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| {{#Wiki_filter:}} | | {{#Wiki_filter:LAKE ENGINEERING CO. P.O. Box296 10 Austin Avenue Greenville, RI 02828 Tel: 401-949-4733 Fax: 401-949-0220 December 5, 2017 U S Nuclear Regulatory Commission Attn: Document Control Room Washington, DC 20555-0001 |
| | |
| | ==Subject:== |
| | Potentially Degraded Snubber SF1154 Hydraulic Fluid Batch 14ELVS145 Final Report per 10 CFR Part 21 This letter reflects new information available since our interim ~eport dated November 3, 2017. Three Mile Island We have concluded that a substantial safety hazard does not exist at this plant as a result of the subject fluid. _ Millstone**, . . We have concluded that a substantial safety hazard does not exist at this plarit as a result oMhe |
| | * subject fluid. * |
| | * The status of the subject issue as it applies to US nuclear plants to which SF1154 fluid from Batch 14ELVS145 was shipped by Lake Engineering Company is summarized in the following table. Millstone Fluid used in some installed snubbers No substantial safety hazards exist. Nine Mile Point , Fluid not used No substantial safety hazards exist. Duane Arnold Fluid not used No substantial safety hazards exist. Monticello Fluid not used No substantial safety hazards exist. Pilgrim Fluid not used No substantial safety hazards exist. Three Mile Island Fluid used in some installed snubbers No substantial safety hazards exist. Grand Gulf Fluid used in some installed snubbers No substantial safety hazards exist. Peach Bottom Fluid used in some installed snubbers No substantial safety hazards exist. |
| | U S Nuclear Regulatory Commission Potentially Degraded Snubber SF1154 Hydraulic Fluid Batch 14ELVS145 Final Report per 1 O CFR Part 21 December 5, 2017 Page2 If there are any questions or if additional information is required, please contact the writer by mail or by phone using the contact information provided above or by email at dbrown@lakeengineeringri.com. DPB/d/let120517.nrc cc: P. Guay-QA Mgr. Very truly yours, LAKE ENGINEERING COMPANY D. P. Brown, P.E. President |
| | }} |
Revision as of 20:17, 22 April 2018
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Category:Deficiency Correspondence (per 10CFR50.55e and Part 21)
MONTHYEARML24239A3972024-08-23023 August 2024 Rssc Wire & Cable LLC Dba Marmon - Part 21 Final Notification - 57243-EN 57243 ML20279A5772020-11-23023 November 2020 U.S. Nuclear Regulatory Commission'S Analysis of Public Service Enterprise Group Nuclear, LLC Decommissioning Plans Update for Salem Generating Station, Hope Creek Generating Station and Peach Bottom Independent Sfsis ML20296A2762020-10-0606 October 2020 Lake Engineering Co. - Third Interim Notification Per 10 CFR Part 21 - Degraded Snubber SF1154 Hydraulic Fluid Batch No. 17BLVS293 ML19325C0942019-11-0707 November 2019 Potentially Degraded Snubber SF1154 Hydraulic Fluid Batch ZJS1518 Final Report Per 10 CFR Part 21 ML19263A6662019-09-0909 September 2019 Lake Engineering Co. - Third Interim Notification Per 10 CFR Part 21: Degraded Snubber SF1154 Hydraulic Fluid Batch No. ZJS1518 ML19080A0592019-03-0808 March 2019 Interim Report of Potential 10CFR Part 21, Eaton A200 Series Starters/Contactors ML19008A0432019-01-0404 January 2019 Third Interim Notification Per 10 CFR Part 21 Degraded Snubber SF1154 Hydraulic Fluid Batch No. 11KLVS146 ML19029A1552018-12-27027 December 2018 10 CFR21 Reporting of Defects and Non-Compliance - Engine Systems, Inc. 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[Table view] |
Text
LAKE ENGINEERING CO. P.O. Box296 10 Austin Avenue Greenville, RI 02828 Tel: 401-949-4733 Fax: 401-949-0220 December 5, 2017 U S Nuclear Regulatory Commission Attn: Document Control Room Washington, DC 20555-0001
Subject:
Potentially Degraded Snubber SF1154 Hydraulic Fluid Batch 14ELVS145 Final Report per 10 CFR Part 21 This letter reflects new information available since our interim ~eport dated November 3, 2017. Three Mile Island We have concluded that a substantial safety hazard does not exist at this plant as a result of the subject fluid. _ Millstone**, . . We have concluded that a substantial safety hazard does not exist at this plarit as a result oMhe
- The status of the subject issue as it applies to US nuclear plants to which SF1154 fluid from Batch 14ELVS145 was shipped by Lake Engineering Company is summarized in the following table. Millstone Fluid used in some installed snubbers No substantial safety hazards exist. Nine Mile Point , Fluid not used No substantial safety hazards exist. Duane Arnold Fluid not used No substantial safety hazards exist. Monticello Fluid not used No substantial safety hazards exist. Pilgrim Fluid not used No substantial safety hazards exist. Three Mile Island Fluid used in some installed snubbers No substantial safety hazards exist. Grand Gulf Fluid used in some installed snubbers No substantial safety hazards exist. Peach Bottom Fluid used in some installed snubbers No substantial safety hazards exist.
U S Nuclear Regulatory Commission Potentially Degraded Snubber SF1154 Hydraulic Fluid Batch 14ELVS145 Final Report per 1 O CFR Part 21 December 5, 2017 Page2 If there are any questions or if additional information is required, please contact the writer by mail or by phone using the contact information provided above or by email at dbrown@lakeengineeringri.com. DPB/d/let120517.nrc cc: P. Guay-QA Mgr. Very truly yours, LAKE ENGINEERING COMPANY D. P. Brown, P.E. President