IR 05000245/2008009

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IR 05000245-08-009, on 03/03/2008 - 04/30/2008, Millstone, Unit 1, PLC Alarm Response
ML081500843
Person / Time
Site: Millstone Dominion icon.png
Issue date: 05/29/2008
From: Ray Lorson
Decommissioning Branch I
To: Christian D
Dominion Resources
References
IR-08-009
Download: ML081500843 (11)


Text

SUBJECT:

MILLSTONE POWER STATION UNIT 1 - SAFSTOR INSPECTION REPORT 05000245/2008009

Dear Mr. Christian:

On April 30, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Millstone Power Station Unit 1. The enclosed inspection report documents the preliminary inspection results, which were discussed on March 5, 2008 with you and other members of your staff. In addition, on May 19, 2008, Mr. Krauth and Mr. Dvorak of your staff were contacted via telephone and a final summary exit was conducted.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations, and with the conditions of your license. The inspector reviewed selected procedures and records, observed activities, and interviewed personnel.

In accordance with 10 CFR Part 2.390 of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA Original Signed By: Mark C. Roberts for:/

Raymond K. Lorson, Chief Decommissioning Branch Division of Nuclear Materials Safety Docket No. 50-245 License No. DPR-21 Enclosure: Inspection Report No. 05000245/2008009 w/ Attachment: Supplemental Information

SUMMARY OF FINDINGS

IR 05000245/2008-009; 03/03/2008 - 04/30/2008; Millstone Power Station U1; PLC Alarm

Response.

The report covered a one-month period of inspection by one region-based inspector. The NRCs program for overseeing the safe operation of a shut-down nuclear power reactor is described in Manual Chapter (MC) 2561, Decommissioning Power Reactor Inspection Program.

NRC-Identified and Self-Revealing Findings

None

Licensee-Identified Violations

None

REPORT DETAILS

Summary of Plant Status

The Millstone site is located in the town of Waterford, Connecticut. Millstone Unit 1 (U1) was a single-cycle, boiling water reactor with a thermal output of 2011 megawatts and a net electrical output of 652.1 megawatts. The plant went into commercial operation on December 28, 1970.

On July 21, 1998, the licensee certified to the NRC that, as of July 17, 1998, U1 had permanently ceased operations and the fuel had been permanently removed from the reactor vessel. Since July 21, 1998, only those conditions or activities associated with the safe storage of fuel and radiological protection (SAFSTOR status) are applicable to the defueled Millstone U1 plant.

OTHER ACTIVITIES

4OA5 Other Activities

.1 Spent Fuel Pool Safety

a. Inspection Scope

(60801 and 71801)

The inspector performed a review of the condition and operational status of structures, systems and components (SSC) important to the safe storage of spent fuel. The inspector reviewed the U1 Defueled Safety Analysis Report (DSAR), Technical Specifications (TS), and Technical Requirements Manual (TRM) and compared these requirements with associated procedures to ascertain that procedures were consistent with the DSAR. The inspector performed walk-downs of the reactor building including, spent fuel pool cooling and ventilation systems, decay heat removal pumps and motors, east corner room, and torus room; the radioactive waste facility to evaluate the general material condition of the facility and equipment (including the radioactive waste facility sump); and the emergency diesel generator (EDG).

b. Findings

No findings of significance were identified.

The inspector toured the facility and verified that systems and components important to the safe storage of spent fuel were operable and adequately maintained. Personnel were knowledgeable of the status of U1 systems and components important to maintaining the safe status of U1. The inspector observed several telltale leak detection stations and noted that there was no obvious indications of active spent fuel pool (SFP)leakage. Material condition of plant equipment and general building areas was adequate. The inspector noted that the radioactive waste facility sumps had overflowed and that condition reports (CRs) had been generated. These CRs are discussed in Section 4OA5.2 of this inspection report. No safety concerns were identified.

The inspector noted that SFP temperature and water level, SFP cooling rates, and decay heat removal (DHR) system flow rates were monitored in accordance with established procedures. Personnel responsible for monitoring these systems were knowledgeable and understood their roles in maintaining safe storage of spent fuel. The systems and operational parameters were maintained within established acceptance criteria.

.2 Self-Assessment, Auditing, and Corrective Action

a. Inspection Scope

(40801)

The inspector reviewed the licensees program for identifying, resolving, and preventing issues that degrade safety or the quality of decommissioning activities. The inspector reviewed the procedures describing the corrective action program (CAP) and reviewed selected CRs, including the CRs related to the inoperability of the radioactive waste (radwaste) building sumps and the CRs related to the loss of normal power to U1 on January 30, 2008. The CRs were reviewed to evaluate the licensees effectiveness in identifying issues that could impact the safe storage of spent fuel and the implementation of associated corrective actions. The inspector discussed the tracking, current status, and closure of selected corrective actions with cognizant personnel.

b. Findings

No findings of significance were identified.

The inspector reviewed the CRs related to the inoperability of the west radwaste floor drain sump pump (M16-8), which occurred in April 2007, and the inoperability of the liquid radwaste sump pump (M-312), which occurred in July 2007. Each condition was self-identified, closed to a trouble report, and repaired through the work order process.

The inspector noted that the jobs were assigned a low priority because they did not impact SSCs important to safety, as defined in the DSAR. The cause of each pump failure was determined and both pumps were replaced. No obvious indications of pump failure have recurred.

The inspector reviewed the CRs related to the loss of power event that occurred on January 30, 2008. Normal power to U1 was lost due to a fault (over-current trip) in the Trayer Switch and related power line, which lead to the off-site power source (Flanders Substation) and subsequently lead to the on-site electrical system. The emergency station service transformer is the on-site electrical system, that supplies power to U1 for normal operations. In response to the loss of power, Dominion entered several off normal procedures and reported the event to the NRC. Dominion established a fire watch and energized an electrical bus to start the EDG. By January 31, Dominion performed a load analysis for the EDG and began to load certain systems and equipment such as, the auxiliary lighting, radiation monitors, heat tracing, and SFP cooling and the DHR pumps. On February 1, Dominion noted that the diesel was not operating at the proper speed because of a defective governor and initiated compensatory measures to obtain and use an offsite backup diesel. Because the EDG was not operating properly, Dominion secured the SFP cooling and DHR pumps to protect them from being damaged.

Also, Dominion contacted the NRC because the spent fuel pool temperature had subsequently increased 1 degree (from 85°F to 86°F) in approximately 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> because the SFP and DHR pumps were off. The U1 TS limit for the spent fuel pool temperature is 150°F. By February 12, Dominion repaired the damage to the Trayer Switch and restored U1 to normal off-site power. After the event, the licensee conducted a post-event debrief and critique, and identified areas for improvement, including procedural enhancements and communication improvements. The inspector noted that the priority for addressing CRs and implementation of corrective actions was adequate and based upon safety significance. The threshold for identification of issues entered into the corrective action program was adequate. Responsible personnel were knowledgeable of the status of corrective actions and had established measures to monitor completion of corrective actions. No adverse trends or safety concerns were identified.

.3 Maintenance and Surveillance

a. Inspection Scope

(62801)

The inspector reviewed Dominions preventive maintenance (PM) program for SSC important for maintaining the safe storage of spent fuel. The review included tracking and trending reports to determine Dominions ability to effectively utilize PM and operator rounds data. The inspector reviewed selected system performance indicator trend data covering a six-month period. Performance data reviewed included SFP temperature and level, SFP and DHR system flow rates, the emergency diesel generator, and U1 maintenance activities. The inspector toured plant areas, observed an annual PM on a DHR motor and pump, and discussed system and component performance with knowledgeable personnel.

b. Findings

No findings of significance were identified.

The inspector noted that, since the previous inspection, Dominion had re-established its dedicated U1 support organization responsible for maintaining U1 SSCs important to the safe storage of spent fuel. The inspector verified that the maintenance for selected systems and components had been conducted within the last six months, in accordance with established procedures. The inspector noted that systems and components were operable and available for service. The inspector noted that the individuals performing the annual PM were knowledgeable of motors and pumps, including the electrical aspects of the PM, and implemented good safety practices during the PM. The inspector also noted that the information obtained during plant equipment operator rounds was utilized in evaluating the adequacy of established PM frequencies and the overall effectiveness of the PM program.

.4 Occupational Radiation Safety

a. Inspection Scope

(83750)

The inspector reviewed implementation of the occupational exposure control program associated with U1 activities. The inspection consisted of interviews with responsible individuals, review of radiological survey plans and radiological survey maps of the radiologically controlled area (RCA), and field observations of radiological postings. The inspector reviewed the 2007 and 2008 year-to-date exposure reports, the 2007 as low as reasonably achievable (ALARA) evaluation for the U1 main steam isolation valve (MSIV) removal project asset recovery activities, and the associated radiation work permit summaries.

b. Findings

No findings of significance were identified.

The inspector noted that the U1 RCA was appropriately posted for radioactive material.

Radiological postings were readily visible, well-maintained, and reflected radiological conditions. The radiological survey maps and related information maintained at the access U1 access point were current.

The inspector noted that the dose total from the U1 2007 and 2008 year-to-date exposure reports were 880 mrem and 49 mrem, respectively. The majority of the exposure during 2007 was attributed to the asset recovery project to remove MSIV# 1-MS-1A from the drywell. From the 2007 ALARA evaluation, the work was budgeted for 305 mrem and was completed for 207 mrem. Pre-job planning and the use of a mock-up to demonstrate plasma cutting were the primary contributors to the low exposure results. The inspector noted that the associated radiation work permit summaries were commensurate with the radiological significance of the task and included the appropriate exposure control measures for the safe implementation of the activity. The inspector noted that the licensee provided adequate controls to limit the exposure of workers to external sources of radiation, posting and labeling of radioactive materials and radiation areas met regulatory requirements, and the radiological controls and dose estimates associated with U1 tasks were effective to achieve dose goals.

4OA6 Meetings, including Exit

Exit Meeting Summary

On March 05, 2008, the inspector presented the preliminary inspection results to Mr. J.A. Price, Site Vice President, and members of his staff. The inspector confirmed that proprietary information was not provided or examined during the inspection. In addition, on May 19, 2008, the licensee was contacted via telephone and a final summary exit was conducted.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

B. Bartron Supervisor, Licensing
D. DelCore Supervisor, Health Physics Operations

D. Dvorak Supervisor Nuclear Maintenance

B. Krauth Licensing, Nuclear Technology Specialist
J. Laine Manager, Radiation Protection/Chemistry
M. Nappi Supervisor, Radiation Protection Support
M. OConnor Manager, Engineering

F.T. Perry Radiation Protection/ALARA Support

T. Petit Engineering Project Management

A. Price Site Vice President

J. Semancik Manager, Operations
D. Smith Acting Director, Nuclear Station Safety & Licensing
G. Sturgeon Operations, Unit 2

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

None

LIST OF DOCUMENTS REVIEWED