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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML19338C4441980-08-11011 August 1980 Ro:On 800804,radioactivity Released in Reactor Bldg.Caused by Helium Circulator Sys Malfunction.Employee Safety Not Jeopardized,Atmospheric Release Negligible & Public Not in Danger ML19318A8991980-06-18018 June 1980 Ro:On 800501 & 0617,minute Releases of Radioactivity Occurred in Reactor Bldg.Caused by Malfunction in Helium Circulator Sys.No Radiation Was Released Into Atmosphere. Public & Personnel Health & Safety Were Not Jeopardized ML19225A2211979-07-12012 July 1979 RO 50-267/77-17(14)1,final on 770506:during Plant Startup at 15% Power,Incorrect Feedwater Flow Trip Existed in 1 of 2 Plant Protective Sys Logics.Caused by Logic Chip Failure in Circular Trip Module CT-2B2 ML19225A1181979-07-12012 July 1979 RO 50-267/76-19A on 760617:while Reactor Was in Shutdown Condition,One Steam Water Dump Valve in Each Loop Opened. Caused by Design Problem.Failure Modes & Effects Analyzed & Steam Water Dump Circuits Revised ML19224D5841979-07-0303 July 1979 RO 50-26/79-13/03-L-0 on 790412:365 Hydraulic Snubbers Found to Be Inoperable During First Functional Test,Causing Both Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Repaired ML20052F1261976-06-14014 June 1976 Ro:On 760521,discrepancies Found in Seismic Certifications for Equipment,Instruments & Components & in Application of Certain Components Required to Meet Seismic Conditions. Caused by Misinterpretation of FSAR Requirements 1980-08-11
[Table view] Category:LER)
MONTHYEARML19338C4441980-08-11011 August 1980 Ro:On 800804,radioactivity Released in Reactor Bldg.Caused by Helium Circulator Sys Malfunction.Employee Safety Not Jeopardized,Atmospheric Release Negligible & Public Not in Danger ML19318A8991980-06-18018 June 1980 Ro:On 800501 & 0617,minute Releases of Radioactivity Occurred in Reactor Bldg.Caused by Malfunction in Helium Circulator Sys.No Radiation Was Released Into Atmosphere. Public & Personnel Health & Safety Were Not Jeopardized ML19225A2211979-07-12012 July 1979 RO 50-267/77-17(14)1,final on 770506:during Plant Startup at 15% Power,Incorrect Feedwater Flow Trip Existed in 1 of 2 Plant Protective Sys Logics.Caused by Logic Chip Failure in Circular Trip Module CT-2B2 ML19225A1181979-07-12012 July 1979 RO 50-267/76-19A on 760617:while Reactor Was in Shutdown Condition,One Steam Water Dump Valve in Each Loop Opened. Caused by Design Problem.Failure Modes & Effects Analyzed & Steam Water Dump Circuits Revised ML19224D5841979-07-0303 July 1979 RO 50-26/79-13/03-L-0 on 790412:365 Hydraulic Snubbers Found to Be Inoperable During First Functional Test,Causing Both Unacceptable Lockup & Bleed Characteristics.Caused by Setpoint Drift,Dirty Oil & Clogged Valves.All Repaired ML20052F1261976-06-14014 June 1976 Ro:On 760521,discrepancies Found in Seismic Certifications for Equipment,Instruments & Components & in Application of Certain Components Required to Meet Seismic Conditions. Caused by Misinterpretation of FSAR Requirements 1980-08-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20196G6731997-07-0101 July 1997 Informs Commission That Decommissioning Process Has Been Completed at PSC of Colorado Fsvngs,Unit 1 Located in Town of Platteville in Weld County,Co ML20141K9961997-05-0505 May 1997 Safety Evaluation Supporting Amend 89 to License DPR-34 ML20140E1121997-04-10010 April 1997 Confirmatory Survey of Group Effluent Discharge Pathway Areas for Fsv Nuclear Station,Platteville,Co ML20134D1661997-01-30030 January 1997 Rev 1,Vol 6 to Final Survey Rept,Final Survey of Group E (Book 2A of 2) ML20137S6111996-12-31031 December 1996 Annual Rept Pursuant to Section 13 or 15(d) of Securities Exchange Act 1934, for Fy Ended Dec 1996 ML20134G6401996-10-29029 October 1996 Rev 0,Volume 6,Books 1 & 2 of 2 to Final Survey of Group E ML20134G6171996-10-29029 October 1996 Rev 2,Volume 1,Books 1 & 2 of 2 to Final Survey Description & Results ML20134G7271996-10-29029 October 1996 Rev 0,Volume 11,Book 1 of 1 to Final Survey of Group J ML20134G6861996-10-29029 October 1996 Rev 0,Volume 8,Books 1 & 2 of 2 to, Final Survey of Group G ML20134G6321996-10-26026 October 1996 Rev 1,Volume 5,Books 2 & 3 of 3 to Final Survey of Group D ML20133D7831996-10-22022 October 1996 Preliminary Rept - Orise Support of NRC License Insp at Fsv on 960930-1003 ML20116A4661996-07-19019 July 1996 Fsv Final Survey Exposure Rate Measurements ML20112J6861996-05-31031 May 1996 June 1996 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning.Rept Covers Period of 960216-0531 ML20112C1531996-05-17017 May 1996 Fsv Final Survey Exposure Rate Measurements ML20101G5521996-03-21021 March 1996 Confirmatory Survey Activities for Fsv Nuclear Station PSC Platteville,Co, Final Rept ML20097E3201996-01-31031 January 1996 Nonproprietary Fort St Vrain Technical Basis Documents for Piping Survey Instrumentation ML20095K4131995-12-26026 December 1995 Rev 3 to Decommissioning Plan ML20095H7211995-12-20020 December 1995 Revs to Fort St Vrain Decommissioning Fire Protection Plan Update ML20095K9751995-12-15015 December 1995 Fort St Vrain Project Update Presentation to NRC, on 951207 & 15 ML20096C1671995-12-13013 December 1995 Rev 4 to Decommissioning Fire Protection Plan ML20094M1651995-11-30030 November 1995 Nonproprietary Fsv Technical Basis Documents for Piping Survey Implementation ML20092F3461995-09-14014 September 1995 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning, Covering Period of 950516-0815.W/ ML20137H3531994-12-31031 December 1994 Partially Withheld, Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, App D,Comments by Mkf & Westinghouse Team & Responses ML20137S2331994-12-31031 December 1994 Rept of Independent Counsel Investigation Concerning Issues at Fort St Vrain Nuclear Generating Station Decommissioning Project, Dec 1994 ML20029C6031993-12-31031 December 1993 1993 Annual Rept Public Svc Co of Colorado. W/940405 Ltr ML20058Q3791993-12-21021 December 1993 Rev 1 to Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20045B3641993-06-30030 June 1993 June 1993 Quarterly 10CFR50.59 Rept of Changes,Tests & Experiments for Fsv Decommissioning. ML20045A4291993-06-0303 June 1993 LER 93-003-00:on 930505,new Source of Natural Gas Introduced within 0.5 Miles of ISFSI & Reactor Bldg W/O Prior NRC Approval.Caused by Field Routing of Natural Gas Pipe.Well Isolated by Well operator.W/930603 Ltr ML20077D1631993-05-10010 May 1993 Enforcement Conference, in Arlington,Tx ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20128D7191992-12-0101 December 1992 Safety Evaluation Approving Exemption from Requirement of 10CFR50.54(q) to Change to Biennial Emergency Plan Exercise Rather than Annual Following Completion of Next Scheduled Exercise at Plant ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20127F5691992-11-0303 November 1992 Informs Commission of Intent to Issue Order Approving Plant Decommissioning Plan & Corresponding Amend to License DPR-34 ML20101E5761992-05-31031 May 1992 Monthly Defueling Operations Rept for May 1992 for Fort St Vrain ML20096E8221992-04-30030 April 1992 Monthly Operating Rept for Apr 1992 for Fort St Vrain.W/ ML20095E9601992-04-17017 April 1992 Rev to Fort St Vrain Proposed Decommissioning Plan ML20100R7431992-03-31031 March 1992 Monthly Operating Rept for Mar 1992 for Fort St Vrain.W/ ML20090L0621992-02-29029 February 1992 Monthly Operating Rept for Feb 1992 for Fort St Vrain Unit 1 ML20092D0081992-01-31031 January 1992 Monthly Operating Rept for Jan 1992 for Fort St Vrain Nuclear Generating Station ML20102B2241992-01-22022 January 1992 Fort St Vrain Station Annual Rept of Changes,Tests & Experiments Not Requiring Prior Commission Approval Per 10CFR50.59, for Period 910123-920122 ML20094N6701991-12-31031 December 1991 Public Svc Co Annual Financial Rept for 1991 ML20091J6251991-12-31031 December 1991 Monthly Operating Rept for Dec 1991 for Fort St Vrain.W/ ML20094D6711991-11-30030 November 1991 Monthly Operating Rept for Nov 1991 for Fort St Vrain Unit 1 ML20090M1871991-11-20020 November 1991 FOSAVEX-91 Scenario for 1991 Plant Exercise of Defueling Emergency Response Plan ML20086D6891991-11-15015 November 1991 Proposed Decommissioning Plan for Fort St Vrain Nuclear Generating Station ML20085N1451991-11-0505 November 1991 Revised Ro:Operability Date of 910830 for Electric Motor Driven Fire Water Pump P-4501 Not Met.Pump Not Actually Declared Operable Until 911025.Caused by Unforseen Matl & Testing Problems.Equivalent Pump Available ML20086C5451991-10-31031 October 1991 Monthly Operating Rept for Oct 1991 for Fort St Vrain.W/ ML20085H6611991-10-10010 October 1991 Assessment of Mgt Modes for Graphite from Reactor Decommissioning ML20091D7671991-10-0101 October 1991 Rev B to Engineering Evaluation of Prestressed Concrete Reactor Vessel & Core Support Floor Structures for Proposed Sys 46 Temp Change ML20085D9861991-09-30030 September 1991 Monthly Operating Rept for Sept 1991 for Fort St Vrain.W/ 1997-07-01
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W C1'4 C CC C V Ci '4 i F C.- U n i
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. CCNTCL ELCCK l l l l l l l (pLEASE D AINT ALL AE3UIRED 1.*;FC AM AT:CN 1 6 LEENSEE NAME LCENSE EN E N T LCENSE NLveFQ 'voE fvat b lC l0 !? lS lV l114 7 89 0 !0l-l0I0l0l0l0l-l0l0l l 4l 1 1l2l0l [ l 15 25 26 30 31 32 CATELAY Ya[ s$$aN =ccxET NLMCEE EVENT CATE RE8C A T O A ?E
[CJ1]CCN r 7 8 l l lT l: l 01510 l- l 0 l 2 l 617 016l1l7l7[6l 0l7 12 l 719 57 56 59 50 61 da 69 74 75 6C EVENT CESC9;PY:CN o2 l Wile the reactor was in a cold shutdown conditica, operations personnel observed that 7 89 ec h lone steam water duca valve in each loop was open. Failure modes and ef fects analyzed. l 7 89 ec
[CIdl Steam water dura circuits revised. l 7 39 gg C,l5 l l
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NAME: l* N* CdhU NCNE: (303) 785-2253
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P2 PORT DATE: July 12, 1979 A3 NORMAL OCCURRENCE 76-19A Page 1 of 6 OCCURRE' ICE DATE: June 17, 1976 FORT ST. VRAIN NUCLEAR GENERATING STATION PU3LIC SERVICE COMPANY OF COLORADO P. O. BOX 361 PLATIEVILLE, COLORADO 80651 REPORT NO. 50-267/ 76-19A Final IEI.;TIFICATION OF OCCURRENCE:
On June 17, 1976, one steam / water dump valve in each loop was open. This has been identified as an abnormal occurrence per the Fort St. Vrain Technical Specifications, Section 2.1, paragraph f.
CONDITIONS PRIOR TO OCCURRENCE: S teady State Power Routine Shutdown Hot Shutdown Routine Load Change X Cold Shutdown Other (specify)
Refueling Shutdown Routine Startup The major plant parameters at the time of the event were as follows:
Power RTR 0 YJth ELECT 0 YJe Secondarf Coolant Pressure
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1,000 psig Temperature 174 *F Flow 100,000 #/hr.
Primary Coolant Pressure 340 psig Temperature 194 *F Core Inlet 194 *F Core Outlet Flow *
- /hr.
347 031 -
ABNORMA1. OCCURRENCE 76-19A Page 2 of 6 CONDITIONS PRIOR TO OCCURRENCE (continued) :
The reactor operator was =aking a routine check of the plant control boards and noticed that a s ea=/ water du=p valve in each loop was open and the alarm light was lit.
APPARENT CAUSE I 0F OCCURRENCE: X Design Unusual Se rvice Cond.
I Including Environ =ent Manufacture Co=penent Failure Ins tallation/Const. Other (specify)
Op era tor Procedure ANALYSIS OF OCCURRENCE:
Reference attached Figure 1 which shows two parallel du=p valves in a loop and the trip signals which will open a du=p valve. Loop 1 and Loop 2 du=p valves discharge to a co==en s team / water du=p tank. Figure 2 shows the inter-locks which were required to be closed to open a s team / water dump valve. If a loop steam / water du=p valve is open, its relay must be energized. Th e en-ergized relay and position switches on the open valve interlock and should prevent automatic opening of either steam / water du=p valve in tF1 other loop.
The seal in circuit also insures that operator action is required to close an open valve by utilizing the hand switch.
The manual bypass can open a valve in each loop but this also requires opera-tor action.
The steam water du=p valves were tested on June 16, 1976, per approved surveil-lance test S R 5 - 3.1-Q .
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bb b
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ABNORMAL OCCL"ARENCE 76-19A
? age 3 of 6 CORRE CTIVE ACTION:
f Approved test, T-46, tested the s team water du=p valve circuitry. The relay l logic system operated as specified and thers was no explanation f or the simul-taneous opening of a s team / water du=p valve in each loop.
Failure modes and effect analysis was perfor=ed. For the s team water du=p circuit as it existed, the analysis did not identify any other unacceptable
, system consequences than were known to exist. These were (1) the potential l for a concurrent du= of Loops 1 and 2 with the permissible nu=ber of moisture
'
monitors out of service and tripped acco=panied by an instrument bus f ailure, and (2) du=p inhibit of Loops 1 and 2 due to single integrated circuit chip failures. For the proposed modified design, the analysis indicated both the
- unacceptable system consequences stated above were eliminated and no others
! were introduced. Based on the results of these analyses, it was concluded
[ that the design modifications to the steam / water du=p system satisfy all Plant Protective System requirements and are consistent with the original design
{, basis of the plant.
t t
i The following describes the modifications resulting from various analysis of i the Fort S t. Vrain steam water dump system circuitry. The modifications are as follows:
'
- l. Made the auto =atic trip upon moisture monitor system f ailure a manual action; and revised the logic to per=it individual manual trip of the associated =cisture monitor (as opposed to disabling by pairs) .
The moisture monitor trip outputs (reflected light) were revised to transmission logic. The alar =.s and indications have been reviewed to assure that the operator is advised of moisture monitor system failure and enable him to readily ascertain manually tripped channels.
+
- 2. Revised the relay interlocks to eli=inate an undesirable single f ailure
- nhibit problem. See Reportable Occurrence Report No. 50-267/77-
'7(14)A.
.
, 3. Removed the temporary time delay relay modification.
I l The modified circuits have b een functionally tested successfully, i
l The applicable operating procedure has been revised.
l l No further corrective action is anticipated or required.
FAILURE DATA /SIMILAR REPORTED OCCURRENCES:
None PROGRA"MATIC IMP ACT:
None CODE IMPACT:
None )k!
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ABNOFXAL OCCUIL" '!CE 7G-19A
, Page 4 of e T
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l HYDRAULIC Y I LOOP 1 VALVES SET , 1 STEAM GENERATOR
- ENE.~GlZE "
MODULES l
TO CLOSE l AAAAAA CHECK Y VALVE bl
- vs N k i FEEDWATER BLOCK REGULATING 6._ __ _ _ _ _ _ _ _ _ . _ _ _ ,
VALVE VALVE I I y . .. _ _
_q , ,
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l i ,
I l .:'
T HIGH REACTOR I
-'
MOISTURE q/ \/ HYDRAULIC
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LEVIL SIGNALS
---t VALVES SET I
ENERGlZE
- :# E TO OPEN l From Loo; HV-2215 y 2 Dump HIGH REACTOR l
!
{ h Valves OUMP -
PRESSURE SIGNALS
---i VALVES y
l L.O. L.O.
I ig.
I g OTHER PLANT ,,,_,___J '
SIGNALS DUMP TANK l V /
\
. h Steam / water du=p syste= (Loop 1)
FIGURE 1
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347 03f
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A3:!OR".AL OCCURRE!!CE 76-19A Page 5 of 6
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Stea=/ water dump actuating signals (1) Both Loop 2 du=p valve relay CR-2216 and CR- --
2218 de-energized % (1 T --
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(2) Both Loop 2 dump valves Manual Bypass closed (position switches }
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on Loop 2 valves). r- gg 11-
_4--
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In (3) Loop 1 or Loop 2 feedwater flow low.
(
1 Prior to Circuit Revis ion f
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_
T (4) -Open whee _ Loop 2 T
(S) Hand switch. #l I CR Loop 1 du=p valve (6).
l (1) Relay contacts are open if the Loop 2 dump relay is energized; closed if de-energized.
(2) Valve position switches are on each Loop 2 dump valve. Contacts open it valve is not fully closed, closed if valve is closed.
(3) Contacts open if Loop 1 or Loop 2 feedwater flow is low.
(l. ) Open if Loop 2 is shutdown by PPS.
(5) Hand switch utilized to terminate a stea=/ water du=p whan required; contact no r= ally closed.
(6) Relay controlling or.e Loop 1 du=p valve relay cust energize to open a Loop 1 dump valve.
FIGURE 2 3 t(7 036 -
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A3 NORMAL OCCURRENCE 76-19A Page 6 of 6 Prepared by: W A, Micpael J. Ferr1[- j Technical Services Engineer Reviewed by-J G4h5 f W.
chnical Services Supervisor Reviewed by: 6 Frank M. Mathie Operations Manager Approved by: W4vu '
Don Warembourg Manager, Nuclear Productuan bk 0
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