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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20043E0991990-05-31031 May 1990 LER 89-018-01:on 890827,cracking Found in Incoloy Alloy 800 Main Steam Ringheaders & Condition Determined to Have Generic Implications.Caused by Creep Failure.Main Steam Ringheaders repaired.W/900531 Ltr ML20042G4211990-05-10010 May 1990 LER 90-001-00:on 900410,non-essential Bus 5,4160/480-volt Transformer N-9215 Experienced Fault.Caused by Breakdown of Insulation on Secondary Coils of Transformer.Coils of Transformer rewound.W/900510 Ltr ML20011D4641989-12-20020 December 1989 LER 89-014-01:on 890818,four Fire Barrier Penetration Seals in Bldg 10 Did Not Meet Foam Seal Structure Criteria of Seal Spec.Caused by Improper Curing During Installation.Fire Watch Established & Seals repaired.W/891220 Ltr ML20024E0021983-07-29029 July 1983 LER 83-023/03L-0:on 830701 & 02,emergency Feedwater Unavailable to Drive Loop I Helium Circulation Water Turbines.Caused by Normal Wear of Valve PV-21243.Valve Internals Replaced & Valve calibr.W/830729 Ltr ML20024B9861983-07-0101 July 1983 LER 83-020/03L-0:on 830604,emergency Feedwater Header Supply to Loop I Helium Circulator Turbine Water Drive Isolated & Bearing Water Make Up Pump Taken Out of Svc.Caused by Flexitallic Gasket Failure Due to Normal wear.W/830701 Ltr ML20024A8521983-06-22022 June 1983 Updated LER 80-041/03X-2:on 800724,one of 12 Helium Circulator Seal Malfunction Pressure Differential Switches Discovered W/Trip Point Outside Tech Spec Limits.Caused by Dirt Accumulation in Electrical switches.W/830622 Ltr ML20023D9021983-05-26026 May 1983 LER 83-017/01T-0:on 830512,insp Performed Per IE Bulletin 83-03 Identified Six of Eight Check Valves Frozen in mid- Position.Caused by Corrosion & Rusting Valve Internal Parts. Valves Cleaned & Internal Components Replaced ML20028G2831983-01-28028 January 1983 LER 82-053/03L-0:on 821229,fuel Storage Well Pressure Exceeded Atmospheric Pressure While Reactor Was Shut Down. Caused by One Gas Compressor Being Out of Svc for Maint and Other Pumping Less than Capacity.Compressors Repaired ML20028G2711983-01-28028 January 1983 LER 82-054/03L-0:on 821229,outlet Temps Exceeded 120 F Limit When Reactor Became Critical During Isolation of Svc Water Flow to Pcrv Cooling Water Hx.Caused by Lack of Cooling Source.Design Change Initiated ML20028F2401983-01-19019 January 1983 LER 82-051/03L-0:on 821220,during Surveillance Test,One of Six Steam Pipe Rupture & One of 12 Steam Pipe Rupture Channels Identified Inoperable Due to Low Response to Calibr Noise.Caused by Failure of Resistor ML20028F2881983-01-17017 January 1983 LER 83-001/01T-0:on 830101 & 02,reactor Operated W/O Min Number of Operable Moisture Monitor Channels Required Per Table 4.4.1 of Limiting Conditions for Operation.Caused by Personnel Misinterpretation of Tech Specs ML20028A3101982-11-10010 November 1982 LER 82-042/03L-0:on 821013,unplanned Radioactive Gas Release Occurred W/Reactor Shutdown & Depressurized.Caused by High Airborne Activity in Reactor Bldg Due to Leaking Blank Flange.Emergency Procedures Initiated.Flange Repaired ML20028A2861982-11-10010 November 1982 LER 82-041/03L-0:on 821011,during Calibr of Radioactive Liquid Effluent Monitors,Trip Point for RIS-6212 Found to Be Less Conservative than Required.Caused by Instrument Drift. High Voltage & Discriminator Settings Adjusted ML20023A7451982-10-0808 October 1982 LER 82-036/03L-0:on 820908,one of Two Bearing Water Makeup Pumps Removed from Svc.Caused by Need to Rebuild Mechanical Seal Due to Normal Wear.Seal Rebuilt ML20052H9881982-05-12012 May 1982 LER 82-011/03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage ML20052H8751982-05-12012 May 1982 LER 82-013/03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned ML20052G4151982-05-10010 May 1982 LER 82-012/03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs ML20052A3331982-04-27027 April 1982 LER 81-044 Has Been Cancelled ML20050B2541982-03-19019 March 1982 LER 82-006/03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels ML20042B8231982-03-17017 March 1982 LER 82-005/03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened ML20041F5791982-03-0808 March 1982 LER 82-007/01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking ML20041C3231982-02-19019 February 1982 LER 82-002/03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr ML20041C2761982-02-19019 February 1982 LER 82-003/03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr ML20041A9891982-02-16016 February 1982 LER 82-004/01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators ML20040G9511982-02-0505 February 1982 LER 82-001/03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired ML20040B8081982-01-13013 January 1982 LER 81-074/03L-0:on 811214,cold Reheat Snubber CRS-219 Found Detached from Pipe Mounting,Rendering Snubber Operable.Caused by Failure of Cotter Pin,Allowing Eyebolt to Be Displaced Out of Pipe & Snubber Rod Mounting ML20040B7911982-01-12012 January 1982 LER 81-075/03L-0:on 811221,two Sample Flow Circuits Found Out of Calibr During Annual Calibr of Primary Coolant Moisture Scram Instrumentation.Caused by Change in Instrument Characteristics.Procedures Being Revised ML20039F4911982-01-0404 January 1982 LER 81-073/03L-0:on 811208,one Helium Circulator Bearing Drain Pressure Low Switch Found to Have Trip Point Outside Required Limits.Caused by Dirt Accumulation in Electrical Switch That Impeded Contact ML20039C6321981-12-17017 December 1981 LER 81-072/03L-0:on 811117,PCRV Rupture Disk M-11701 Setpoint Exceeded Tech Specs Limits.Caused by Belleville Washer Operating Point Drift.Disks Under Evaluation ML20011A6371981-10-22022 October 1981 LER 81-060/03L-0:between 810922-1013,emergency Feedwater to Loop 1 Helium Circulator Water Turbine Drives Was Isolated on Three Occasions.Caused by Leakage Between Seat Ring & Valve Body Pressure Control Valve ML20010H9131981-09-11011 September 1981 LER 81-052/03L-0:on 810812,standby Bearing Water Makeup Pump Removed from Svc.Caused by Need to Repair Bonnet Leak in Valve in Suction Line to Pump.Pump Returned to Svc After Repair Completed ML20010J0141981-09-11011 September 1981 LER 81-050/03L-0:on 810814,total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent for 810809 Was Discovered to Have Exceeded Tech Specs.Caused by Improper Circulating Water Blowdown Arrangement.Blowdown Adjusted ML20010H8821981-09-0404 September 1981 LER 81-048/03L-0:on 810808 & 25 Loop 1 Prestressed Concrete Reactor Vessel Cooling Water Outlet Temp Exceeded 120 F Due to Failure of Temp Controller.Caused by Cold Solder Joint & Failure of Transistor in Output Circuit,Respectively ML20010H9301981-09-0101 September 1981 LER 81-049/03L-0:during 810802-07,increase Occurred in Offgassing from Core & Core Outlet Temps.Caused by Increased Primary Coolant Moisture & Oxidants from Refueling Shutdown ML20010G2711981-08-26026 August 1981 LER 81-046/03L-0:on 810728,emergency Feedwater Supply to Loop 1 Helium Circular Water Turbines Isolated to Repair Leaking 2-inch Consolidated Safety Relief Valves.Caused by Valve Leakage Downstream of Pressure Control Valve ML20010G1691981-08-26026 August 1981 LER 81-045/03L-0:on 810727,during Normal Startup Operation, Primary Coolant Dewpoint Exceeded Tech Spec Limits.Caused by Contamination Due to Moisture.Contaminants Removed from Primary Coolant ML20010G3371981-08-20020 August 1981 LER 81-051/03L-0:on 810721,Class I Snubbers Removed from Svc for Structural Mods W/Plant Operating at Power.Caused by Seismic Restraint Analysis Program.Snubbers Returned to Svc Following Mods ML20010G3181981-08-14014 August 1981 LER 81-043/03L-0:on 810717 & 0807,reactor Operated at Power W/One Class I Snubber Inoperable.Caused by Empty Oil Reservoirs on BFS-398E & MSS-149 Due to Leaking Fitting on Valve Block & Leaking Piston Seal.Fitting Tightened ML20010A1601981-07-16016 July 1981 LER 81-041/03L-0:on 810616,control Room Exhaust Damper Failed to Close.Caused by Dust Accumulation on Damper Vanes. Damper Operated Properly When Retested.Preventive Maint Program to Be Developed to Inspect & Clean Vanes ML20009E5101981-07-0202 July 1981 LER 81-039/03L-0:on 810602,following Routine Chlorination of Circulating Water Sys,Sample Indicated Excessive Residual Chlorine in Plant Liquid Effluent.Cause Unknown.Subsequent Chlorinations Showed No Abnormalities ML20009E5581981-07-0202 July 1981 LER 81-040/03L-0:between 810604 & 09,eight Hydraulic Shock Suppressors Were Found Out of Oil.Caused by Empty Hydraulic Oil Reservoirs Due to Leaking Seals & O-rings in Snubbers. Reservoirs Cleaned.Seals & O-rings Replaced ML20009E7191981-06-18018 June 1981 Revised LER 81-008/03X-1:on 810120,during Shutdown Maint & Primary Coolant Pressure Scram Calibr,Voltage Outputs of Pressure Transmitter Discovered High.Caused by Instrument Drift.Transmitter Calibr.Surveillance Test Completed ML20009E7011981-06-10010 June 1981 LER 81-035/03L-0:on 810511,w/plant at 70% Thermal Power During a Diesel Generator Set Surveillance Test,B Engine Tripped & Declutched.Caused by Failed Exhaust Temp Switch. Switch Repaired.Test Completed.Generator Returned to Svc ML20009A5501981-06-0505 June 1981 LER 81-038/03L-0:on 810507,two Class I Hydraulic Shock Suppressors Removed from Svc.Caused by Decision to Modify Suppressors to Original Configuration W/Zero Bleed Rate Block Valves ML20009A5341981-06-0303 June 1981 LER 81-034/03L-0:on 810504,equipment Necessary to Terminate Release from Liquid Waste Sys & Reactor Sump Found Not Operating Properly.Caused by Plugged Sense Lines on Flow Element Associated W/Control Valve ML20009A5281981-05-28028 May 1981 LER 81-032/03L-0:on 810428,hot Reheat Snubber HRS-244 Found Inoperable.Caused by Empty Hydraulic Oil Reservoir Due to Leaking Elbow Fitting.Fitting Tightened,Reservoir Refilled & Snubber Returned to Svc ML20004D5781981-05-27027 May 1981 LER 81-036/01T-0:on 810512,liquid Waste Discharge Exceeded Specified Limit for Tritium Concentration.Caused by Design Deficiency.Downstream of Valve HV 6212,150-200 Gallon Dead Leg Released Regardless of Dilution Flow Adequacy ML20004D7171981-05-27027 May 1981 LER 81-031/03L-0:on 810427,during Normal Surveillance Testing,Diesel Engine B Tripped & Declutched on Starting. Caused by Load Imbalance Between Engines a & B Due to Normal Wear of Linkage.Linkage Was Adjusted ML20004D6661981-05-27027 May 1981 LER 81-033/03L-0:on 810427,helium Circulator 1C Speed/Wobble Modifier Malfunctioned Causing Loss of Plant Protective Sys Functions to High Speed Trip Circuits.Caused by Electronic Circuit Unbalance.Spare Speed Element Installed 1993-06-03
[Table view] Category:RO)
MONTHYEARML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20043E0991990-05-31031 May 1990 LER 89-018-01:on 890827,cracking Found in Incoloy Alloy 800 Main Steam Ringheaders & Condition Determined to Have Generic Implications.Caused by Creep Failure.Main Steam Ringheaders repaired.W/900531 Ltr ML20042G4211990-05-10010 May 1990 LER 90-001-00:on 900410,non-essential Bus 5,4160/480-volt Transformer N-9215 Experienced Fault.Caused by Breakdown of Insulation on Secondary Coils of Transformer.Coils of Transformer rewound.W/900510 Ltr ML20011D4641989-12-20020 December 1989 LER 89-014-01:on 890818,four Fire Barrier Penetration Seals in Bldg 10 Did Not Meet Foam Seal Structure Criteria of Seal Spec.Caused by Improper Curing During Installation.Fire Watch Established & Seals repaired.W/891220 Ltr ML20024E0021983-07-29029 July 1983 LER 83-023/03L-0:on 830701 & 02,emergency Feedwater Unavailable to Drive Loop I Helium Circulation Water Turbines.Caused by Normal Wear of Valve PV-21243.Valve Internals Replaced & Valve calibr.W/830729 Ltr ML20024B9861983-07-0101 July 1983 LER 83-020/03L-0:on 830604,emergency Feedwater Header Supply to Loop I Helium Circulator Turbine Water Drive Isolated & Bearing Water Make Up Pump Taken Out of Svc.Caused by Flexitallic Gasket Failure Due to Normal wear.W/830701 Ltr ML20024A8521983-06-22022 June 1983 Updated LER 80-041/03X-2:on 800724,one of 12 Helium Circulator Seal Malfunction Pressure Differential Switches Discovered W/Trip Point Outside Tech Spec Limits.Caused by Dirt Accumulation in Electrical switches.W/830622 Ltr ML20023D9021983-05-26026 May 1983 LER 83-017/01T-0:on 830512,insp Performed Per IE Bulletin 83-03 Identified Six of Eight Check Valves Frozen in mid- Position.Caused by Corrosion & Rusting Valve Internal Parts. Valves Cleaned & Internal Components Replaced ML20028G2831983-01-28028 January 1983 LER 82-053/03L-0:on 821229,fuel Storage Well Pressure Exceeded Atmospheric Pressure While Reactor Was Shut Down. Caused by One Gas Compressor Being Out of Svc for Maint and Other Pumping Less than Capacity.Compressors Repaired ML20028G2711983-01-28028 January 1983 LER 82-054/03L-0:on 821229,outlet Temps Exceeded 120 F Limit When Reactor Became Critical During Isolation of Svc Water Flow to Pcrv Cooling Water Hx.Caused by Lack of Cooling Source.Design Change Initiated ML20028F2401983-01-19019 January 1983 LER 82-051/03L-0:on 821220,during Surveillance Test,One of Six Steam Pipe Rupture & One of 12 Steam Pipe Rupture Channels Identified Inoperable Due to Low Response to Calibr Noise.Caused by Failure of Resistor ML20028F2881983-01-17017 January 1983 LER 83-001/01T-0:on 830101 & 02,reactor Operated W/O Min Number of Operable Moisture Monitor Channels Required Per Table 4.4.1 of Limiting Conditions for Operation.Caused by Personnel Misinterpretation of Tech Specs ML20028A3101982-11-10010 November 1982 LER 82-042/03L-0:on 821013,unplanned Radioactive Gas Release Occurred W/Reactor Shutdown & Depressurized.Caused by High Airborne Activity in Reactor Bldg Due to Leaking Blank Flange.Emergency Procedures Initiated.Flange Repaired ML20028A2861982-11-10010 November 1982 LER 82-041/03L-0:on 821011,during Calibr of Radioactive Liquid Effluent Monitors,Trip Point for RIS-6212 Found to Be Less Conservative than Required.Caused by Instrument Drift. High Voltage & Discriminator Settings Adjusted ML20023A7451982-10-0808 October 1982 LER 82-036/03L-0:on 820908,one of Two Bearing Water Makeup Pumps Removed from Svc.Caused by Need to Rebuild Mechanical Seal Due to Normal Wear.Seal Rebuilt ML20052H9881982-05-12012 May 1982 LER 82-011/03L-0:during 820412-20,plant Operated in Degraded Mode of Limiting Conditions for Operation 4.2.11 Three Times & 4.2.10 Once.Caused by Offgas of Moisture from Core as Plant Returned to Power from Maint Outage ML20052H8751982-05-12012 May 1982 LER 82-013/03L-0:on 820412,separation in Axial Positions of Two Partially Inserted Control Rod Groups Fell Slightly Below Limit of 10 Ft.Cause Not Stated.Control Rods Repositioned ML20052G4151982-05-10010 May 1982 LER 82-012/03L-0:on 820410,at 10% Power,Instrument Air Compressor 1C Temporarily Taken Out of Svc to Repair after- Cooler Leak.Water Leak Caused by Normal Wear of after- Cooler.Air Compressor Returned to Svc After Repairs ML20052A3331982-04-27027 April 1982 LER 81-044 Has Been Cancelled ML20050B2541982-03-19019 March 1982 LER 82-006/03L-0:on 820218,primary Coolant Moisture Exceeded Tech Specs.Caused by Contamination W/Moisture During Maint Outage.Reactor Shutdown & Coolant Purification Trains Utilized to Reduce Impurity Levels ML20042B8231982-03-17017 March 1982 LER 82-005/03L-0:on 820215,loop 2 Steam Generator Penetration Rupture Disk 1 Leak Alarm Pressure Switch Found Isolated.Caused by Closed Pressure Switch Isolation Valve.Valve Opened ML20041F5791982-03-0808 March 1982 LER 82-007/01T-0:on 820222,control Rod Pairs for Regions 7 & 28 Did Not Insert Automatically Following Manual Scram. Possibly Caused by Binding or Sticking of Control Rod Drive Mechanism.Control Rods Exercised to Eliminate Sticking ML20041C3231982-02-19019 February 1982 LER 82-002/03L-0:on 820121,during Surveillance Testing, W/Reactor Shut Down,Three Loss of Bearing Water Pressure Differential Switches Found W/Setpoints Less Conservative than Required.Caused by Instrument Drift.Switches Recalibr ML20041C2761982-02-19019 February 1982 LER 82-003/03L-0:on 820122,one Drain Malfunction Pressure Differential Switch on 1C Helium Circulator Found Less Conservative than Tech Specs.Caused by Dirty Contacts. Contacts Cleaned & Switch Recalibr ML20041A9891982-02-16016 February 1982 LER 82-004/01T-0:on 820202,inadvertent Radioactive Liquid Waste Release Occurred from Receiver a During Plant Shutdown for Design Mods to Circulator Auxiliary Sys.Caused by Improper Valve Lineup.Event Reviewed W/Operators ML20040G9511982-02-0505 February 1982 LER 82-001/03L-0:on 820108,18 Snubbers Found Inoperable During Surveillance Testing,Indicating Inoperability During Reactor Operation.Caused by Seal Leakage & Deficiencies in Piston Position & Oil Level.Snubbers Repaired ML20040B8081982-01-13013 January 1982 LER 81-074/03L-0:on 811214,cold Reheat Snubber CRS-219 Found Detached from Pipe Mounting,Rendering Snubber Operable.Caused by Failure of Cotter Pin,Allowing Eyebolt to Be Displaced Out of Pipe & Snubber Rod Mounting ML20040B7911982-01-12012 January 1982 LER 81-075/03L-0:on 811221,two Sample Flow Circuits Found Out of Calibr During Annual Calibr of Primary Coolant Moisture Scram Instrumentation.Caused by Change in Instrument Characteristics.Procedures Being Revised ML20039F4911982-01-0404 January 1982 LER 81-073/03L-0:on 811208,one Helium Circulator Bearing Drain Pressure Low Switch Found to Have Trip Point Outside Required Limits.Caused by Dirt Accumulation in Electrical Switch That Impeded Contact ML20039C6321981-12-17017 December 1981 LER 81-072/03L-0:on 811117,PCRV Rupture Disk M-11701 Setpoint Exceeded Tech Specs Limits.Caused by Belleville Washer Operating Point Drift.Disks Under Evaluation ML20011A6371981-10-22022 October 1981 LER 81-060/03L-0:between 810922-1013,emergency Feedwater to Loop 1 Helium Circulator Water Turbine Drives Was Isolated on Three Occasions.Caused by Leakage Between Seat Ring & Valve Body Pressure Control Valve ML20010H9131981-09-11011 September 1981 LER 81-052/03L-0:on 810812,standby Bearing Water Makeup Pump Removed from Svc.Caused by Need to Repair Bonnet Leak in Valve in Suction Line to Pump.Pump Returned to Svc After Repair Completed ML20010J0141981-09-11011 September 1981 LER 81-050/03L-0:on 810814,total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent for 810809 Was Discovered to Have Exceeded Tech Specs.Caused by Improper Circulating Water Blowdown Arrangement.Blowdown Adjusted ML20010H8821981-09-0404 September 1981 LER 81-048/03L-0:on 810808 & 25 Loop 1 Prestressed Concrete Reactor Vessel Cooling Water Outlet Temp Exceeded 120 F Due to Failure of Temp Controller.Caused by Cold Solder Joint & Failure of Transistor in Output Circuit,Respectively ML20010H9301981-09-0101 September 1981 LER 81-049/03L-0:during 810802-07,increase Occurred in Offgassing from Core & Core Outlet Temps.Caused by Increased Primary Coolant Moisture & Oxidants from Refueling Shutdown ML20010G2711981-08-26026 August 1981 LER 81-046/03L-0:on 810728,emergency Feedwater Supply to Loop 1 Helium Circular Water Turbines Isolated to Repair Leaking 2-inch Consolidated Safety Relief Valves.Caused by Valve Leakage Downstream of Pressure Control Valve ML20010G1691981-08-26026 August 1981 LER 81-045/03L-0:on 810727,during Normal Startup Operation, Primary Coolant Dewpoint Exceeded Tech Spec Limits.Caused by Contamination Due to Moisture.Contaminants Removed from Primary Coolant ML20010G3371981-08-20020 August 1981 LER 81-051/03L-0:on 810721,Class I Snubbers Removed from Svc for Structural Mods W/Plant Operating at Power.Caused by Seismic Restraint Analysis Program.Snubbers Returned to Svc Following Mods ML20010G3181981-08-14014 August 1981 LER 81-043/03L-0:on 810717 & 0807,reactor Operated at Power W/One Class I Snubber Inoperable.Caused by Empty Oil Reservoirs on BFS-398E & MSS-149 Due to Leaking Fitting on Valve Block & Leaking Piston Seal.Fitting Tightened ML20010A1601981-07-16016 July 1981 LER 81-041/03L-0:on 810616,control Room Exhaust Damper Failed to Close.Caused by Dust Accumulation on Damper Vanes. Damper Operated Properly When Retested.Preventive Maint Program to Be Developed to Inspect & Clean Vanes ML20009E5101981-07-0202 July 1981 LER 81-039/03L-0:on 810602,following Routine Chlorination of Circulating Water Sys,Sample Indicated Excessive Residual Chlorine in Plant Liquid Effluent.Cause Unknown.Subsequent Chlorinations Showed No Abnormalities ML20009E5581981-07-0202 July 1981 LER 81-040/03L-0:between 810604 & 09,eight Hydraulic Shock Suppressors Were Found Out of Oil.Caused by Empty Hydraulic Oil Reservoirs Due to Leaking Seals & O-rings in Snubbers. Reservoirs Cleaned.Seals & O-rings Replaced ML20009E7191981-06-18018 June 1981 Revised LER 81-008/03X-1:on 810120,during Shutdown Maint & Primary Coolant Pressure Scram Calibr,Voltage Outputs of Pressure Transmitter Discovered High.Caused by Instrument Drift.Transmitter Calibr.Surveillance Test Completed ML20009E7011981-06-10010 June 1981 LER 81-035/03L-0:on 810511,w/plant at 70% Thermal Power During a Diesel Generator Set Surveillance Test,B Engine Tripped & Declutched.Caused by Failed Exhaust Temp Switch. Switch Repaired.Test Completed.Generator Returned to Svc ML20009A5501981-06-0505 June 1981 LER 81-038/03L-0:on 810507,two Class I Hydraulic Shock Suppressors Removed from Svc.Caused by Decision to Modify Suppressors to Original Configuration W/Zero Bleed Rate Block Valves ML20009A5341981-06-0303 June 1981 LER 81-034/03L-0:on 810504,equipment Necessary to Terminate Release from Liquid Waste Sys & Reactor Sump Found Not Operating Properly.Caused by Plugged Sense Lines on Flow Element Associated W/Control Valve ML20009A5281981-05-28028 May 1981 LER 81-032/03L-0:on 810428,hot Reheat Snubber HRS-244 Found Inoperable.Caused by Empty Hydraulic Oil Reservoir Due to Leaking Elbow Fitting.Fitting Tightened,Reservoir Refilled & Snubber Returned to Svc ML20004D5781981-05-27027 May 1981 LER 81-036/01T-0:on 810512,liquid Waste Discharge Exceeded Specified Limit for Tritium Concentration.Caused by Design Deficiency.Downstream of Valve HV 6212,150-200 Gallon Dead Leg Released Regardless of Dilution Flow Adequacy ML20004D7171981-05-27027 May 1981 LER 81-031/03L-0:on 810427,during Normal Surveillance Testing,Diesel Engine B Tripped & Declutched on Starting. Caused by Load Imbalance Between Engines a & B Due to Normal Wear of Linkage.Linkage Was Adjusted ML20004D6661981-05-27027 May 1981 LER 81-033/03L-0:on 810427,helium Circulator 1C Speed/Wobble Modifier Malfunctioned Causing Loss of Plant Protective Sys Functions to High Speed Trip Circuits.Caused by Electronic Circuit Unbalance.Spare Speed Element Installed 1993-06-03
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
[Table view] |
Text
NRC FORM 384 U.S. NUCLEAR REGULATO%Y COMMISSION csm Q' LICENSEE EVENT REPORT CONTROL 8 LOCK: l 1
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(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) lo TTI 7 8 9 l C l LICENSEE o l F l CODE S l V l 14l !@l 15 0 l 0 l - l 0 LICENSE l 0 l 0NUMBER l 0 l 0 l- l 0 l 0 25l@l264 l 1LICENSE l 1 l 2TYPEl 040l@l5 7 CATl l@
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7 8 60 61 DATE 75 REPORT DATE EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h 10121 l On Thursday, March 13,1980, at 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br />, while the plant was operating at less l l0l3l l than 2% power, it was determined that due to the orifice valve in region 31 being l gl more open than the orifice valves in the other seven-column regions, all orifice l lo lsi l valves were not set for equal flows and the temperature limit of LCO 4.1.9, Figure l l0 is l l 4.1.9-2 was exceeded. This is being reported per Fort St. Vrain Technical Specifi- l l 0 l 71 l cation AC 7.5.2(a)2. No accompanying occurrence. No affect on public health and l loIal I safety. l 7 8 9 80 E CODE SL8C DE COMPONENT CODE SUSCODE SU E 10l9l 7 8 l R l B l@ W@ lZ l@ l Zl Zl Zl Zl Zl Zlh W@ W @
9 10 11 12 13 18 19 20
_ SECUENTIAL OCCURRENCE REPORT REVISION Lg g ,po EVENT YE AR REPORT No. CODE TYPE NO.
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_ 21 22 23 24 26 27 28 29 30 31 32 K N AC O P NT MET HoVRS S8 i FOR 8. SUPPLI MANUFAC RER lJ3Xl@[_Zj@34 l3b Zl@ [_Zj@
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44 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l3 lO; j Inability to close orifice valve to equal flow position, coupled with personnel I gl interpretation of Technical Specifications, resulted in operation outside the limits I l i 121 l of LCO 4.1.9, Figure 4.1.9-2. Valve freed uo. Personnel re-i n s truc te rt . Personnel l I,l j l instructed that written record to be maintained on future interpretations. Techni- l gl cal Specification LCO 4.1.9 to be amended for clarification. I 7 8 9 80
$A % POWER OTHER STATUS Ol$ RY DISCOVERY DESCRIPTloN l1 15 l W@ l0 l0 l1 l@lN/A l l A l@l Personnel Observation l A T1vlTY CO TENT RELEASED QP RELEASE IIl6l [_Z_j @ W @ lN/A AMOUNT OF ACTIVITY lN/A @ lLOCATION oF RELEASE @ l PERSONNEL EXPOS ES NuMSER TYPE oESCRiPTiON @
g l 0 l 0 l 0 l@l Z l@l N/A l PERSONNE t iNJUliES NuuSER oESCRiPTiON@
t a l 0 l 0 l 0 l@l12N/A l 7 8 9 Il 80 LOSS OF oR DAMAGE To FACILITY Q TYPE DESCRIPTION v y l Z l@l N/A o0099in "
. gll l l 7 8 9 10 80 g ISSUE @l DESCRIPTION N/A l llllllllll lllj 7 8 9 10 68 69 80 5 l
//// // . . . . . . . (1011 785-2253 9
March 13, 1980 MR. KARL V. SEYFRIT REGION IV REGULATORY OPERATIONS NUCLEAR REGULATORY COMMISSION 611 RIAN PLAZA DRIVE, SUITE 1000 ARLINGTON, TEXAS 76012 ON THURSDAY, MARCH 13,1980, AT 0830 HOURS, WHILE THE PLANT WAS OPERATING AT LESS THAN 2% POWER, IT WAS DETERMINED THAT DUE TO THE ORIFICE VALVE IN REGION 31 BEING MORE OPEN THAN THE ORIFICE VALVES IN THE OTHER SEVEN COLUMN REGIONS, ALL ORIFICE VALVES WERE NOT SET FOR EQUAL FLOWS AND THE TEMPERATURE LIMIT OF LCO 4.1.9, FIGURE 4.1.9-2 WAS EXCEEDED. ALTHOUGH THE BASIS OF LCO 4.1.9 ADDRESSES LOW HELIUM FLOW RATES WHICH WOULD RESULT FROM A CLOSED ORI-FICE VALVE, THE LCO DOES NOT ALLOW FOR INTERPRETATION OF ONLY THAT CONDITION.
AN INVESTIGATION IS IN PROGRESS TO IDENTIFY THE CAUSE.
THIS EVENT APPEARS TO BE REPORTABLE OCCURRENCE NO. 50-267/80-12/01-T-0 AND IS REPORTABLE PER FORT ST VRAIN TECHNICAL SPECIFICATION AC 7.5.2(a)2.
PLEASE CONFIRM RECEIPT OF THIS TRANSMITTAL BY CALL BACK TO J. W. GAHM AT (303) 785-6300.
J. W. GAHM NUCLEAR GENERATING STATION FORT ST. VRAIN PUBLIC SERVICE CONPANY OF COLORADO 550 FIFTEENTH STREET, DENVER, COLORADO 80202 I
l I
1
REPORT DATE: March 25, 1980 REPORTABLE OCCURRENCE 80-12 ISSUE O OCCURRENCE DATE: March 11. 1980 Page 1 of 7 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO 16805 WELD COUNTY ROAD 19 1/2 PLATTEVILLE, COLORADO 80651 REPORT NO. 50-267/80-12/01-T-1 FINAL IDENTIFICATION OF OCCURRENCE:
On Thursday, March 13,1980, at 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br />, while the plant was operating at less than 2% power, it was determined that due to the orifice valve in region 31 being more open than the orifice valves in the other seven column regions, all orifice valves were not set for equal f18ws and the temperature limit of LCO 4.1.9, Figure 4.1.9-2 was exceeded.
This is being reported per Fort St. Vrain Technical Specification AC 7.5.2(a)2.
CONDITIONS PRIOR-TO OCCURRENCE:
Routine startup.
The major plant parameters at the time of the event were as follows:
Reactor Power 7.58 MRth, 0.9%
Electrical Power 0 MWe Secondary Coolant Pressure 876 psig Secondary Coolant Temperature 223*F.
Secondary Coolant Flow 423,900 #/hr.
Primary Coolant Pressure 366 psia Primary Coolant Core Inlet Temperature 212*F.
Primary Coolant Core Outlet Temperature 242*F.
Primary Coolant Flow 277,000 #/hr., 7.9%
Circulator 1A Self-Turbining Circulator 1B 2,200 RPM Circulator 1C 2,200 RPM Circulator 1D Self-Turbining
REPORTABLE OCCURRENCE 80-12 ISSUE O Page 2 of 7 l
DESCRIPTION OF CCCURRENCE:
Prior to reactor startup on March 11, 1980, core orifice valves had been adjusted for equal flow settings, with the exception of the region 31 orifice valve, which was stuck in a position more open than that required for equal flows.
The reactor was taken critical at 2120 hours0.0245 days <br />0.589 hours <br />0.00351 weeks <br />8.0666e-4 months <br /> on March 11, 1980. At that time, requirements of LCO 4.1.7 and 4.1.9 dealing with core orifices and region temperature rise were met. With the core orifice valves set for other than equal flows, the provisions of LCO 4.1.9, Figure 4.1.9-2 were applicable.
When verification of compliance with Technical Specifications occurred at approximately 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on March 11, 1980, requirements of LCO 4.1.7 were still being met, but the temperature rise limits of LCO 4.1.9, Figure 4.1.9-2 had been exceeded for a number of core regions. In checking the requirements of LCO 4.1.9, the operator noted that the basis of this speci-I fication is addressed to prevent very low flow conditions which would exist l as the result of a nearly closed orifice valve. With the region 31 orifice i
I stuck in a more open position, the LCO requirements did not appear to be applicable. The operator discussed his interpretation of the Technical Specification requirements with supervisory personnel. It was determined that the intent of the LCO was met, and that no excessive fuel temperatures would be expected with the temperature rise across some regions outside the allowable limits of LCO 4.1.9, Figure 4.1.9-2. Based on this inter-pretation, no action was required, and none was taken.
The interpretation outlined above was discussed with on-coming shif t personnel, and reactor operation continued at a fairly constant power level of approximately 1.8%. Continued attempts to close the valve to equal flow position were unsuccessful, .ad a Plant Trouble Report was initiated at 0510 hours0.0059 days <br />0.142 hours <br />8.43254e-4 weeks <br />1.94055e-4 months <br /> on March 12, 1980. Technical Specification com-pliance verifications utilizing the above interpretation continued until 1615 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.145075e-4 months <br /> on March 12, 1980, at which time the valve was freed and returned to the proper setting, and equal flow conditions were restored.
j For equal flow conditions, Figure 4.1.9-2 is not applicable. Subsequent compliance verifications indicated that the requirements of both LCO 4.1.7 and LCO 4.1.9, Figure 4.1.9-1 were met.
APPARENT CAUSE OF OCCURRENCE:
Inability to close the orifice valve in region 31 to the equal flow position, coupled with the interpretation of the Technical Specification taken by operations personnel, resulted in a condition where the temperature rise limits of LCO 4.1.9, Figure 4.1.9-2 were exceeded.
REPORTABLE OCCURRENCE 80-12 ISSUE O l Page 3 of 7 ANALYSIS OF OCCURRENCE:
Prior to taking the reactor critical, verification is made to assure com-pliance with all applicable Technical Specifications. At the time of the reactor startup on March 11, 1980, core orifice valves had been set for equal flow conditions, with the exception of the orifice valve for ;
region 31. For startup conditions, equal flow settings of 17% open for seven column regions and 10% open for five column regions are utilized. 1 The orifice valve for region 31 (a seven-column region) was sticking at a 26% open position.
A verification of Technical Specification compliance indicated that re-quirements of both LCO 4.1.7 and LCO 4.1.9 were met. LCO 4.1.7(b) requires that for core average outlet temperatures less than or equal to 950*F.,
individual region outlet temperatures are not to exceed the core average outlet temperature plus 400*F. This LCO also specifies that the requirements of LCO 4.1.9 must be met. For the conditions which existed with core orifices 3 set at other than equal flow positions and the reactor pressurized to greater l than 50 psia, the maximum allowable helium coolant temperature rise across !
a region as a function of power level is specified by Figure 4.1.9-2. I Technical Specification compliance was again verified at approximately 2300 hours0.0266 days <br />0.639 hours <br />0.0038 weeks <br />8.7515e-4 months <br /> on March 11, 1980, j ust prior to shif t change. At that time, i l
it appeared that the temperature rise limits of LCO 4.1.9, Figure 4.1.9-2 l had been exceeded for some core regions. At the time of the compliance verification, total helium flow was approximately 8.5% with a reactor power level of approximately 0.4%. This "overblowing" condition ensures ;
that very low helium coolant flow rates could not exist in any coolant i channel. Based on this condition, the operator on duty initiated a review of the basis of LCO 4.1.9. Af ter noting that neither low helium flow rates nor excessive temperature conditions existed, the operator further noted that the basis of the LCO had been directed to conditions which would exist if an orifice valve were stuck in a more closed position than required for equal flows. This review seemed to indicate that the LCO was not ap-plicable under the conditions prevailing at the time - an interpretation which was agreed to by supervisory personnel. Based on the interpretation that Figure 4.1.9-2 limits were not applicable, it was determined that l requirements for compliance with LCO 4.1.9 had been satisfied. No action with regard to meeting Figure 4.1.9-2 temperature requirements was required.
Although no written record of the interpretation was entered in the logs, on-coming personnel were made aware of the interpretation being used to verify compliance with LCO 4.1.9, concurred, and used this interpretation for subsequent compliance verifications.
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l ,
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REPORTABLE OCCURRENCE 80-12 ISSUE O Page 4 of i ANALYSIS OF OCCURRENCE: (Cont'd)
Continuing attempts were made to close the valve and establish equal flow corditions. At 0510 hours0.0059 days <br />0.142 hours <br />8.43254e-4 weeks <br />1.94055e-4 months <br /> on March 12, 1980, a Plant Trouble Report was initiated regarding inability to close the region 31 orifice valve to the equal flow position. At approximately 1615 hours0.0187 days <br />0.449 hours <br />0.00267 weeks <br />6.145075e-4 months <br /> on March 12, 1980, the valve was feed and closed to the equal flow position of ap-proximately 17%. Following return to equal flow conditions, the requirements of LCO 4.1.9, Figure 4.1.9-2 were no longer applicable. At that time, total helium flow was 8.9%, which was well above the Figure 4.1.9.1 re-quirement of 7% for the 1.2% power level which existed at the time.
At 0830 hours0.00961 days <br />0.231 hours <br />0.00137 weeks <br />3.15815e-4 months <br /> on March 13, 1980, a review of the logs and Plant Trouble Reports for the time period beginning at 2152 hours0.0249 days <br />0.598 hours <br />0.00356 weeks <br />8.18836e-4 months <br /> on March 11, 1980, indicated that although the intent of LCO 4.1.9 was not violated, the LCO makes no provisions for the type of interpretation taken by the personnel involved. The intent of the LCO is to prevent very low helium flow rates and corresponding excessive fuel temperatures. The temperature rise limits of Figure 4.1.9-2 were developed based on the assumption of a nearly closed orifice valve. Neither low flow rates nor excessive temperatures existed during the period of unequal flow settings. Upon return to equal flow settings, no abnormal temperature changes were observed, indicating that no stagnant flow conditions had existed. Refer to Figure 1 for comparative information at 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on March 12,1980, (with unequal flow conditions) and 1100 hours0.0127 days <br />0.306 hours <br />0.00182 weeks <br />4.1855e-4 months <br /> on March 13,1980 (with equal flow conditions) . Orifice positions and temperatures for the region with the stuck orifice valve are boldly outlined. Note that the change in shim group and rod position was due to rod insertion to compensate for Xenon burn-out.
Although a review of the data available and the basis of the LCO supports the interpretation that Figure 4.1.9-2 requirements were not applicable, a strict interpretation of the Technical Specifications provides no leeway for the more open orifice valve position or for conditions of "overblowing" the core which existed at the time. Thus, this situation is being reported per AC 7.5.2(a)2.
i y .--
~~ ,
, - .. FIGURE 1- REPORTABLE OCCURRENCE 80-12 ORIFICE POSITIONS ISSUE O AND REGION OUTLET Page 5 of'7' TEMPERATURES n' n s, ne m a Orifice 16.7. 10.1 Positions
16.7 " 460 421 0.0 " Region Outlet 8
(% OPan 16.8 1* "
Temperatures 451 i. '
17.1 " " 413 "
ly 0 ,
437 M9 .
' 16.8
451 '
451 n
0*
16.9 = n 587 n 16.4 " "
17.0 17.0 i
, 9,9 490 6.8 17.1 401 . 430 400
550 543 a
-16.7
, 17.0 438 , 384 16.7 16.8 . E, "
500 n
" 568 1 .0 a 27.8 ,, 16.8 406 "
4 = 17.2 6.6 .
426 388 17.2 a 441 a Untq l 17.0 a 10. 15 a M n 386 ,
17.2 "
Flow Po-0.1 16.8 432 382 sition 401 ,
1 Data / Time: March 12, 1980, 1100 hrs. Operating Circulators: A and C l
Reactor Power: 1.6% Reactor Pressure: 407 psia Primary Coolant Flow: 8.6% -
Shim Group / Position: 4B/41.5"
, Avarage Temperature Rise: '172*F.
n n n n Orifice " "
16.6 10.1 468 425 Positions a 16.8 s'
(% oPsn 10.0 " 17.2 Region Outlet "
p 16.7 Tempe ratures 463 " 386
,, , ,, 407 9 ,,
1 .0 16.7 ,
16.7 456 3 ' l 17.0 , ,
408
" 16.9 " " 438 l n , u 560 a 584 ,
17.1 17.1 , 478 .
,7 17.1 4.9 391 . 432 408 l
- " 53 u *g 16.9 u n 545 543 n
10.
16.7
386
, 16.8 80 a
" 16.8 16.7 "
,, 559 n 16.9 n 16.9 n n
16.7 16.6 451 406 ,
" 386 n 419 l 17,1 n 429 17.4
si 0. a l Flow Po- :=
17,1 a I
sition 10.1 16.8 377 409 439 Dats/ Time: March 13,1980,1100 hrs. Operating Circulators: A and D Reactor Power: 1.9% Reactor Pressure: 394 psia Primary Coolant Flow: 8.8% Shim Group / Position: 2A/138.5" Avarage Temperature Rise: 175'F.
REPOT. TABLE OCCURRENCE 80-12 ISSUE O Page 6 of 7 CORRECTIVE ACTION:
Continued attempts to close the stuck crifice valve to the equal flow po-sition were successful, and the valve is now operable.
Personnel have been instructed to make a literal interpretation of the LCO.
Operations personnel were instructed that if interpretations are made in the future, a written record of the interpretation is to be entered in the logs.
An amendment to clarify the intent and applicability of LCO 4.1.9 is being prepared and will be submitted to the commission for approval and imple-mentation upon completion.
No further corrective action is anticipated or required.
FAILURE DATA /SIMILAR REPORTED OCCURRENCES:
None PROGRAMMATIC IMPACT:
None CODE IMPACT:
None l
I
REPORTABLE OCCURRENCE 80-12 ISSUE O Page 7 of 7 Prepared By: tC tr -
- f. 2c!)
Cathy C.fHirsch Technical Services Technician Reviewed By:
f.W.Gahm Technical Services Supervisor Reviewed By:
Frank M. Mathie Operations Manager Approved By: /b M4;< [e Don Warembourg g Manager, Nuclear Production