality R. Shadis, New England Coalition Staff S. Comley, We The People D. Katz, Citizens Awareness Network (CAN)

R. Bassilakis, CAN

SUMMARY OF FINDINGS

.........................................................................................................3

REPORT DETAILS

.....................................................................................................................6

REACTOR SAFETY

...................................................................................................................6 1R01 Adverse Weather Protection..........................................................................................6 1R04 Equipment Alignment.....................................................................................................7 1R05 Fire Protection...............................................................................................................8 1R06 Flood Protection Measures............................................................................................9 1R07 Heat Sink Performance................................................................................................10 1R11 Licensed Operator Requalification Program................................................................10 1R12Maintenance Effectiveness .........................................................................................11 1R13 Maintenance Risk Assessments and Emergent Work Control.....................................11 1R15 Operability Evaluations................................................................................................12 1R18 Plant Modifications.......................................................................................................15 1R19 Post-Maintenance Testing...........................................................................................16 1R22 Surveillance Testing.....................................................................................................17 1EP6 Drill Evaluation.............................................................................................................21 1EP7 Force-On-Force Exercise Evaluation...........................................................................22

RADIATION SAFETY

...............................................................................................................22 2OS1 Access to Radiological Significant Areas.....................................................................22 2OS2 ALARA Planning and Controls....................................................................................24

OTHER ACTIVITIES

[OA]........................................................................................................26

4OA1 Performance Indicator (PI) Verification........................................................................26 4OA2 Identification and Resolution of Problems...................................................................27 4OA6 Meetings, including Exit...............................................................................................29

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

..................................................................................................A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

......................................................A-2

LIST OF DOCUMENTS REVIEWED

......................................................................................A-2

LIST OF ACRONYMS

............................................................................................................A-9

SUMMAR Y
OF [[]]
FINDIN [[]]

GS IR 05000336/2008-002, 05000423/2008-002; 01/01/2008 - 03/31/2008; Millstone Power Station

Unit 2 and Unit 3; Operability Determinations and Surveillance Testing.

The report covered a three-month period of inspection by resident and region-based inspectors.

Three green findings were identified, two of which were non-cited violations (NCVs). The

significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter 0609, "Significance Determination Process." Findings for which the

significance determination process (SDP) does not apply may be Green or be assigned a

severity level after

NRC management review. The

NRC's program for overseeing the safe

operation of commercial nuclear power reactors is described in

NUR [[]]

EG-1649, "Reactor

Oversight Process," Revision 4, dated December 2006.

A. [[]]

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Green. The inspectors identified a finding for Dominion's failure to evaluate a non-conforming plant condition against the current licensing basis (CLB) as required by

Dominion procedure

OP -

AA-102-1101, Revision 0, "Development of Technical Basis to

Support Operability Determinations." Specifically, Dominion, in multiple instances, failed to evaluate the impact that a potential common mode charging system failure would

have on the Updated Final Safety Analysis Report Chapter 14.6.1, "Inadvertent Opening

of Power Operated Relief Valves (PORVs)," event, the analysis of record for which

credited both charging and safety injection availability. Corrective actions for this issue

included the initiation of an operations standing order and crew briefings to ensure all

crews understood the CLB related to Unit 2 charging and the need to implement the

compensatory action for this chapter 14.6.1 event, and a subsequent operability

determination (OD) revision to ensure charging was properly evaluated and documented

within the OD. This finding is more than minor because, if left uncorrected, the issue would become a

more significant safety concern. Specifically, degraded and non-conforming plant

conditions must be evaluated against their credited functions in the CLB to ensure the

adverse condition is properly evaluated for operability. This finding was determined to

be of very low safety significance (Green) because it did not result in a loss of charging

system operability or functionality. This finding has a cross-cutting aspect in the area of

Problem Identification and Resolution, Corrective Action Program component, because

Dominion did not thoroughly evaluate a Unit 2 charging system non-conforming

condition against the

CLB [[[P.1(c)]. (Section 1R15) Green. The inspectors identified a non-cited violation (]]
NCV ) of
10 CFR 50, Appendix B, Criterion

XI, "Test Control," for Dominion's failure to adequately evaluate surveillance

test results to ensure test acceptance criteria had been met on June 20, 2007.

Specifically, the inspectors identified that the "A" charging pump pulsation dampener

4surveillance test had incorrect data (i.e., testing duration time) and had been accepted as satisfactorily complete, although the test data was outside the surveillance

acceptance criteria. The test, in part, demonstrated that nitrogen gas from a failed

charging pump discharge dampener would not migrate into the common suction line

prior to the credited operator action to shut the pump's suction valve. A subsequent

review determined the surveillance test data was incorrect and the "A" charging pump

was operable. Dominion's corrective actions for this issue included briefings to provide

additional coaching and heighten awareness to the Unit 2 operations shift crews, a

review of actual surveillance computer data and review of subsequent surveillances to

ensure system operability, and the creation of a trend condition report including other

related human performance errors (CR-08-03220). This finding was more than minor because it was associated with the human

performance attribute of the Mitigating Systems cornerstone and affected the

cornerstone objective of ensuring the availability of systems that respond to initiating

events to prevent undesirable consequences (i.e., core damage). Specifically, the

failure to identify out of specification data could result in the failure to identify inoperable

equipment. The inspectors also concluded that if the failure to properly evaluate

charging pump discharge dampener test data was not corrected, a more significant

concern could exist (i.e. common mode failure of charging). The finding was

determined to be of very low significance (Green), because it was a deficiency

confirmed not to result in loss of safety function. The performance deficiency had a

cross-cutting aspect in the area of Problem Identification and Resolution, Corrective

Action Program component, because Dominion did not identify out of specification test

data P.1(a). (Section 1R22). Green. The inspectors identified a non-cited violation (NCV) of

10 CFR 50, Appendix B, Criterion

XVI, "Corrective Action," for Dominion's failure to identify a condition adverse to

quality after the "B" service water (SW) pump failed a Technical Specification in-service

test (IST). Specifically, on March 9, 2008, Dominion declared the "B" Service Water

(SW) pump operable, despite a failed IST flow surveillance. Dominion based this

declaration on the incorrect assumption that the failed pump differential pressure (dp)

was indicative of faulty test equipment vice an actual equipment issue. On March 10, 2008, Dominion determined that the unacceptable "B" SW dp was caused by

back pressure from the running "C" SW pump through the shut "B" swing pump cross

connect valve (2-SW-79B). The inspectors identified that Dominion did not have a

reasonable basis to consider the IST invalid based on the information available at the

time. Corrective actions for this issue included implementing an alternate plant

configuration to ensure train separation, performing an assessment to evaluate past

operability and to establish a bounding service water temperature at which the "B"

service water pump would be considered inoperable, and incorporating the 2-SW-97B

leakage repair in the 2R18 refueling outage. This finding was more than minor because it was associated with the equipment

performance attribute of the Mitigating System cornerstone, and affected the

cornerstone's objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences (i.e., core

damage). Specifically, Dominion concluded that the "B"

SW pump

IST containing

5unacceptable dp data was invalid based, in part, on an inability to justify the results (i.e. high dp and nominal flow). Consequently, the "B" SW pump was inappropriately

declared operable and the actual degraded condition was not promptly identified and

corrected. This finding is of very low safety significance (Green) because it did not

result in a confirmed loss of service water train operability. This finding has a

cross-cutting aspect in the area Human Performance, Decision Making Component,

because Dominion did not use conservative assumptions in restoring "B" SW pump

operability following a failed IST surveillance H.1(b). (Section 1R22)

B. Licensee-Identified Violations None.
6REPORT [[]]

DETAILS Summary of Plant Status

Millstone Units 2 & 3 operated at or near 100 percent through out the inspection period with the

following exceptions. Unit 3 reduced power to 88 percent on January 18, 2008, and to 90 percent

on February 6, 2008, to perform turbine control valve testing. 1.

REACTO R

SAFETY Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity 1R01 Adverse Weather Protection (71111.01) .1 Seasonal Site Inspection a. Inspection Scope (1 Sample) The inspectors reviewed Unit 3 readiness for seasonal site conditions, specifically extreme cold weather. The inspectors reviewed procedures and operator logs, interviewed

the work control supervisor, and walked down the heat tracing for the high head safety

injection pumps recirculation line and the component cooling water make-up pumps, to

determine if the actions required by Dominion's procedures were completed. Documents

reviewed during the inspection are listed in the Attachment.

b. Findings No findings of significance were identified.

.2 Impending Adverse Weather Conditions Inspection a. Inspection Scope (1 Sample) The inspectors reviewed Unit 2 readiness for impending adverse weather conditions,

specifically high winds and rain, potentially accompanied by external flooding. The

inspector walked down flood protection barriers in the intake structure (circulating water

pumps and

SW pumps), the emergency diesel generators (

EDGs) rooms, and the related

sumps and drains for the ground water system. The inspectors also reviewed Dominion

procedures for coping with external flooding, and interviewed the shift manager to

determine if the flooding mitigation plans and equipment were consistent with the

licensee's design requirements and the risk analysis assumptions. Documents reviewed

during the inspection are listed in the Attachment.

b. Findings No findings of significance were identified. 1R04 Equipment Alignment (71111.04)

.1 Partial System Walkdowns (4 Samples) a. Inspection Scope The inspectors performed four partial system walkdowns during this inspection period.

The inspectors reviewed the documents listed in the Attachment to determine the correct

system alignment. The inspectors conducted a walkdown of each system to determine if

the critical portions of selected systems were correctly aligned, in accordance with

applicable procedures, and to identify any discrepancies that may have had an effect on

operability. The walkdowns included selected switch and valve position checks, and

verification of electrical power to critical components. Finally, the inspectors evaluated

other elements, such as material condition, housekeeping, and component labeling.

Documents reviewed during the inspection are listed in the Attachment. The following

systems were reviewed based on their risk significance for the given plant configuration:

Unit 2 * "A" & "B" trains of high pressure safety injection (HPSI) while the "C"

HPSI [[pump was inoperable for maintenance; and * "A" & "B" trains of charging with the "B" charging pump out of service. Unit 3 * "C" charging while aligned to the "A" train due to "A" charging pump rotating element replacement; and * "B" residual heat removal (]]

RHR) system while the "A" RHR system was out of service for testing. b. Findings

No findings of significance were identified, .2 Complete System Walkdown (71111.04S)

a. Inspection Scope (1 Sample) The inspectors completed a detailed review of the alignment and condition of the Unit 3

"B" EDG. The inspectors conducted a walkdown of the system to determine whether

critical portions, such as valve positions, switches, and breakers, were correctly aligned in

8accordance with procedures to identify any discrepancies that may have had an effect on operability. The inspectors also conducted a review of outstanding maintenance work orders to

determine if the deficiencies significantly affected the "B" EDG system functions. In

addition, the inspectors discussed system health with the system engineer and reviewed

the condition report (CR) database to determine whether equipment alignment problems

were being identified and appropriately resolved. Documents reviewed during the

inspection are listed in the Attachment.

b. Findings

No findings of significance were identified. 1R05 Fire Protection (71111.05Q) a. Inspection Scope (14 Samples) The inspectors performed walkdowns of fourteen fire protection areas during the

inspection period. The inspectors reviewed Dominion's fire protection program to

determine the required fire protection design features, fire area boundaries, and

combustible loading requirements for the selected areas. The inspectors walked down

these areas to assess Dominion's control of transient combustible material and ignition

sources. In addition, the inspectors evaluated the material condition and operational

status of fire detection and suppression capabilities, fire barriers, and any related

compensatory measures. The inspectors compared the existing conditions of the areas to

the fire protection program requirements to determine if all program requirements were

being met. Documents reviewed during the inspection are listed in the Attachment. The

fire protection areas reviewed included: Unit 2 * Auxiliary Building Boric Acid Batch Tank / Chemical Addition Tank (Fire Area A-12); * Auxiliary Building 480 Volt

MCC B61 and B41A (Fire Area A-13); * Auxiliary Building Spent Fuel Pool and Cask Laydown Area (Fire Area A-14); *
EDG "A" Cubicle (Fire Area A-15); *
EDG "B" Cubicle (Fire Area A-16); and * Intake Structure Pump Room (Fire Area I-1 Zone A). Unit 3 * Main Steam Valve Enclosure, Elevation 24' 6" (Fire Area
MSV -1); * Main Steam Valve Enclosure, Elevation 49' (Fire Area
MSV -1); * Main Steam Valve Enclosure, Elevation 58' (Fire Area
MSV -1); * Main Steam Valve Enclosure, Elevation 71' (Fire Area MSV-1); * Circulating & Service Water Pumphouse, North Floor Area, Elevation 14' 6" (Fire Area
9CWS -1); * Circulating & Service Water Pumphouse, South Floor Area, Elevation 14' 6" (Fire Area
CWS -2); * Control Room, Elevation 47'-6" (Fire Area
CB -9); and * Cable Spreading Room, Elevation 24'-6" (Fire Area

CB-8). b. Findings No findings of significance were identified.

.2 Annual Fire Drill Observation (71111.05A)

a. Inspection Scope (1 Sample) Unit 2 The inspectors observed a fire brigade drill on January 22, 2008, to evaluate the

readiness of station personnel to fight fires. The drill simulated a fire in the Unit 2

Drumming/Maintenance Room. The inspectors observed the fire brigade members using

protective clothing, turnout gear, and self-contained breathing apparatus and entering the

fire area. The inspectors also observed the fire fighting equipment brought to the fire

scene to evaluate whether sufficient equipment was available to effectively control and

extinguish the simulated fire. The inspectors evaluated whether the permanent plant fire

hose lines were capable of reaching the fire area and whether hose usage was

adequately simulated. The inspectors observed the fire fighting directions and

communications between fire brigade members. The inspectors also evaluated whether

the pre-planned drill scenario was followed, and observed the post drill critique to evaluate

if the drill objectives were satisfied and that any drill weaknesses were discussed.

b. Findings No findings of significance were identified.

1R06 Flood Protection Measures (71111.06)

.1 Internal Flooding Inspection a. Inspection Scope (1 Sample) The inspectors reviewed the internal flood protection measures for the Unit 3 auxiliary

feedwater pump cubicles. This review was conducted to evaluate Dominion's protection

of the enclosed safety-related systems from internal flooding conditions. The inspectors

performed a walkdown of the area and reviewed the Updated Final Safety Analysis Report

(UFSAR), the internal flooding evaluation, and related documents. The inspectors

examined the as-found equipment and conditions to determine if they remained consistent

with those indicated in the design basis documentation, flooding mitigation documents,

10and risk analysis assumptions. Documents reviewed during the inspection are listed in the Attachment.

b. Findings No findings of significance were identified.

1R07 Heat Sink Performance (71111.7A) Inspection Scope (1 Sample) The inspectors reviewed one sample associated with the Unit

3 HVQ [[]]

ACUS1B heat

exchanger. The inspectors observed the as-found condition of the heat exchanger once it

was opened to verify that any adverse fouling concerns were appropriately addressed.

The inspectors reviewed the results of the inspections performed in accordance with

Dominion procedures including Proto-Power Calculation 03-100, Revision A. The

inspectors reviewed the inspection results against the acceptance criteria contained within

the procedure to determine whether all acceptance criteria had been satisfied. The

inspectors also reviewed the

UFS [[]]

AR to determine if heat exchanger inspection results

were consistent with the design basis. Documents reviewed during the inspection are

listed in the Attachment.

b. Findings No findings of significance were identified. 1R11 Licensed Operator Requalification Program (71111.11) Resident Inspector Quarterly Review (71111.11Q)

a. Inspection Scope (2 Samples) The inspectors observed simulator-based licensed operator requalification training for Unit

on January 29, 2008, and the Unit 3 Operational Exam 22, Revision 1, on

January 29, 2008. The inspectors evaluated crew performance in the areas of clarity and

formality of communications; ability to take timely actions; prioritization, interpretation, and

verification of alarms; procedure use; control board manipulations; oversight and direction

from supervisors; and command and control. Crew performance in these areas was

compared to Dominion management expectations and guidelines as presented in

OP -

MP-100-1000, AMillstone Operations Guidance and Reference Document.@ The inspectors compared simulator configurations with actual control board configurations. The inspectors also observed Millstone evaluators discuss identified weaknesses with the

crew and/or individual crew members, as appropriate. Documents reviewed during the

inspection are listed in the Attachment.

11 b. Findings

No findings of significance were identified. 1R12 Maintenance Effectiveness (71111.12Q) a. Inspection Scope (4 Samples) The inspectors reviewed four samples of Dominion's evaluation of degraded conditions,

involving safety-related structures, systems, and/or components for maintenance

effectiveness during this inspection period. The inspectors reviewed licensee

implementation of the Maintenance Rule. The inspectors reviewed Millstone=s ability to identify and address common cause failures, the applicable maintenance rule scoping document for each system, the current classification of the systems in accordance with

CFR 50.65 (a)(1) or (a)(2), and the adequacy of the performance criteria and goals

established for each system, as appropriate. The inspectors also reviewed recent system

health reports, CRs, apparent cause determinations, function failure determinations,

operating logs and discussed system performance with the responsible system engineer.

Documents reviewed are listed in the Attachment. The specific systems/components

reviewed were: Unit 2 * charging pumps and associated instrumentation; and * EDG room sumps, drains, and backflow preventers.

Unit 3 * SW strainers; and * auxiliary feedwater system.

b. Findings No findings of significance were identified. 1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13) a. Inspection Scope (6 Samples) The inspectors evaluated online risk management for emergent and planned activities.

The inspectors reviewed maintenance risk evaluations, work schedules, and control room

logs to determine if concurrent planned and emergent maintenance or surveillance

activities adversely affected the plant risk already incurred with out-of-service

components. The inspectors evaluated whether Dominion took the necessary steps to

control work activities, minimize the probability of initiating events, and maintain the

functional capability of mitigating systems. The inspectors assessed Dominion=s risk

2management actions during plant walkdowns. Documents reviewed during the inspection are listed in the Attachment. The inspectors reviewed the conduct and adequacy of

scheduled and emergent maintenance risk assessments for the following maintenance

and testing activities: Unit 2 * Planned work activities associated with "B"

EDG unavailability due to equipment issues and "A"

EDG unavailability following a fast start run on January 11, 2008; * Planned work activities associated with "D" circulating water pump (reactor trip risk) and Facility 1 reserve station service transformer (RSST) testing on January 22, 2008;

and * Planned work activities associated with "B" charging pump check valve leakage repairs on February 22, 2008. Unit 3 * Dominion's operational decision making implementation action plan for resolving "C" accumulator leakage on January 18, 2008; * Dominion's troubleshooting efforts for the electrohydraulic control system's over response to grid frequency changes in Load Set on January 18, 2008; and * Planned work activities associated with "A" charging pump replacement, "B" Safety Injection High (SIH) pump operational test, and "A" SIH pump run on

February 13, 2008. b. Findings No findings of significance were identified. 1R15 Operability Evaluations (71111.15) a. Inspection Scope (7 Samples) The inspectors evaluated seven

OD s against the guidance contained in

NRC Regulatory

Issue Summary 2005-20, Revision to Guidance Formerly Contained in NRC Generic

Letter 91-18,

AI nformation to Licensees Regarding Two

NRC Inspection Manual Sections on Resolution of Degraded and Nonconforming Conditions and on Operability.@ The inspectors also discussed the conditions with operators and system and design engineers, as necessary. Documents reviewed during the inspection are listed in the Attachment.

13The inspectors reviewed the adequacy of the following evaluations of degraded or non-conforming conditions:

Unit 2 *

OD [[]]
MP 2-024-07, "D" Channel of
TMLP [[[Thermal Margin Low Pressure] is Fluctuating between 2010 and 2060]]
PSIA ;" *
OD [[]]
MP 2-004-08 and
CR -08-00639, "The 'B' Charging Pump Relay was noted to be Cycling/Chattering;" *
OD [[]]
MP 2-005-08 and

CR-08-01810, "Impact from PZR Blockhouse Modification Needs to be Quantified and Addressed for Future Unit 2 Pressurizer Safety Valve Setpoint

Testing;" *

OD [[]]
MP -008-08 and
CR -08-02403, "2-
SW -97B ('B'
SW Header Cross-tie Valve) has Significant Seat Leakage;" and *

OD MP2-008-06, "Unit 2 Charging System Common Mode Failure."

Unit 3 *

OD [[]]
MP 3-006-06 and
CR 08-00894, "
STR 1C Strainer Boroscope Inspection Results Indicate Separated Welds;" and *
CR -07-11784, "Samples of Water Obtained from the Unit 3

ESF Outdoor Sump Indicated Tritium Levels." b. Findings Introduction. The inspectors identified a finding for Dominion's failure to evaluate a non-conforming plant condition against the current licensing basis (CLB) as required by

Dominion procedure

OP -

AA-102-1101, Revision 0, "Development of Technical Basis to

Support Operability Determinations." Specifically, Dominion, in multiple instances, failed to evaluate the impact that a potential common mode charging system failure would have

on the

UFS [[]]

AR Chapter 14.6.1, "Inadvertent Opening of Power Operated Relief Valves

(PORVs)," event, the accident analysis of record for which credited both charging and

safety injection availability. Description. On January 9, 2006, a charging system common mode failure occurred at Unit 2. After a charging pump was secured, nitrogen from a failed discharge dampener

bladder migrated backwards through the charging pump's internal check valves and into

the common suction line. This resulted in the remaining standby charging pumps

becoming gas bound shortly after they were started. Dominion initiated

OD [[]]

MP2-008-06

to ensure that the common mode failure would not reoccur before a final corrective action

plan could be implemented to ensure long term success. The OD assumed that upon a

bladder failure and its associated charging pump being secured, it would take at least two

hours for nitrogen gas migration to bind the common suction header. The OD determined

that the charging system remained operable since it instituted a compensatory measure

that required a charging pump's suction valve to be shut within the two hour period thus

preventing the nitrogen gas from reaching the common suction line. The OD, and

subsequent charging related ODs, concluded that the charging pumps were not credited

14in any

UFSAR Chapter 14 accident analysis event. On August 7, 2007, Dominion initiated
CR -07-08295 which identified that
UFS [[]]

AR Chapter

14.6.1, "Inadvertent Opening of the Pressurizer Power Operated Relief Valves (PORVs),"

stated that "The charging and SISs' [safety injection systems] have been shown to have

sufficient capacity to easily compensate for the loss of primary coolant mass through the

inadvertent opening of the pressurizer relief valves. Therefore, the core is not expected to

uncover during this event." Dominion identified that Areva had performed the analysis in

the first cycle for which they provided fuel (cycle 10) and had remarked in the

UFS [[]]
AR markup that the rate of coolant loss of the inadvertent opening of the
PO [[]]

RVs was

compensated by the actions of the safety injection and charging pumps. Furthermore, the

modeling of the Emergency Core Cooling System (ECCS) that accompanied cycle 10

included the automatic actuation of the charging pumps. This CR was assigned a level N

significance (lowest significance and identified as a condition not adverse to quality) and

did not contain an operation's assessment to determine if the CR adversely impacted

plant operations (i.e., impact of operability not evaluated). The CR created a corrective

action to perform an engineering technical evaluation to evaluate the effects that removing

charging system flow would have on the

UFSAR Chapter 14.6.1 event (M2-

EV-08-004).

This evaluation was completed on February 15, 2008, and concluded that

HP [[]]

SI, by itself,

was adequate to prevent uncovering the core following inadvertent opening of the

PORV s. On March 14, 2008, the inspectors identified to operations that
OD [[]]
MP 2-008-06 did not evaluate the impact that the non-conforming condition had on the

UFSAR Chapter 14.6.1

event. Dominion determined that the charging system remained operable since the Unit 2

charging system was not credited in the chapter 14.6.1 event. Dominion engineering

concluded that the

UFS [[]]

AR Chapter 14.6.1 statements were administrative and not

reflective of the

CLB. From March 14, 2006 through March 25, 2008, the inspectors engaged Dominion's operations, engineering staff, and management on the inadequate

OD; and, therefore the

inadequate basis to support charging system operability. Dominion initiated

CR 08-02880, and concluded that the charging pumps remained operable based on the

outcome of the previously performed technical evaluation (M2-EV-08-004). On

March 25, 2008, the inspectors reviewed the CR and determined that operations did not

adequately evaluate the non-conforming condition against the CLB since technical

evaluation (M2-EV-08-004) had not been processed through the 10 CFR 50.59 process.

The inspectors concluded and communicated to Dominion that technical evaluation

M2-EV-08-004 did not change the

CLB. On March 26, 2008, Dominion initiated

CR-08-02919, and concluded that CR-08-02880

did not have an adequate basis to support charging system operability based on its

reference to technical evaluation M2-EV-08-004. The CR concluded that the previously

established

OD compensatory actions must apply to the Chapter 14.6.1 event. Analysis. The performance deficiency associated with this finding was that Dominion failed to evaluate a Unit 2 non-conforming charging system condition against its

CLB, as

15required by Dominion procedure

OP -

AA-102-1101. This finding is more than minor because, if left uncorrected, the issue would become a more significant safety concern.

Specifically, degraded and non-conforming plant conditions must be evaluated against

their credited functions in the CLB to ensure the adverse condition is properly evaluated

for operability. This finding was evaluated in accordance with IMC 0609, Attachment 4,

"Phase 1 - Initial Screening and Characterization of Findings" and determined to be of

very low safety significance (Green) since it did not result in a loss of charging system

operability or functionality. This finding has a cross-cutting aspect in the area of Problem Identification and Resolution (PI&R), Corrective Action Program component, because Dominion did not

thoroughly evaluate a Unit 2 charging system non-conforming condition against the CLB.

P.1(c)

Enforcement. Enforcement does not apply because the performance deficiency, not evaluating a non-conforming condition against the CLB as required by Dominion

procedure

OP -

AA-102-1101, Revision 0, "Development of Technical Basis to Support

Operability Determinations," did not involve a Technical Specifications (TS) required

procedure. Dominion entered this issue into their corrective action program

(CR-08-02919). Corrective actions for this issue included the initiation of an operations

standing order and crew briefings to ensure all crews understood the CLB related to Unit

charging and need to implement the compensatory action for this chapter 14.6.1 event,

and a subsequent OD revision to ensure charging was properly evaluated and

documented within the OD. Because this finding does not involve a violation of regulatory

requirements and is of very low safety significance (Green), it is identified as

FIN 05000336/2008002-01, Failure to Evaluate a Unit 2 Charging System Non-conforming Condition against the Current Licensing Bases. 1R18 Plant Modifications (

IP 71111.18)

.1 Permanent Modification

a. Inspection Scope (1 Sample)

The inspectors reviewed a Unit 3 modification that installed a hydrostatic pump to refill the

safety injection accumulators due to system leakage. The modification was reviewed to

verify that the design bases, licensing bases, and performance capability of risk significant structures, systems, and components had not been degraded through the plant

modification and that the configuration change did not place the plant in an unsafe

condition. To assess the adequacy of the modifications, the inspectors performed a

system walkdown, interviewed plant staff, and reviewed applicable documents, including

procedures, modification packages, drawings, corrective action program documents, the

CFR 50.59 screening, post maintenance test, the

UFSAR and TS. Documents

reviewed during the inspection are listed in the Attachment.

16b. Findings No findings of significance were identified.

.2 Temporary Modification

a. Inspection Scope (1 Sample) The inspectors reviewed a Unit 3 temporary modification which installed a manual

isolation valve in the "C" safety injection accumulator test header (DCN DM3-00-0013-08).

The modification was reviewed to evaluate if the temporary modification adversely

affected the function of the associated safety systems. The inspectors reviewed the

temporary modification and the associated

10 CFR 50.59 screening against the

UFSAR

and TS to determine whether the modification affected system operability or availability.

Documents reviewed during the inspection are listed in the Attachment.

b. Findings No findings of significance were identified. 1R19 Post-Maintenance Testing (71111.19) a. Inspection Scope (5 Samples) The inspectors reviewed five post-maintenance test (PMT) activities to determine whether

the PMT adequately demonstrated that the safety-related function of the equipment was

satisfied, given the scope of the work specified, and that operability of the system was

restored. In addition, the inspectors evaluated the applicable test acceptance criteria to

evaluate consistency with the associated design and licensing bases, as well as TS requirements. The inspectors also evaluated whether conditions adverse to quality were

entered into the corrective action program for resolution. Documents reviewed during the

inspection are listed in the Attachment. The following maintenance activities and their

PMTs were evaluated:

Unit 2 * "B" EDG testing following troubleshooting activities on January 10, 2008.

Unit 3 *

3SIH -V822 testing following installation of the valve in the "C" safety injection accumulator test header on February 1, 2008; *
OP 3304C, "Primary Makeup and Chemical Addition," Revision 21, after replacement of a relay in the reactor coolant makeup controller on February 28, 2008; *
3HVQ *

ACU 2A following replacement of two freon pressure control valves and the hot gas bypass valve on March 19, 2008; and

17*

SPROC [[]]

ENG08-3-001, "'A' Charging Pump Post Shaft Replacement Functional Test," Revision 1, following pump overhaul on March 15, 2008.

b. Findings

No findings of significance were identified. 1R22 Surveillance Testing (71111.22) a. Inspection Scope (9 Samples) The inspectors reviewed nine surveillance activities to determine whether the testing

adequately demonstrated equipment operational readiness and the ability to perform the

intended safety-related function. The inspectors attended pre-job briefs, reviewed

selected prerequisites and precautions to determine if they were met, and observed the

tests to determine whether they were performed in accordance with the procedural steps.

Additionally, the inspectors reviewed the applicable test acceptance criteria to evaluate

consistency with associated design bases, licensing bases, and TS requirements and that

the applicable acceptance criteria were satisfied. The inspectors also evaluated whether

conditions adverse to quality were entered into the corrective action program for

resolution. Documents reviewed during the inspection are listed in the Attachment. The

following surveillance activities were evaluated:

Unit 2 *

SP 2605G, "Containment Isolation System
CIV Stroke and Timing
IST , Facility 1," Revision 6, on January 23, 2008; *
SP 2602A, "Reactor Coolant Leakage," Revision 006-001, on January 16, 2008; *
SP 2612A, "'A' and 'B' Service Water Pump and Facility 1 Discharge Check Valve
IST ," Revision 002-02, on March 8, 2008; *
SP 2264, "Charging Pump "A" Pulsation Dampener Test," Revision 001-02, on July 20, 2007; and *

SP 2664A, "'A' Charging Pump Pulsation Dampener Test," Rev. 000, on March 25, 2008.

Unit 3 *

SP 3443C21, "Protection Set Cabinet
III Operational Test Data Sheet," Revision 19, on January 14, 2008; *
SP 3601F.6, "Reactor Coolant System Water Inventory Measurement," Revision 005-05, on January 15, 2008; *
SP 3623.2, "Turbine Overspeed Protection System Test," Revision 009-02, on February 6, 2008; and *
SP 3610A.1, "Residual Heat Removal Pump 3

RHS*P1A Operation Readiness Test," Revision 011-05, on March 19, 2008.

18b. Findings

.1 Failure to Identify Unacceptable Unit 2 Charging Pump Surveillance Test Data Introduction. The inspectors identified a non-cited violation (NCV) of

10 CFR 50, Appendix B, Criterion

XI, "Test Control," for Dominion's failure to adequately evaluate

surveillance test results to ensure test acceptance criteria had been met on

June 20, 2007. Specifically, the inspectors identified that the "A" charging pump pulsation

dampener surveillance test had incorrect data (i.e., testing duration time) and had been

accepted as satisfactorily complete, although the test data was outside the surveillance

acceptance criteria. The test, in part, demonstrated that nitrogen gas from a failed

charging pump discharge dampener would not migrate into the common suction line prior

to the credited operator action to shut the pump's suction valve.

Description. On February 24, 2008, the inspectors reviewed surveillance form SP 2264, "Charging Pump 'A' Pulsation Dampener Test," performed on June 19, 2007, as part of a

review to evaluate the effectiveness of the corrective actions from a previous NRC

identified finding, (NCV 05000336/2007003-03, "Failure to Adequately Evaluate

Surveillance Test Data"). The inspectors identified that the acceptance criteria for the

time duration of the test had not been met. Specifically, the test data indicated the test

had not been performed for a minimally acceptable period of one hour since the

surveillance record listed 9:52 p.m. and 10:04 p.m. as the times that the initial pump

pressure and final pump pressure were measured (12 minutes).

During the review of the surveillance results, and final approval of the surveillance, several

personnel had accepted this data as being satisfactory. Following the observation, the

inspectors notified system engineering and operations personnel of this discrepancy, and

they agreed that the acceptance criteria had not been met. Based on a review of

computer data related to the June 19, 2007, surveillance and subsequent surveillance test, Dominion concluded the "A" charging pump remained operable.

Analysis. The performance deficiency associated with this NRC identified finding involved an inadequate review of surveillance test results to ensure the Unit 2 charging system was

not susceptible to a previously identified common mode failure. This finding was more

than minor because it was associated with the human performance attribute of the

Mitigating Systems cornerstone and affected the cornerstone objective of ensuring the

availability of systems that respond to initiating events to prevent undesirable

consequences (i.e., core damage). Specifically, the failure to identify out of specification data could result in the failure to identify inoperable equipment. The inspectors also

concluded that if the failure to properly evaluate charging pump discharge dampener test

data was not corrected, a more significant concern could exist (i.e., common mode failure

of charging).

The inspectors conducted a Phase 1 SDP Table 4a worksheet for Mitigating Systems and

determined that the finding was of very low significance (Green), because it was a

deficiency confirmed not to result in loss of safety function.

19The performance deficiency had a cross-cutting aspect in the area of PI&R, Corrective Action Program component, because Dominion did not identify out of specification test

data. P.1(a).

Enforcement.

10 CFR 50, Appendix B, Criterion

XI, "Test Control," states, in part, that test results shall be documented and evaluated to assure the test requirements have

been satisfied. Contrary to the above, on June 20, 2007, Dominion failed to identify that

the Unit 2 "A" charging pump pressure decay test had documented an unacceptable test

time frame of 12 minutes when compared to the minimum one hour time required per the

surveillance acceptance criteria. This surveillance was originally approved as satisfactory

until identified by the inspectors. Corrective actions for this issue included briefings to

provide additional coaching and heighten awareness to the Unit 2 crews, a review of

actual surveillance computer data and review of subsequent surveillances to ensure

system operability, and the creation of a trend CR including other related human

performance errors such as

NRC identified finding

NCV 05000336/2007003-03. Since

this finding is of very low safety significance (Green) and had been entered into the

licensee's corrective action program (CR-08-00817), this violation is being treated as a

NCV , consistent with Section
VI.A. 1 of the
NRC Enforcement Policy. (

NCV 05000336/2008002-02, Failure to Identify Unacceptable Unit 2 Charging Pump

Surveillance Test Data). .2 Failure to Identify a Service Water Bypass Flow Path following a Failed

IST Introduction. The inspectors identified a
NCV of 10

CFR 50, Appendix B, Criterion XVI, "Corrective Action," for Dominion's failure to identify a condition adverse to quality after

the "B"

SW pump failed a

TS IST. Specifically, on March 9, 2008, Dominion declared the

"B"

SW pump operable despite a failed

IST flow surveillance. Dominion based this

declaration on the incorrect assumption that the failed pump dp was indicative of faulty

test equipment vice an actual equipment issue.

Description. On March 8, 2008, at 9:28 p.m., operations entered

TS 3.7.4.1, "Service Water System," and commenced a scheduled

IST for the "B" SW pump in accordance

with

SP 2612F, "'B' Service Water Pump

IST, Facility 1," Revision 002-01. On March 9,

2008, at 12:30 a.m., the

IST for the "B"

SW pump, and "A" SW pump and discharge

check valve was completed. Operations identified that the "B" SW pump dp of 47.8 psid

had exceeded the established IST acceptance criteria of 45.7 psid. Operations

appropriately identified in step 4.1.11c that these results were unsatisfactory and

maintained the pump in an inoperable status. Operations noted in their logs that attempts

were made to adjust Facility 1 service water flow within the allowable band, however, the

"B"

SW pump dp remained greater than the maximum acceptable. In addition, the Facility
SW flow instrument was noted by a condition based monitoring (

CBM) technician to be

providing valid data. The "A"

SW pump and discharge check valve

IST results were

reviewed and accepted since the values were within the allowed acceptance criteria

although the pump dp appeared higher than normal. Based on satisfactory "A"

SW pump
IST results,

TS 3.7.4.1 was exited with the "A" SW pump operating and aligned to Facility

and "C" SW pump operating and aligned to Facility 2 at 5:40 a.m. on March 9, 2008.

20Dominion initiated

CR -08-02281 to document that the "B"
SW pump failed its quarterly
IST surveillance with pump dp 2.08 psid above the acceptable range. The
CR documented that
CBM verified that the flow instrument was functioning properly. The

CR

was assigned a significance level N (lowest significance and identified as a condition not

adverse to quality). The shift manager's comment section noted that this issue appeared

to be an issue with the instrumentation used during the surveillance since it was difficult to

understand pump dp exceeding the maximum value unless instrumentation was suspect.

The

CR noted that the "B"

SW pump was considered inoperable based on the failed test

results (submitted at 4:51 a.m., on March 9, 2008).

On March 9, 2008, at 8:30 p.m., Dominion conducted a management conference call and

concluded that the "B"

SW pump failed the

IST due to faulty flow monitoring equipment.

Although the CBM technician verified that the flow instrumentation was providing valid

data, Dominion concluded that faulty flow monitoring equipment would have also

explained the higher than normal "A"

SW dp results. Operations concluded that both

ISTs

were therefore invalid. Operations subsequently declared the "B" SW pump operable and

started the "B"

SW pump. Operations then secured and declared the "A"

SW pump

inoperable since the

IST performed on the "A"

SW pump had been used as a post

maintenance test following its previous overhaul.

On March 10, 2008, at 6:21 p.m., Dominion determined that the high Facility 1 "B" SW dp

was caused by back pressure from the running Facility 2 "C" SW pump through the shut

"B" swing pump cross connect valve (2-SW-97B). As a result of this valve leaking by,

approximately 500 gallon per minute of Facility 2 service water flow was being bypassed

into the Facility 1 train. Dominion subsequently shut 2-SW-97A to ensure SW Facility

train separation was maintained and entered

TS 3.7.4.1 since both the "A" and "B"

SW

pumps were then considered inoperable. On March 11, 2008, at 11:27 a.m., Dominion

exited

TS 3.7.4.1 following a successful "A"

SW IST.

On March 11, 2008, the inspectors determined that Dominion did not have an adequate

basis to declare the "B"

SW pump

IST invalid after the unsatisfactory test results on

March 9, 2008, following the management conference call. The inspectors determined

that while the "B"

SW pump was initially declared inoperable following the failed

IST,

operations improperly subsequently concluded that the data was not correct based on

past instrumentation performance. The inspectors concluded that since the CBM

technician had actually verified the flow instrumentation was working properly, Dominion

had specific information which directly conflicted with their conclusion; therefore, the

station did not act in a conservative manner. The inspectors identified that it was

reasonable for Dominion to identify the cause of the high "B" SW pump dp prior to

declaring the system operable. The inspectors determined that with the "B" SW pump

inservice for Facility 1, a SW bypass flow path existed from Facility 2 (through the shut

2-SW-79B valve and through the open 2-SW-79A valve into Facility 1). The inspectors

identified that upon a loss of Facility 1, a significant portion of the "C" SW pump's flow

would be have been diverted to the Facility 1 header reducing flow to the redundant

Facility 2 train.

21Analysis. This finding was more than minor because it was associated with the equipment performance attribute of the Mitigating System cornerstone, and affected the

cornerstone's objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences (i.e., core damage).

Specifically, Dominion concluded that a "B"

SW pump

IST containing unacceptable dp

data was invalid based, in part, on an inability to interpret the results (i.e. high d/p and

nominal flow). Consequently, the "B" SW pump was inappropriately declared operable

and the actual degraded condition was not promptly identified and corrected. This finding

is of very low safety significance (Green) because it did not result in a confirmed loss of

SW train operability.

This finding has a cross-cutting aspect in the area Human Performance, Decision Making

Component, because Dominion did not use conservative assumptions in restoring "B" SW

pump operability following a failed IST surveillance. H.1(b).

Enforcement.

10 CFR 50, Appendix B, Criterion

XVI, "Corrective Action," states, in part, that measures shall be established to assure that conditions adverse to quality are

promptly identified and corrected. Contrary to the above, on March 9, 2008, following a

failed "B"

IST [[]]

SW surveillance, Dominion did not identify, evaluate or correct the cause

prior to restoring the system to operable status. Dominion concluded that the test was

invalid based on the belief the data was invalid due to flow instrumentation monitoring

issues and not an actual SW equipment issue despite conflicting information. As a result,

a safety-related SW system was restored to operable status and degraded service water

by-pass flow condition reintroduced. Corrective actions for this issue included

implementing an alternate plant configuration to ensure train separation, performing an

OD to evaluate past operability and to establish a bounding

SW temperature at which the

"B"

SW pump would be considered inoperable, and incorporating the 2-

SW-97B leakage

repair in the 2R18 refueling outage. Because this finding is of very low safety significance

(Green) and was entered into the licensee's corrective action program (CR-08-02383),

this violation is being treated as an

NCV , consistent with Section
VI.A. 1 of the
NRC Enforcement Policy. (
NCV 05000336/2008002-03, Failure to Identify a Service Water Bypass Flow Path following a Failed
IST ). Cornerstone: Emergency Preparedness (

EP) 1EP6 Drill Evaluation (71114.06 - 2 Samples)

.1 Classification and Notification During Requalification Training

a. Inspection Scope The inspectors reviewed the operators' emergency classification and notification

completed during requalification Unit 3 training on January 29, 2008. The inspectors

verified the classification, notification, and protective action recommendations were

accurate and timely.

2 b. Findings

No findings of significance were identified.

.2 Combined Functional Drill

a. Inspection Scope The inspectors observed the conduct of a Unit 3 licensed operator training emergency

planning drill on March 18, 2008. The inspectors observed the operating crew

performance at the simulator and the emergency response organization performance at

the technical support center and emergency operations facility. The inspectors evaluated

the classification, notification, and protective action recommendations for accuracy and

timeliness. Additionally the inspectors assessed the ability of Dominion's evaluators to

adequately address operator performance deficiencies identified during the exercise.

b. Findings

No findings of significance were identified.

1EP7 Force-On-Force Exercise Evaluation (71114.07)

a. Inspection Scope (1 Sample) The inspectors observed licensee performance in the Technical Support Center during

one site emergency preparedness drill conducted in conjunction with a Force-On-Force

exercise, documented in inspection report 05000336/2008201 and 05000423/2008201.

The inspectors observed communications, event classification and notification activities by

the simulated shift personnel for Units 2 & 3 during the drill on March 25, 2008. The

inspectors verified the classification, notification and protective action recommendations

were accurate and timely. The inspectors also observed portions of the post drill critique

to determine whether any deficiencies were also identified by Dominion evaluators.

b. Findings

No findings of significance were identified. 2.

RADIAT [[]]
ION [[]]
SAFETY Cornerstone: Public Radiation Safety 2

OS1 Access to Radiological Significant Areas (71121.01)

a. Inspection Scope (11 Samples) During the period February 11-15, 2008, the inspectors conducted the following activities

to determine whether the licensee was properly implementing physical, administrative,

23and engineering controls for access to locked high radiation areas, and other radiological controlled areas (RCA) during normal power operations, and that workers were adhering

to these controls when working in these areas. Implementation of these controls was

reviewed against the criteria contained in

10 CFR 20,

TS, and Dominion procedures. This activity represents the completion of 11 samples relative to this inspection area

partially completing the annual inspection requirement of 21. Plant Walk down and Radiation Work Permit (RWP) Reviews (1) The inspectors toured accessible RCAs in Unit 2 and Unit 3 and, with the assistance of a radiation protection technician, performed independent radiation surveys of selected areas and components, to confirm the accuracy of survey

data, and the adequacy of postings. Surveys were conducted in the Auxiliary

Buildings, Waste Buildings, and Fuel Storage Buildings. (2) The inspectors identified plant areas where radiologically significant work activities were being performed. These activities included obtaining a Unit 3 spent resin

sample, performing maintenance on a Unit 3 charging pump, and performing

radiography on Unit

3 SW piping. The inspectors reviewed the applicable

RWPs

for these activities to determine if the radiological controls were acceptable,

attended pre-job briefings, and reviewed the electronic dosimeter dose/dose rate

alarm set points to determine if the set points were consistent with plant policy. (3) The inspectors determined that there were no current RWPs for airborne radioactivity areas with the potential for individual worker internal exposures to

exceed 50 mrem. (4) During 2007, there were no internal dose assessments for any actual internal exposures that reached the reporting threshold of greater than 10 mrem

Committed Effective Dose Equivalent (CEDE). The inspectors also reviewed data

for the five highest exposed individuals for 2007, and the dose/dose rate alarm

reports and determined that no exposure exceeded site administrative, regulatory,

or performance indicator criteria. Additionally, the inspectors confirmed that no

declared pregnant workers were employed during 2007. Problem Identification and Resolution (5) A review of assessment reports and field observation reports was conducted to determine if problems related to implementing radiological controls were entered

into the corrective action program for resolution. (6) Nine CRs, associated with radiation protection control access, initiated between October, 2007, and January, 2008, were reviewed and discussed with the licensee

staff to determine if the followup activities were being conducted in an effective

and timely manner, commensurate with their safety significance.

24High Radiation Area (HRA) and Very High Radiation (VHRA) Area Controls

(7) Procedures for controlling access to

HRA s and

VHRAs were reviewed to determine if the administrative and physical controls were adequate. The

inspectors determined that a recently implemented corporate procedure

(RP-AA-201, "Access Controls for High and Very High Radiation Areas"), provided

additional controls over the replaced site procedure RPM 5.1.3, that was

previously implemented. (8) Keys to locked high radiation areas (LHRA) stored at the control points and in the Unit 3 Control Room were inventoried and accessible

LH [[]]

RA's were verified to be

properly secured and posted during plant tours. (9) The inspectors reviewed corporate procedure

RP -

AA-260, "Control of Radiography," and attended the pre-job briefing for performing radiography on Unit

SW piping. The inspectors determined whether access controls, including

postings, technician coverage, and site notifications, were appropriate for the

transient

HRA s that would occur during radiography. Radiation Worker and Radiation Protection Technician Performance (10) Several radiological related

CRs were reviewed to evaluate if the incidents resulted from repetitive worker errors to determine if an observable pattern traceable to a

similar cause was evident. (11) Radiation protection technicians and radworkers were questioned regarding their knowledge of plant radiological conditions and associated controls.

b. Findings No findings of significance were identified.

2OS 2

ALARA Planning and Controls (71121.02)

a. Inspection Scope (8 Samples) During the period February 11-15, 2008, the inspectors conducted the following activities

to determine whether the licensee was properly implementing operational, engineering,

and administrative controls to maintain personnel exposure as low as is reasonably achievable (ALARA) for past activities performed during 2007. Also reviewed were the

dose controls for current activities and the preparations being made for the spring (2R18)

2008 refueling outage. Implementation of these controls was reviewed against the criteria

contained in 10 CFR 20, applicable industry standards, and Dominion procedures.

25Radiological Work Planning (1) The inspectors reviewed pertinent information regarding cumulative exposure history, current exposure trends, and ongoing activities to assess past (2007)

performance and dose challenges for 2008, including the spring refueling outage

(2R18). (2) The inspectors reviewed the exposure data for tasks performed during 2007 and compared actual exposure with forecasted estimates. Included in this review were

the tasks performed during the Unit 3 (3R11) outage, on-line tasks performed for

both operating units, and dry cask loading/storage operations. (3) The inspectors evaluated the departmental interfaces between radiation protection, operations, maintenance, and engineering to identify missing

ALA [[]]

RA

program elements and interface problems. The evaluation was accomplished by

reviewing recent

ALA [[]]
RA Council meeting and outage challenge board minutes,
ALA [[]]

RA evaluations, departmental dose summaries, attending a 2R18 pre-outage

challenge board for steam generator eddy current testing, and interviewing the

ALA [[]]

RA coordinator. The inspectors also reviewed the Radiation Protection

Department continuous improvement initiatives and the 5-year

ALA [[]]

RA Plan

(2007-2011) that identifies areas for further improving radiological controls. Verification of Dose Estimates (4) The inspectors reviewed the assumptions and basis for the annual (2007) site collective exposure projections for routine power operations and maintenance

activities and compared the estimated dose with the actual dose received by

workers. The inspectors also reviewed the dose projections for the 2R18 refueling

outage to determine if there were significant deviations from the actual exposures

received for various tasks in past outages. (5) The inspectors reviewed Dominion procedures associated with monitoring and re-evaluating dose estimates when the forecasted cumulative exposure for tasks

differed from the actual dose received. The inspectors reviewed the dose/dose

rate alarm reports and exposure data for selected individuals receiving the highest

total effective dose equivalent (TEDE) exposures for 2007 to confirm that no

individual exposure exceeded the regulatory limit, or met the performance indicator

reporting guideline. Jobs-In-Progress (6) The inspectors reviewed the RWPs, attended the pre-job briefings, and observed various aspects of jobs-in-progress performed at Unit 3, including obtaining a

spent resin sample (RWP 3-08-17), charging pump repair (RWP 3-08-30), and

radiography on

SW piping (

RWP 3-08-25). The inspectors also reviewed the

documentation and discussed preparation for transferring spent resin into a

shipping cask at Unit 2.

26 (7) The inspectors reviewed recent

ALA [[]]

RA evaluations developed for controlling low dose tasks. These evaluations addressed Unit 3 charging pump maintenance and

Unit 3 containment entries at power for venting the safety injection system. Problem Identification and Resolution (8) The inspectors reviewed elements of the licensee's corrective action program related to implementing the

ALA [[]]

RA program to determine if problems were being

entered into the program for timely resolution. Eight CRs related to controlling

individual personnel exposure and programmatic

ALA [[]]

RA challenges were

reviewed.

b. Findings No findings of significance were identified. 4.

OTHER [[]]
ACTIVI [[TIES [OA]]]
4OA 1 Performance Indicator (

PI) Verification (71151) .1 Cornerstone: Barrier Integrity a. Inspection Scope (4 Samples)

The inspectors reviewed Dominion submittals for the PIs listed below to verify the

accuracy of the data reported during that period. The PI definitions and guidance

contained in

NEI 99-02,

ARegulatory Assessment Indicator Guideline,@ Revision 5, were used to verify the basis for reporting each data element. The inspectors reviewed portions of the operations logs, monthly operating reports, Licensee Event Reports (LERs),

surveillances, and discussed the methods for compiling and reporting the PIs with

cognizant licensing and engineering personnel. Documents reviewed during this

inspection are listed in the Attachment. Unit 2 * "Reactor coolant system specific activity" between April 1, 2007 and December 31, 2007; and * "Reactor coolant system leak rate" between April 1, 2007 and December 31, 2007. Unit 3 * "Reactor coolant system specific activity" between January 1, 2007 and December 31, 2007; and * "Reactor coolant system leak rate" between January 1, 2007 and December 31, 2007.

27b. Findings No findings of significance were identified. 4OA2 Identification and Resolution of Problems (71152 - 2 Annual Samples) .1 Review of Items Entered into the Corrective Action Program a. Inspection Scope As required by Inspection Procedure 71152, "Identification and Resolution of Problems,"

and in order to help identify repetitive equipment failures or specific human performance

issues for followup, the inspectors performed a daily screening of items entered into

Dominion's corrective action program. This was accomplished by reviewing the

description of each new CR and attending daily management review committee meetings.

Documents reviewed are listed in the Attachment.

b. Findings No findings of significance were identified. .2 Annual Sample - Review of Gases in the Unit 2 "B"

EDG Jacket Water Cooling System a. Inspection Scope The inspectors performed a focused review of the actions taken and planned in response to a number of "B"
EDG jacket water cooling system expansion tank overflow events. The review included a recent event that occurred in February 2008. The inspectors reviewed the causal evaluations contained in the associated
CR s, corrective actions that have been taken, ongoing troubleshooting efforts, and planned corrective actions. The inspectors also interviewed personnel and performed a plant walkdown of the Unit 2
EDG s. b. Findings and Observations No findings of significance were identified. The inspectors noted the expansion tank overflow issue has existed for several years as documented in a number of
CR [[s between 2003 and February 2008. The licensee has determined that the most likely cause of the tank overflowing is the introduction of combustion gases into the jacket water system due to leakage past a copper gaskets where the fuel injector, air start valve, and cylinder indicator adapters are threaded into the cylinder liners. The same issue has not been experienced with the "A"]]
EDG and the problem has been intermittent with the "B"
EDG in that it does not occur during every monthly surveillance run and there were no events identified in 2006. The inspectors noted that the condition does not appear to be as significant as that experienced at other plants where trips of

EDGs occurred due to a resultant fluctuation in jacket cooling water

28pump discharge pressure. The licensee has taken a number of actions that have not yet been successful in resolving the issue. Licensee actions have included replacement of all gaskets in 2005 and again in 2007 as well as the installation of sight glasses in the system to allow monitoring for the presence of gas bubbles. Additionally, the inspectors verified that surveillance and maintenance procedures have been updated to include relevant operating experience information involving aspects such as gasket installation instructions and monitoring of the EDG jacket water system parameters during operation. The inspectors confirmed that the licensee was continuing to evaluate this issue in an effort to identify additional corrective actions that may be taken to confirm and correct the

cause of the expansion tank overflows. Ongoing actions being considered are

documented in CR 08-01137 and include: * investigating the development and use of a lapping tool that could be used to improve the seating surface at the mechanical joint between the adapters and the cylinder

liners; * continuing the troubleshooting data collection for at least several more months; * performance of an independent peer review to assess the issue; * evaluating the potential need to replace the cylinder liners based on the results of the peer review and the results of seat lapping evaluation and/or performance; and * obtaining additional information from the vendor to improve adapter installation techniques. The inspectors found that although the issue has not had a significant impact on the ability

of the EDG to perform its safety function, appropriate additional licensee actions to

identify and correct the cause of the overflow events are continuing.

.3 Annual Sample - Unit 3 Main Turbine Control Valve Testing and Load Set Operation a. Inspection Scope The inspectors performed a focused review of the actions taken in response to an overpower condition that occurred during turbine valve testing in November 2007. The inspectors interviewed personnel involved in the corrective actions and reviewed the causal evaluations contained in the associated CR, completed corrective actions, and the results of the subsequent test conducted in February 2008. b. Findings and Observations No findings of significance were identified.

The inspectors reviewed Dominions corrective actions resulting from the investigations

which included: reducing reactor power to 90 percent for control valve testing to minimize

turbine response and resulting reactor power fluctuations due to small changes in grid

29frequency, closely monitoring turbine first stage pressure and adjusting turbine load to maintain first stage pressure, and making changes to the test procedure to incorporate

the results of the apparent cause investigations. The inspectors concluded that

Dominion's corrective actions were adequate. 4OA6 Meetings, including Exit Exit Meeting Summary

On April 8, 2008, the resident inspectors presented the overall inspection results to

Mr. Alan Price, and other members of his staff. The inspectors confirmed that no

proprietary information was provided or examined during the inspection.

ATTACH [[]]
MENT [[:]]
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION A-1
SUPPLE [[]]
MENTAL [[]]
INFORM [[]]
ATION [[]]
KEY [[]]
POINTS [[]]
OF [[]]

CONTACT Licensee personnel

G. Auria Nuclear Chemistry Supervisor

B. Bartron Supervisor, Licensing

J. Cambell Manager, Security

C. Chapin Supervisor, Nuclear Shift Operations Unit 2
A. Chyra Nuclear Engineer,

PRA

F. Cietek Maintenance Management/Asset Strategy

T. Cleary Licensing Engineer

G. Closius Licensing Engineer

L. Crone Supervisor, Nuclear Chemistry

C. Dempsey Assistant Plant Manager
J. Dorosky Health Physicist
III [[]]
M. Finnegan Supervisor, Health Physics,

ISFSI

R. Griffin Director, Nuclear Station Safety & Licensing

W. Gorman Supervisor, Instrumentation & Control

J. Grogan Assistant Plant Manager

C. Houska I&C Technician

A. Jordan Site Plant Manager

J. Kunze Supervisor, Nuclear Operations Support

B. Krauth Licensing, Nuclear Technology Specialist

J. Laine, Manager, Radiation Protection/Chemistry

J. Langan Manager, Nuclear Oversight

P. Luckey, Manager, Emergency Preparedness

R. MacManus Director, Engineering

H. McKenney Supervisor, Nuclear Engineering

M. O'Connor Manager, Engineering

D. Presuitti Fire Analyst, Asset Production

A. Price Site Vice President

M. Roche Senior Nuclear Chemistry Technician

J. Semancik Manager, Operations

S. Smith Supervisor, Nuclear Shift Operations Unit 3

J. Spence Manager, Training

S. Turowski Supervisor, Health Physics Technical Services
C. Vournazos

IT Specialist, Meteorological Data

A-2LIST

OF [[]]
ITEMS [[]]
OPENED ,
CLOSED ,
AND [[]]

DISCUSSED Opened

None Opened and Closed

05000336/2008002-01 FIN Failure to Evaluate a Unit 2 Charging System Non-conforming Condition against the Current

Licensing Bases (Section 1R15)05000336/2008002-02 NCV Failure to Identify Unacceptable Unit 2 Charging Pump

Surveillance Test Data (Section 1R22)05000336/2008002-03 NCV Failure to Identify a Service Water Bypass Flow Path

following a Failed

IST (Section 1R22)
LIST [[]]
OF [[]]
DOCUME [[]]
NTS [[]]
REVIEW [[]]
ED Section 1R01: Adverse Weather Protection
AOP -2560, Storms, Winds and High Tides

OP-2336A, Station Drains and Sumps

OP 3352, Heat Tracing, Rev. 013-02

Primary Equipment Operator Outside Logs, 2/12/08

CR-06-07697

CR -06-07890
CR -06-07878
CR -07-09182 CR-07-09725
CR -07-10069
CR -08-01021 CR-08-01261
CR -08-01300 Section 1R04: Equipment Alignment
OPS -OP-2308, Revision 012-01, High Pressure Safety Injection System
OPS -
OP -2340E11, Revision 000-03, "A" Charging Pump Maintenance
OPS -
OP -2340E51, Revision 000-05, "B" Charging Pump Maintenance
OPS -

OP-2340E21, Revision 000-04, "C" Charging Pump Maintenance

OP 3326-008, Emergency Diesel Generator B Service Water System Supply, Rev. 004
OP 3346A-002,
EDG B-Cooling Water Valve Lineup, Rev. 007
OP 3346A-004,
EDG B-Lube Oil Valve Lineup, Rev. 006
OP 3346A-006,
EDG B-Starting Air Valve Lineup, Rev 009-01
OP 3346A-010,

EDG B-Instrument Valve Lineup, Rev. 007-01

OP3346B-2, Valve Lineup for "B" Diesel Fuel System, Rev. 4

OP3346B-007, B Diesel Fuel Oil Electrical Alignment, Rev. 000

Millstone Unit 3 Emergency Diesel Generator Health Report, 2nd & 3rd Quarter 2007.

A-3CR-07-04159

CR -07-06912
CR -07-07679
CR -07-09413 CR-07-10591
CR -07-10632
CR -07-10859 CR-07-10906
CR -07-12668

CR-08-00419 Work Orders: M3020337

M3030831

M3031424

M3050160

M3050814

M3051016 M3051051 M3051762

M3060379

M3060623

M3060944

M3060952 M3060968 M3070296

M3070626

M3070927

M3070942

M3070944 M3071440 M3071455

M3071508

M3071705

M3080037

M3980032

A-4Section 1R05: Fire Protection

FHA Unit 2 "Fire Hazards Analysis" Fire Area A-12 Zone A

FHA Unit 2 "Fire Hazards Analysis" Fire Area A-13

FHA Unit 2 "Fire Hazards Analysis" Fire Area A-14

FHA Unit 2 "Fire Hazards Analysis" Fire Area A-15

FHA Unit 2 "Fire Hazards Analysis" Fire Area A-16

FHA Unit 2 "Fire Hazards Analysis" Fire Area I-1 Zone A

EN 31084, Operating Strategy for Service Water System at Millstone Unit 3, Rev. 007

M3-EV-02-0031, Technical Evaluation for Service Water Heat Exchanger Monitoring Millstone

Unit 3, Rev. 2

Fire Protection Evaluation Report, Millstone Nuclear Power Station Unit 3

Section 1R06: Flood Protection Measures

ERC 25212-

ER-04-0035 Calculation PBD-10B-1

Calculation Number 12179-P(R)-1194

CR-04-03704

Section 1R07: Heat Sink Performance SP 3626.13, Service Water Heat Exchanger Fouling Determination, Rev. 021-00, performed 2/2/08

SP 3626.13, Service Water Heat Exchanger Fouling Determination, Rev. 021-00, performed

2/10/08

EN 31084, Operating Strategy for Service Water System at Millstone Unit 3, Rev. 007

CR-07-02093

CR-07-04204

CR-07-04294

CR-07-04673

Work Orders: M30610651,

3HVQ [[]]

ACUS1B Heat Exchanger Inspection, Performed 6/20/07

M30701961,

3HVQ [[]]

ACUS1B Eddy Current Testing During 3R, Performed 3/7/07

Section 1R11: Licensed Operator Requalification Program Unit 2 Simulator Exam on January 29, 2008 Section 1R12: Maintenance Effectiveness

CR -08-00639

CR-08-00112

CR-07-12005

CR-07-11588

CR-07-11518

CR-07-09409

CR-07-07844

CR-07-07631

CR -07-07492
CR -07-07351

CR-07-06525 CR-07-00616

CR-07-04858

CR-07-07655

CR-07-08585

CR-07-09904

CR-08-01069

CR-07-11516

CR -07-10161
CR -07-08793

CR-07-08774 CR-07-08732

CR-07-08731

CR-07-08730

CR-07-08729

CR-07-05526

CR-07-05113

CR-07-04844

CR-07-04498

CR-06-10759

A-5CR-06-09865

CR -06-08555
CR -06-07674
CR -06-07665 CR-06-04984
CR -06-04971
CR -07-11781 Auxiliary Feedwater System System Health Reports, 1st through 4th Quarters 2007 Millstone Unit 2 Maintenance Rule Scoping Table
CV [[]]

CS-Volume Control (11/14/2007)

Millstone Unit 3 Maintenance Rule (a)(1) Evaluation for the Auxiliary Feedwater System (3322),

Rev. 1

Millstone Unit 3 Maintenance Rule (a)(2) Disposition for the Auxiliary Feedwater Sysyem (3322),

Rev. 0

Maintenance Rule Scoping Table for Auxiliary Feedwater, 2/14/08

MP -24-
MR -FAP730 "Maintenance Rule Goal Setting and Monitoring" (Rev 000-04)
MPS -2

UFASR Chapter 14 Section 14.6, Decreases in Reactor Coolant Inventory

RP-5, Operability Determinations (Rev 006-01)

Millstone Unit 3 Maintenance Rule (a)(1) Evaluation for the Service Water System (3326)

Service Water System Health Report Fourth Quarter 2007

Operability Determination MP3-007-08

Unit 2 Internal Flooding Evaluation

Work Order M30602421 Section 1R13 Maintenance Risk Assessments and Emergent Work Control

CR -08-0422

CR-07-08221

CR-07-09478

CR-08-00162

CR-08-00732

Unit 2 Operator Logs date 1/11/2008

MP -13-
PRA -FAP01.1, Revision 002-4, "Performing (a)(4) Risk Reviews"
MP -13-

PRA-FAP01.1, Performing (a)(4) Risk Reviews, Rev. 002-04

Millstone Power Station Operational Focus Report, 2/13/08

Plan of the Week (T-0) by FEG, Week 0807

Section 1R15: Operability Evaluations Operability Determination

MP 2-024-07, ""D" Channel of
TMLP is Fluctuating between 2010 and
2060 PS [[]]

IA"

Operability Determination

MP 2-004-08,

SSC Affected by the Degraded or Non-Conforming

Condition - ("B" Charging Pump Cycling)

Operability Determination

MP 2-005-08,

PZR Blockhouse Modification Affect on PZR Safety Valve

Setpoints

Operability Determination

MP 2-005-08

PZR Blockhouse Modification Affect on PZR Safety Valve

Setpoints

CR-08-01810

CR-08-00639

A-6Section 1R18: Plant Modifications

DM 3-00-0010-08, Temporary Accumulator Fill from
RWST M3 08-00271, Alternate Method for Filling Accumulators with Hydro Pump
IAW [[]]

DCN DM3-00-

0010-08

OA 8, Housekeeping of Station Buildings, Facilities, Equipment, and Grounds, Rev. 007-03

OP 3310B, Accumulator Low Pressure Safety Injection, Rev. 014-14

212-26913 Sheet 1, Piping & Instrumentation Diagram High Pressure Safety Injection, Rev. 27

50.59 Screening DM3-00-0010-08

CR-07-04711

CR-07-04723

CR -07-10127
CR -07-11511 Section 1R19: Post Maintenance Testing
AMO 11M203519, Priority 1 Maintenance associated with "B" EDG troubleshooting/repair Post Repair/Replacement Component Leakage Test for M3-07-00831 & M3 07 00833
SPROC [[]]

ENG07-3-006, Functional Test of HVQ Units Pressure Control Valves, Rev. 000

Work Orders: M30700831,

3HVQ *

ACU 2A Freon Pressure Control Valve

M30700833,

3HVQ *

ACU 2A Freon Pressure Control Valve

M30801809, Heat Exchanger Inlet Pressure Control Valve Section 1R22: Surveillance Testing

SP 2602A, Reactor Coolant Leakage, Rev. 006-001, Performed 1/16/08

SP 3601F.6, Reactor Coolant System Water Inventory Measurement, Rev. 005-05, Performed

1/15/08

SP 3601F.6-001,
RCS Inventory Balance, Rev. 002-03
SP 3610A.1, Residual Heat Removal Pump 3
RHS *P1A Operational Readiness Test, Rev. 011-05
SP 2605G, Revision 006-02, Containment Isolation System (
CIV ) Stroke Timing IST, Facility 1
SP 2612A, Revision 002-02, ""A"

SW Pump and Facility 1 Discharge Check Valve IST

CR-08-00545

CR-08-00653

CR -08-00659
OP -
AA -102, Revision 1, Operability Determination
DN [[]]

AP-0509, Revision 8, Dominion Nuclear Procedure Adherence and Usage

M2-EV-98-0227, Revision 0, Technical Evaluation for Single Failure Vulnerability Review Section

1EP 6: Emergency Preparedness Millstone Unit 3 Evaluated Exercise

CFD 08-02, March 18, 2008 CR-08-02722

Section 2: Radiation Safety

RPM 1.3.8, Criteria for Dosimetry Issue, Rev. 8

RPM 1.3.13, Bioassay Sampling and Analysis, Rev. 8

RPM 1.3.14, Personnel Dose Calculations and Assessments, Rev. 7
RPM 1.4.1,
ALARA Reviews and Reports, Rev. 7
RPM 1.4.2,

ALARA Engineering Controls, Rev. 2

A-7RPM 1.6.4, Siemens Electronic Dosimetry System, Rev.

4 RPM 2.1.1, Issuance and Control of
RWP s, Rev. 7
RPM 2.1.2,

ALARA Interface with the RWP Process, Rev. 2

RPM 2.1.3, Identification and Control of High Radiological Risk Work, Rev. 2

RPM 5.2.2, Basic Radiation Worker Responsibilities, Rev. 10
RPM 5.2.3,
ALARA Program and Policy, Rev. 3
RPM -
GDL -008, Electronic Dosimeter Alarm Set Points, Rev. 0
RP -
AA -201, Access Controls for High and Very High Radiation Areas, Rev. 0
RP -
AA -202, Radiological Posting, Rev. 0
RP -
AA -220, Radiological Survey Scheduling, Rev. 0
RP -
AA -221, Radiological Survey Records, Rev. 0
RP -
AA -230, Personnel Contamination Monitoring and Decontamination, Rev. 0
RP -
AA -260, Control of Radiography, Rev. 0
MP -
SA -07-61, 2007 Health Physics Continuing Training
MP -

SA-07-60, Radiation Worker Practices at RCA Exits

Field Observation Report Nos. 6351,07-070, 07-014,07-074, 07-077,

CR-07-06128

CR-07-06271

CR-07-06670

CR-07-07990

CR-07-08300

CR-07-08540

CR-07-08670

CR-07-10789

CR-07-11974

CR-07-05589

CR-07-06325

CR-07-06512

CR-07-06794

CR-07-06952

CR-07-07948

CR-07-10540

CR -07-11418
ALA [[]]

RA Evaluations: Nos. 3-08-04, 2-08-02, 3-08-05, 3-08-04, 3-08-06, 2-08-01, 3-08-01, 3-08-

03, 3-08-02

ALA [[]]

RA Council Meeting Minutes: 01/31/2008, 12/14/2007, 07/09/2007

Challenge Board Meeting Handouts/Action Items for 2R18 Projects: Steam Generator Eddy

Current Testing and I&C Tasks

Troubleshooting Plan for

MP 3 Foundation

SRW Sump No. 3

Dose and Dose Rate Alarm Reports for October 2007 through January 2008

Section 40A1: Performance Indicator (PI) Verification

SP 2602A-001, Manual

RCS Leak Rate Determination, Rev. 006-00 SP 2619A-001, Control Room Daily Surveillance, Modes 1&2, Rev. 045-03

SP 2830 Sampling Reactor Coolant for Dissolved Oxygen, Chloride and Fluoride Analysis, Rev.

007-02

SP 2832-001, Reactor Coolant Analysis for Iodines and

DEI-131, Rev. 006-02

SP 3670.1-001, Mode 1-4 Daily and Shiftly Control Room Rounds, Rev. 025-01

A-8SP 3680.1-003, Containment Leakage Trending, Rev. 002-01 SP 3802E, Reactor Coolant Gas Sampling and Analysis, Rev. 001-03

SP 3855, Reactor Coolant Analysis for Dose Equivalent I-131, Rev. 006-00

SP 3855-001, Reactor Coolant Analysis for Dose Equivalent I-131, Rev. 007-00

CR-08-00490

CR -08-00545
CR -08-01054 Section 4
OA 2: Identification and Resolution of Problems
MP 2719J, Emergency Diesel Generator Jacket Coolant and Air Coolant System Maintenance, Rev. 002-02
OP [[]]
3353.MB 4C, Tave Hi Alarm Response Procedure, rev. 005-12
OP -MP-100-1000, Millstone Operations Gard, Rev.
2 SP 3623.2, Turbine Overspeed Protection System Test, Rev. 009-02
CR -03-00479
CR -04-09492
CR -05-03122
CR -05-05281
CR -07-01673
CR -07-02244
CR -07-03190
CR -07-06193
CR -07-09710
CR -07-11322
CR -07-11454
CR -07-11659
CR -07-12231
CR -07-12538
CR -07-12566
CR -07-12703
CR -08-01137
CR -08-01732 Fairbanks Morse Owner's Group Draft Position - Exhaust Gas Leakage In the Jacket Water Cooling System of Opposed Piston Engines, dated July 24, 2006
NRC Information Notice 2004-15, Dual-Unit Scram at Peach Bottom Units 2 and 3, dated July 22, 2004 Operability Evaluation
MP -2-002-08, dated February 9, 2008 Surveillance Form - Periodic

DG Slow Start Operability Test, Facility 2 (Loaded Run), Rev, 003-03, performed March 5, 2008 Vendor Manual 25203-138-002, Installation, Operation and Maintenance of Emergency Diesel Engine, Rev. 2 Work Orders: M20701994 M20709828

A-9LIST

OF [[]]
ACRONY MS
ADA [[]]
MS Agencywide Documents Access and Management System
ALA [[]]

RA as low as reasonably achievable

CBM condition base monitoring
CE [[]]

DE committed effective dose equivalent

CFR Code of Federal Regulations

CLB current licensing basis

CR condition report

dp differential pressure

DRP Division of Reactor Projects

DRS Division of Reactor Safety
EC [[]]

CS emergency core cooling system

EDG emergency diesel generator

EP Emergency Preparedness

ESF engineered safety features
HP [[]]

SI High Pressure Safety Injection

HRA high radiation areas

I&C Instrumentation and Control

IMC inspection manual chapter

IST in-service test

LER licensee event reports
LH [[]]

RA Locked High Radiation Areas

mrem millerem

NCV non-cited violation

NEI Nuclear Energy Institute

NRC Nuclear Regulatory Commission

OA Other Activities

OD operability determination
PA [[]]

RS Publicly Available Records System

PI performance indicator

PI&R problem identification and resolution

PMT post maintenance testing
PO [[]]
RV power operated relief valve
PS [[]]

ID pounds square inch differential

RAI request for additional information

RCA Radiological Controlled Area

RHR residual heat removal
RS [[]]

ST reserve station service transformer

RWP radiological work permit

SDP significance determination process

SIH safety injection high

SIS safety injection system

SW service water
TE [[]]
DE total effective dose equivalent
TM [[]]

LP thermal margin low pressure

TS technical specification

A-10UFSAR Updated Final Safety Analysis Report

VH [[]]
RA very high radiation areas