Information Notice 2002-10, Manual Reactor Trip and Steam Generator Water Level Setpoint Uncertainties: Difference between revisions

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{{#Wiki_filter:UNITED STATES
{{#Wiki_filter:UNITED STATES


NUCLEAR REGULATORY COMMISSION
===NUCLEAR REGULATORY COMMISSION===
OFFICE OF NUCLEAR REACTOR REGULATION


OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, DC 20555-0001


WASHINGTON, DC 20555-0001 June 28, 2002 NRC INFORMATION NOTICE 2002-10, SUPPLEMENT 1:                 DIABLO CANYON MANUAL
===June 28, 2002===
NRC INFORMATION NOTICE 2002-10, SUPPLEMENT 1:


===DIABLO CANYON MANUAL===
REACTOR TRIP AND STEAM
REACTOR TRIP AND STEAM


GENERATOR WATER LEVEL
===GENERATOR WATER LEVEL===
 
SETPOINT UNCERTAINTIES
SETPOINT UNCERTAINTIES


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failure of the main feedwater regulating valve, non-conservative steam generator setpoints and
failure of the main feedwater regulating valve, non-conservative steam generator setpoints and


contributing causes, and other licensee actions relating to these events. This supplement
contributing causes, and other licensee actions relating to these events. This supplement


provides information that became available after the issuance of the original information notice
provides information that became available after the issuance of the original information notice


(IN). The NRC expects that recipients will review the information for applicability to their
(IN). The NRC expects that recipients will review the information for applicability to their


facilities and consider taking actions, as appropriate. However, this supplement does not
facilities and consider taking actions, as appropriate. However, this supplement does not


contain any NRC requirements and does not require any specific action or written response.
contain any NRC requirements and does not require any specific action or written response.
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automatic reactor trip and emergency feedwater actuation on low-low water level in the steam
automatic reactor trip and emergency feedwater actuation on low-low water level in the steam


generator (LER 1-2002-001-00). The NRC issued IN 2002-10 on March 7, 2002, to inform
generator (LER 1-2002-001-00). The NRC issued IN 2002-10 on March 7, 2002, to inform


licensees of this event. Following the issuance of the original IN, the NRC staff conducted a
licensees of this event. Following the issuance of the original IN, the NRC staff conducted a


Special Inspection at Diablo Canyon, as well as a public meeting with Westinghouse. In
Special Inspection at Diablo Canyon, as well as a public meeting with Westinghouse. In


addition, Diablo Canyon has completed its Licensee Event Reports (LERs), Westinghouse has
addition, Diablo Canyon has completed its Licensee Event Reports (LERs), Westinghouse has
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ML021820008
ML021820008


IN 2002-10 Sup 1 level of Steam Generator 2-4. The indicated narrow-range water level decreased to 7.5 percent
IN 2002-10 Sup 1 level of Steam Generator 2-4. The indicated narrow-range water level decreased to 7.5 percent


and leveled out. Operators tripped the Unit 2 reactor within approximately 1 minute after the
and leveled out. Operators tripped the Unit 2 reactor within approximately 1 minute after the


main feedwater regulating valve closed. On February 14, 2002, after the Unit 2 restart but while
main feedwater regulating valve closed. On February 14, 2002, after the Unit 2 restart but while


still investigating the event, the licensee identified a potentially unanalyzed condition involving
still investigating the event, the licensee identified a potentially unanalyzed condition involving


the narrow-range steam generator water level instrumentation. The licensee determined that
the narrow-range steam generator water level instrumentation. The licensee determined that


during the plant transient, the actual water level in steam generator 2-4 fell below the 7.2- percent narrow-range trip setpoint for engineered safety feature and reactor trip actuations
during the plant transient, the actual water level in steam generator 2-4 fell below the 7.2- percent narrow-range trip setpoint for engineered safety feature and reactor trip actuations


before operators manually tripped the reactor. The steam generator vendor attributed this
before operators manually tripped the reactor. The steam generator vendor attributed this


water-level discrepancy to a previously unaccounted for differential pressure created by steam
water-level discrepancy to a previously unaccounted for differential pressure created by steam


flow past the mid-deck plate in the moisture separator section of the steam generator. This
flow past the mid-deck plate in the moisture separator section of the steam generator. This


differential pressure phenomenon caused the steam generator narrow-range instruments to
differential pressure phenomenon caused the steam generator narrow-range instruments to


indicate a higher-than-actual water level. Thus, the steam generator narrow-range water level
indicate a higher-than-actual water level. Thus, the steam generator narrow-range water level


low-low setpoint was non-conservative during the loss of normal feedwater transient.
low-low setpoint was non-conservative during the loss of normal feedwater transient.


===Physical Phenomenon and System Description===
===Physical Phenomenon and System Description===
Steam generators designed by Westinghouse incorporate two-stage moisture separation. The
Steam generators designed by Westinghouse incorporate two-stage moisture separation. The


first stage uses centrifugal separators, and the second stage uses chevron-type separators. A
first stage uses centrifugal separators, and the second stage uses chevron-type separators. A


mid-deck divider plate separates the two stages. The steam generator water level
mid-deck divider plate separates the two stages. The steam generator water level


instrumentation uses differential pressure instruments with two ranges, a wide-range non- safety-related instrument and three or four (depending on plant) narrow-range safety-related
instrumentation uses differential pressure instruments with two ranges, a wide-range non- safety-related instrument and three or four (depending on plant) narrow-range safety-related


instruments. The wide-range instrument spans essentially the entire length of the downcomer
instruments. The wide-range instrument spans essentially the entire length of the downcomer


region, while the narrow-range instruments span only the upper 25 percent of the wide-range to
region, while the narrow-range instruments span only the upper 25 percent of the wide-range to


cover the normal operating band. The upper taps for all four instruments are located above the
cover the normal operating band. The upper taps for all four instruments are located above the


mid-deck plate, while the lower taps are all located below this plate.
mid-deck plate, while the lower taps are all located below this plate.
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as orifices which restricted steam flow and allowed pressure differences with water levels
as orifices which restricted steam flow and allowed pressure differences with water levels


below the mid-deck region. At higher steam flow rates with a decreasing steam generator
below the mid-deck region. At higher steam flow rates with a decreasing steam generator


water level, steam exiting the first stage separators along with the moisture being separated
water level, steam exiting the first stage separators along with the moisture being separated


was enough to build up pressure below the plate that was not acting above the plate. Since the
was enough to build up pressure below the plate that was not acting above the plate. Since the


upper steam generator water level instrument taps were connected above the plate, a pressure
upper steam generator water level instrument taps were connected above the plate, a pressure
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difference acted on the four instruments and provided a bias that caused the instruments to
difference acted on the four instruments and provided a bias that caused the instruments to


indicate a higher-than-actual level. For the limiting safety setting of the low-low steam
indicate a higher-than-actual level. For the limiting safety setting of the low-low steam


generator water level setpoint, this bias acts in the non-conservative direction. The magnitude
generator water level setpoint, this bias acts in the non-conservative direction. The magnitude


of the bias drops as the steam flow decreases.
of the bias drops as the steam flow decreases.
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Following this event, the NRC completed an onsite special team inspection at Diablo Canyon
Following this event, the NRC completed an onsite special team inspection at Diablo Canyon


Nuclear Power Plant. The inspection examined the events surrounding the Unit 2 reactor trip
Nuclear Power Plant. The inspection examined the events surrounding the Unit 2 reactor trip


on February 9, 2002, as they relate to safety and compliance with the Commissions rules and
on February 9, 2002, as they relate to safety and compliance with the Commissions rules and


regulations and the conditions of the Diablo Canyon license. The inspection consisted of
regulations and the conditions of the Diablo Canyon license. The inspection consisted of


examining procedures and records, and interviewing station personnel and staff members, as
examining procedures and records, and interviewing station personnel and staff members, as


well as the reactor plant contractor. The NRCs Special Inspection Team also developed a
well as the reactor plant contractor. The NRCs Special Inspection Team also developed a


detailed sequence of events and organizational response time line which is summarized in the
detailed sequence of events and organizational response time line which is summarized in the
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IN 2002-10 Sup 1 This event provided an unusual challenge to the licensee in that it involved an unrecognized
IN 2002-10 Sup 1 This event provided an unusual challenge to the licensee in that it involved an unrecognized


phenomenon. Many plant events involve equipment behaving in an unexpected manner, but
phenomenon. Many plant events involve equipment behaving in an unexpected manner, but


the failure mechanisms are usually well-understood. However, a well-structured corrective
the failure mechanisms are usually well-understood. However, a well-structured corrective


action process should still be effective under these circumstances by being sufficiently rigorous
action process should still be effective under these circumstances by being sufficiently rigorous
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to recognize conditions that are adverse to quality and then treating them according to their
to recognize conditions that are adverse to quality and then treating them according to their


safety significance. From a review of the post trip review, the NRCs Special Inspection Team
safety significance. From a review of the post trip review, the NRCs Special Inspection Team


concluded that the licensees process was narrowly focused on finding, understanding, and
concluded that the licensees process was narrowly focused on finding, understanding, and


correcting the cause of the trip. While the stations post-trip analysis procedure contained steps
correcting the cause of the trip. While the stations post-trip analysis procedure contained steps


to review plant behavior before, during, and after the event, this was effectively not performed.
to review plant behavior before, during, and after the event, this was effectively not performed.
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behavior expected under those conditions, the licensee failed to recognize that an automatic
behavior expected under those conditions, the licensee failed to recognize that an automatic


plant trip and ESF actuation of auxiliary feedwater did not occur when required. Had this been
plant trip and ESF actuation of auxiliary feedwater did not occur when required. Had this been


recognized, the licensee would probably have delayed restarting the plant until after the cause
recognized, the licensee would probably have delayed restarting the plant until after the cause
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wide-range indication did not track with narrow-range indication, which was thought to have
wide-range indication did not track with narrow-range indication, which was thought to have


indicated accurately. The NRCs Special Inspection Team concluded that the licensees theory
indicated accurately. The NRCs Special Inspection Team concluded that the licensees theory


and supporting data were not compared with other available but conflicting indications. The
and supporting data were not compared with other available but conflicting indications. The


licensee calculated that the event would have resulted in loss of approximately 75 percent of
licensee calculated that the event would have resulted in loss of approximately 75 percent of
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the initial water mass in the affected steam generator, and should have caused the wide-range
the initial water mass in the affected steam generator, and should have caused the wide-range


level to be 20 percent of the actual level. The licensee did not note that the bottom of the
level to be 20 percent of the actual level. The licensee did not note that the bottom of the


narrow-range corresponds to approximately 75 percent wide-range level, so the narrow-range
narrow-range corresponds to approximately 75 percent wide-range level, so the narrow-range


instruments should have been expected to be reading off scale low. Also, when auxiliary
instruments should have been expected to be reading off scale low. Also, when auxiliary


feedwater actuated, narrow-range level instruments did not show increasing level until after
feedwater actuated, narrow-range level instruments did not show increasing level until after
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In addressing the wide-range instrument question, it was clear that the licensee was not fully
In addressing the wide-range instrument question, it was clear that the licensee was not fully


satisfied that the issue was well-understood. However, rather than clarify the issue
satisfied that the issue was well-understood. However, rather than clarify the issue


immediately, the licensee used a station administrative process that required resolution of the
immediately, the licensee used a station administrative process that required resolution of the
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issue within 30 days, and declared the problem to be an issue needing validation to determine
issue within 30 days, and declared the problem to be an issue needing validation to determine


impact on operability. The NRCs Special Inspection Team concluded that this process was not
impact on operability. The NRCs Special Inspection Team concluded that this process was not


integrated with the stations operability determination process, and could permit an issue that
integrated with the stations operability determination process, and could permit an issue that
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for the uncertainties associated with the differential pressure created by the steam flow past the
for the uncertainties associated with the differential pressure created by the steam flow past the


mid-deck plate in the moisture separator section of the steam generator. A plant power
mid-deck plate in the moisture separator section of the steam generator. A plant power


reduction was commenced at 4:58 p.m. on February 28, 2002, to decrease reactor power to
reduction was commenced at 4:58 p.m. on February 28, 2002, to decrease reactor power to
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differential pressure created by the steam flow past the mid-deck plate in the moisture
differential pressure created by the steam flow past the mid-deck plate in the moisture


separator section of the steam generator. As a conservative measure, after Westinghouse
separator section of the steam generator. As a conservative measure, after Westinghouse


identified this issue via NSAL 02-3, Sequoyah actuated the environmental allowance monitor
identified this issue via NSAL 02-3, Sequoyah actuated the environmental allowance monitor


(EAM) on Friday, February 15, 2002. This feature changed the steam generator low-low level
(EAM) on Friday, February 15, 2002. This feature changed the steam generator low-low level


reactor trip setpoint from 10.7 percent to 15 percent. Since the known steam generator channel
reactor trip setpoint from 10.7 percent to 15 percent. Since the known steam generator channel


uncertainty was 8.3 percent with a narrow-range span uncertainty of 5.3 percent, Sequoyah
uncertainty was 8.3 percent with a narrow-range span uncertainty of 5.3 percent, Sequoyah
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Callaway, Salem, and Sequoyah have since recalibrated the low-low water level setpoints for
Callaway, Salem, and Sequoyah have since recalibrated the low-low water level setpoints for


the steam generator with the additional margin to account for this newly identified error. The
the steam generator with the additional margin to account for this newly identified error. The


licensees completed this instrument recalibration before increasing the plants power level to full
licensees completed this instrument recalibration before increasing the plants power level to full
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The event described in this IN highlights the potential impact of steam generator water level
The event described in this IN highlights the potential impact of steam generator water level


setpoint errors. These errors could delay the expected automatic reactor trip and emergency
setpoint errors. These errors could delay the expected automatic reactor trip and emergency


feedwater actuation. The IN identifies additional accident analyses and systems associated
feedwater actuation. The IN identifies additional accident analyses and systems associated


with the mid-deck plate phenomenon and highlights the importance of a thorough post-trip
with the mid-deck plate phenomenon and highlights the importance of a thorough post-trip


analysis prior to restart. The IN also provides some of the corrective actions taken because of
analysis prior to restart. The IN also provides some of the corrective actions taken because of


this event and provides information sources for further investigation.
this event and provides information sources for further investigation.


IN 2002-10 Sup 1 This information notice does not require any specific action or written response. If you have
IN 2002-10 Sup 1 This information notice does not require any specific action or written response. If you have


any questions about the information in this notice, please contact any of the technical contacts
any questions about the information in this notice, please contact any of the technical contacts
Line 309: Line 311:


/RA/
/RA/
                                      William D. Beckner, Program Director


===William D. Beckner, Program Director===
Operating Reactor Improvements Program
Operating Reactor Improvements Program


Division of Regulatory Improvement Programs
===Division of Regulatory Improvement Programs===
Office of Nuclear Reactor Regulation


Office of Nuclear Reactor Regulation
Technical contacts:


Technical contacts:    Jerry Dozier, NRR             Neil OKeefe, Region IV
===Jerry Dozier, NRR===
Neil OKeefe, Region IV


(301) 415-1014               (361) 972-2507 Email: jxd@nrc.gov            Email: nfo@nrc.gov
(301) 415-1014
(361) 972-2507 Email: jxd@nrc.gov


Hukam Garg, NRR
Email:  nfo@nrc.gov


(301) 415-2929 Email: hcg@nrc.gov
===Hukam Garg, NRR===
(301) 415-2929 Email: hcg@nrc.gov


Attachments:
Attachments:  
1. List of References
1. List of References


2. Overview and Sequence of Events
2. Overview and Sequence of Events


3. List of Recently Issued NRC Information Notices
3. List of Recently Issued NRC Information Notices


IN 2002-10 Sup 1 This information notice does not require any specific action or written response. If you have
IN 2002-10 Sup 1 This information notice does not require any specific action or written response. If you have


any questions about the information in this notice, please contact any of the technical contacts
any questions about the information in this notice, please contact any of the technical contacts
Line 341: Line 347:


/RA/
/RA/
                                      William D. Beckner, Program Director


===William D. Beckner, Program Director===
Operating Reactor Improvements Program
Operating Reactor Improvements Program


Division of Regulatory Improvement Programs
===Division of Regulatory Improvement Programs===
Office of Nuclear Reactor Regulation


Office of Nuclear Reactor Regulation
Technical contacts:


Technical contacts:    Jerry Dozier, NRR             Neil OKeefe, Region IV
===Jerry Dozier, NRR===
Neil OKeefe, Region IV


(301) 415-1014               (361) 972-2507 Email: jxd@nrc.gov            Email: nfo@nrc.gov
(301) 415-1014
(361) 972-2507 Email: jxd@nrc.gov


Hukam Garg, NRR
Email:  nfo@nrc.gov


(301) 415-2929 Email: hcg@nrc.gov
===Hukam Garg, NRR===
(301) 415-2929 Email: hcg@nrc.gov


Attachments:
Attachments:  
1. List of References
1. List of References


2. Overview and Sequence of Events
2. Overview and Sequence of Events


3. List of Recently Issued NRC Information Notices
3. List of Recently Issued NRC Information Notices


DISTRIBUTION:
DISTRIBUTION:
Line 369: Line 379:
IN File
IN File


ADAMS ACCESSION #:                                                     *See previous concurrence
ADAMS ACCESSION #:
*See previous concurrence


DOCUMENT NAME: G:RORP\OES\Dozier\in2002-10s1shortversion.wpd
DOCUMENT NAME: G:RORP\\OES\\Dozier\\in2002-10s1shortversion.wpd


OFFICE RSE:RORP:DRIP TECH EDITOR                     RSE:RIII          RSE:DE:EEIB
OFFICE RSE:RORP:DRIP TECH EDITOR


NAME IJDozier                                        NOKeefe*          HGarg*
RSE:RIII
  DATE      06 /03/2002        06/03/2002              06/03/2002        06/25/2002 OFFICE BC:DE:EEIB            SC:OES:RORP:DRIP PD:RORP:DRIP


NAME JCalvo*                TReis                    WDBeckner
RSE:DE:EEIB


DATE      06/25/2002        06/27/2002              06/28/2002 OFFICIAL RECORD COPY
NAME


Attachment 1 IN 2002-10 Sup 1 REFERENCES
IJDozier
 
NOKeefe*
HGarg*
DATE
 
06 /03/2002
06/03/2002
06/03/2002
06/25/2002 OFFICE BC:DE:EEIB
 
SC:OES:RORP:DRIP
 
PD:RORP:DRIP
 
NAME
 
JCalvo*
TReis
 
WDBeckner
 
DATE
 
06/25/2002
06/27/2002
06/28/2002
 
===OFFICIAL RECORD COPY===
 
===Attachment 1===
IN 2002-10 Sup 1 REFERENCES


LER 1-2002-001-00, Technical Specification Violation Due to Non-Conservative Steam
LER 1-2002-001-00, Technical Specification Violation Due to Non-Conservative Steam
Line 441: Line 482:
2002.
2002.


Attachment 2 IN 2002-10 Sup 1 Overview and Sequence of Events
===Attachment 2===
IN 2002-10 Sup 1 Overview and Sequence of Events


This section discusses applicable events and actions before, during, and following the failure of
This section discusses applicable events and actions before, during, and following the failure of
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In 1989, Diablo Canyon revised the steam generator narrow-range low-low level trip setpoint in
In 1989, Diablo Canyon revised the steam generator narrow-range low-low level trip setpoint in


accordance with License Amendment 34 for Unit 1 and Amendment 33 for Unit 2. The nuclear
accordance with License Amendment 34 for Unit 1 and Amendment 33 for Unit 2. The nuclear


steam supply system (NSSS) vendor (Westinghouse) provided the analysis to reduce the low- low trip setpoint in topical report, WCAP-11784, Calculation of Steam Generator Level Low and
steam supply system (NSSS) vendor (Westinghouse) provided the analysis to reduce the low- low trip setpoint in topical report, WCAP-11784, Calculation of Steam Generator Level Low and


Low-Low Trip Setpoints With Use of a Rosemount 1154 Transmitter. The licensee reduced
Low-Low Trip Setpoints With Use of a Rosemount 1154 Transmitter. The licensee reduced


the setpoint from 15 to 7.2 percent narrow-range on May 10, 1989, for Unit 1, and on April 12,
the setpoint from 15 to 7.2 percent narrow-range on May 10, 1989, for Unit 1, and on April 12,
1989, for Unit 2. However, the licensee did not factor the mid-deck plate differential pressure
1989, for Unit 2. However, the licensee did not factor the mid-deck plate differential pressure


into the narrow-range low-low level trip setpoint at this time because the mid-deck phenomenon
into the narrow-range low-low level trip setpoint at this time because the mid-deck phenomenon
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new (replacement) steam generators using computer modeling tools that were not available
new (replacement) steam generators using computer modeling tools that were not available


during the design review for the original steam generators. Westinghouse began accounting
during the design review for the original steam generators. Westinghouse began accounting


for this bias in the setpoint calculation during design work for replacement steam generators.
for this bias in the setpoint calculation during design work for replacement steam generators.
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Westinghouse began assessing the potential impact of the mid-deck plate for original model
Westinghouse began assessing the potential impact of the mid-deck plate for original model


steam generators in late 1999. Westinghouse was planning to issue Nuclear Safety Advisory
steam generators in late 1999. Westinghouse was planning to issue Nuclear Safety Advisory


Letters about the mid-deck phenomenon at about the time of the Diablo Canyon manual reactor
Letters about the mid-deck phenomenon at about the time of the Diablo Canyon manual reactor
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trip.
trip.


On February 9, 2002, the Main Feed Regulating Valve (MFRV) FW-2-FCV-540 failed closed, stopping the feedwater flow to steam generator 2-4. After a failed attempt to reopen the MFRV,
On February 9, 2002, the Main Feed Regulating Valve (MFRV) FW-2-FCV-540 failed closed, stopping the feedwater flow to steam generator 2-4. After a failed attempt to reopen the MFRV,
operators initiated a manual reactor trip. The cause of the MFRV failure was excess current in
operators initiated a manual reactor trip. The cause of the MFRV failure was excess current in


the coil of an Asco model L206-381-6F solenoid valve (SV), which in turn caused the failure of a
the coil of an Asco model L206-381-6F solenoid valve (SV), which in turn caused the failure of a
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shift supervision expressed skepticism that the steam generator level dropped as low as
shift supervision expressed skepticism that the steam generator level dropped as low as


observed by the steam generator wide-range instrument during the trip. The shift technical
observed by the steam generator wide-range instrument during the trip. The shift technical


advisor confirmed that the wide-range level indication reached 10 percent. Diablo Canyons
advisor confirmed that the wide-range level indication reached 10 percent. Diablo Canyons


Engineering Services reported that steam generator structural integrity was not affected by low
Engineering Services reported that steam generator structural integrity was not affected by low


wide-range level. Engineering Services preliminarily concluded that dynamic processes
wide-range level. Engineering Services preliminarily concluded that dynamic processes


contributed to inaccurate wide-range level indication. Later that night, during a conference call
contributed to inaccurate wide-range level indication. Later that night, during a conference call


with the NRC staff to discuss the licensees plans for the restart of Unit 2, the licensee reviewed
with the NRC staff to discuss the licensees plans for the restart of Unit 2, the licensee reviewed


its corrective actions for the feedwater regulating valve and other failed components. The NRC
its corrective actions for the feedwater regulating valve and other failed components. The NRC


staff expressed concern that wide-range indicated level was abnormally low for this transient.
staff expressed concern that wide-range indicated level was abnormally low for this transient.
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the wide-range level indication was overly conservative but did not impact operator response to
the wide-range level indication was overly conservative but did not impact operator response to


such an indication. The NRC decided to conduct follow up activities on level anomalies. The
such an indication. The NRC decided to conduct follow up activities on level anomalies. The


Plant Staff Review Committee reviewed the results of the trip event response team investigation
Plant Staff Review Committee reviewed the results of the trip event response team investigation


and readiness for restart. The steam generator wide-range water level anomaly issue was
and readiness for restart. The steam generator wide-range water level anomaly issue was


Attachment 2 IN 2002-10 Sup 1 discussed and determined not to be a restart issue. The issue was classified as an issue
===Attachment 2===
IN 2002-10 Sup 1 discussed and determined not to be a restart issue. The issue was classified as an issue


needing validation to determine impact on operability (INVDIO). The Station Director granted
needing validation to determine impact on operability (INVDIO). The Station Director granted


permission to restart the plant.
permission to restart the plant.


Unit 2 was restarted the next day (February 10, 2002). The licensee continued its investigation
Unit 2 was restarted the next day (February 10, 2002). The licensee continued its investigation


of the Unit 2 steam generator response during the transient. Diablo Canyon personnel sent
of the Unit 2 steam generator response during the transient. Diablo Canyon personnel sent


plant trip data to Westinghouse for review. The licensee began to focus on steam generator
plant trip data to Westinghouse for review. The licensee began to focus on steam generator


narrow-range indication as a potential concern. During a conference call between the licensee
narrow-range indication as a potential concern. During a conference call between the licensee


and Westinghouse on February 14, 2002, Westinghouse informed the licensee about a new
and Westinghouse on February 14, 2002, Westinghouse informed the licensee about a new
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process measurement error term related to mid-deck plate differential pressure that had not
process measurement error term related to mid-deck plate differential pressure that had not


been included in the existing setpoint analysis. Operators in both units declared all channels of
been included in the existing setpoint analysis. Operators in both units declared all channels of


narrow-range level instrumentation inoperable and entered Technical Specification 3.0.3.
narrow-range level instrumentation inoperable and entered Technical Specification 3.0.3.


Operations issued a shift order to manually trip the reactor on loss of feedwater flow. Operators
Operations issued a shift order to manually trip the reactor on loss of feedwater flow. Operators


in both units began reducing power to less than 60-percent thermal power to restore the
in both units began reducing power to less than 60-percent thermal power to restore the


narrow-range instruments to an operable condition and exit Technical Specification 3.0.3. On
narrow-range instruments to an operable condition and exit Technical Specification 3.0.3. On


the basis of information received from Westinghouse, the licensee promptly completed an
the basis of information received from Westinghouse, the licensee promptly completed an


operability assessment which concluded that the existing trip setpoint at a 7.2 percent narrow- range level remained operable at or below 60-percent reactor power. Operators stopped power
operability assessment which concluded that the existing trip setpoint at a 7.2 percent narrow- range level remained operable at or below 60-percent reactor power. Operators stopped power


reductions at 60-percent power. This action had to be taken because the failure to correct this
reductions at 60-percent power. This action had to be taken because the failure to correct this


condition prior to restart resulted in Unit 2 changing Modes (Mode 3 to 2 to 1) with the reactor
condition prior to restart resulted in Unit 2 changing Modes (Mode 3 to 2 to 1) with the reactor
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inoperable and subsequent operation of Units 1 and 2 (Mode 1) in a condition prohibited by
inoperable and subsequent operation of Units 1 and 2 (Mode 1) in a condition prohibited by


Technical Specification 3.3.1. This Technical Specification requires that the reactor trip system
Technical Specification 3.3.1. This Technical Specification requires that the reactor trip system


instrumentation for steam generator level low-low be operable for Modes 1 and 2 and the
instrumentation for steam generator level low-low be operable for Modes 1 and 2 and the
Line 569: Line 612:
On February 15, 2002, the licensee implemented setpoint changes on both units to raise the
On February 15, 2002, the licensee implemented setpoint changes on both units to raise the


steam generator low-low setpoint to 15 percent. After implementation, operators increased
steam generator low-low setpoint to 15 percent. After implementation, operators increased


power to 100 percent in both units. Westinghouse issued NSAL 02-3, Steam Generator Mid- Deck Plate Pressure Loss Issue on February 19, 2002. That NSAL warned plants with
power to 100 percent in both units. Westinghouse issued NSAL 02-3, Steam Generator Mid- Deck Plate Pressure Loss Issue on February 19, 2002. That NSAL warned plants with


Westinghouse-designed steam generators that the error source has not been accounted for
Westinghouse-designed steam generators that the error source has not been accounted for
Line 577: Line 620:
and has potentially adverse effects on steam generator level low-low uncertainty calculations as
and has potentially adverse effects on steam generator level low-low uncertainty calculations as


a bias in the indicated high direction. Westinghouse further warned that for plants for which
a bias in the indicated high direction. Westinghouse further warned that for plants for which


Westinghouse maintains the calculation of record, this pressure drop effect may require a
Westinghouse maintains the calculation of record, this pressure drop effect may require a


maximum decrease of approximately 9 percent (in percent narrow-range span) in the safety
maximum decrease of approximately 9 percent (in percent narrow-range span) in the safety


analysis limit (SAL) for establishing the low-low steam generator water level reactor trip for the
analysis limit (SAL) for establishing the low-low steam generator water level reactor trip for the
Line 587: Line 630:
loss of normal feedwater (LONF) transient or the loss of offsite power (LOOP) transient to
loss of normal feedwater (LONF) transient or the loss of offsite power (LOOP) transient to


compensate for this bias. NSAL 02-3 added additional transients to consider, such as the
compensate for this bias. NSAL 02-3 added additional transients to consider, such as the


steamline break mass and energy release, and for plants with feed line check valves inside
steamline break mass and energy release, and for plants with feed line check valves inside


containment, the feedline break transient, to compensate for this described bias. Revision 1 to
containment, the feedline break transient, to compensate for this described bias. Revision 1 to


the NSAL 02-3 also provided updated information regarding the steam generator water level
the NSAL 02-3 also provided updated information regarding the steam generator water level


mid-deck plate pressure loss issue. Specifically, Westinghouse revised the NSAL to address
mid-deck plate pressure loss issue. Specifically, Westinghouse revised the NSAL to address


the impact of this issue on the feedwater line break analysis (when feedwater check valves
the impact of this issue on the feedwater line break analysis (when feedwater check valves
Line 601: Line 644:
were located inside containment), the ATWS mitigation system actuation circuitry system, and
were located inside containment), the ATWS mitigation system actuation circuitry system, and


steamline break mass and energy release calculations. Westinghouse subsequently issued
steamline break mass and energy release calculations. Westinghouse subsequently issued


NSAL 02-4, Maximum Reliable Indicated Steam Generator Water Level, and NSAL 02-5, Steam Generator Water Level Control System Uncertainty Issue on February 19, 2002.
NSAL 02-4, Maximum Reliable Indicated Steam Generator Water Level, and NSAL 02-5, Steam Generator Water Level Control System Uncertainty Issue on February 19, 2002.
Line 607: Line 650:
Revision 1 to NSAL 02-5 was written to clarify the need to calculate the steam generator water
Revision 1 to NSAL 02-5 was written to clarify the need to calculate the steam generator water


Attachment 2 IN 2002-10 Sup 1 level uncertainties at normal operating level, including the impact, if any, of the mid-deck plate
===Attachment 2===
IN 2002-10 Sup 1 level uncertainties at normal operating level, including the impact, if any, of the mid-deck plate


pressure differential and to compare the uncertainties used in the initial condition of the safety
pressure differential and to compare the uncertainties used in the initial condition of the safety


analyses to determine if they remain bounding. NSAL 02-5, Rev. 1, also discusses the
analyses to determine if they remain bounding. NSAL 02-5, Rev. 1, also discusses the


potential impact on safety analyses performed at reactor power levels other than 100 percent
potential impact on safety analyses performed at reactor power levels other than 100 percent
Line 621: Line 665:
Advisory Letter 02-3 and the void content of the two phase mixture above the mid-deck plate
Advisory Letter 02-3 and the void content of the two phase mixture above the mid-deck plate


(NSAL 02-4). Westinghouse also held a workshop with industry representatives on
(NSAL 02-4). Westinghouse also held a workshop with industry representatives on


February 28, 2002 and a public meeting with the NRC staff on March 20, 2002.
February 28, 2002 and a public meeting with the NRC staff on March 20, 2002.
Line 631: Line 675:
generator narrow-range low-low level protection setpoints.
generator narrow-range low-low level protection setpoints.


Attachment 3 IN 2002-10 Sup 1 LIST OF RECENTLY ISSUED
______________________________________________________________________________________
OL = Operating License


NRC INFORMATION NOTICES
CP = Construction Permit


===Attachment 3===
IN 2002-10 Sup 1 LIST OF RECENTLY ISSUED
===NRC INFORMATION NOTICES===
_____________________________________________________________________________________
_____________________________________________________________________________________
Information                                             Date of
Information


Notice No.             Subject                         Issuance       Issued to
Date of
 
Notice No.
 
Subject
 
Issuance
 
Issued to


_____________________________________________________________________________________
_____________________________________________________________________________________
2002-22           Degraded Bearing Surfaces in         06/28/2002      All holders of operating licenses
2002-22
 
===Degraded Bearing Surfaces in===
GM/EMD Emergency Diesel
 
Generators


GM/EMD Emergency Diesel                                for pressurized- or boiling-water
06/28/2002


Generators                                            nuclear power reactors, including
===All holders of operating licenses===
for pressurized- or boiling-water
 
nuclear power reactors, including


those that have ceased
those that have ceased
Line 651: Line 716:
operations but have fuel on site.
operations but have fuel on site.


2002-21           Axial Outside-Diameter               06/25/2002      All holders of operating licenses
2002-21 Axial Outside-Diameter


Cracking Affecting Thermally                           for pressurized-water reactors
===Cracking Affecting Thermally===
Treated Alloy 600 Steam


Treated Alloy 600 Steam                                (PWRs), except those who have
===Generator Tubing===
06/25/2002


Generator Tubing                                      permanently ceased operations
===All holders of operating licenses===
for pressurized-water reactors
 
(PWRs), except those who have
 
permanently ceased operations


and have certified that fuel has
and have certified that fuel has
Line 665: Line 737:
the reactor.
the reactor.


2002-19           Medical Misadministrations           06/14/2002      All nuclear pharmacies and
2002-19
 
===Medical Misadministrations===
Caused By Failure to Properly
 
===Perform Tests on Dose===
Calibrators for Beta-and Low- Energy Photon-Emitting


Caused By Failure to Properly                          medical licensees.
===Radionuclides===
06/14/2002


Perform Tests on Dose
===All nuclear pharmacies and===
medical licensees.


Calibrators for Beta-and Low- Energy Photon-Emitting
2002-18
 
===Effect of Adding Gas Into===
Water Storage Tanks on the


Radionuclides
===Net Positive Suction Head For===
Pumps


2002-18          Effect of Adding Gas Into            06/06/2002       All holders of operating licenses
06/06/2002


Water Storage Tanks on the                            for nuclear power reactors, Net Positive Suction Head For                          except those who have
===All holders of operating licenses===
for nuclear power reactors, except those who have


Pumps                                                  permanently ceased operations
permanently ceased operations


and have certified that fuel has
and have certified that fuel has
Line 687: Line 772:
the reactor.
the reactor.


2002-17           Medical Use of Strontium-90           05/30/2002       All U.S. Nuclear Regulatory
2002-17 Medical Use of Strontium-90
Eye Applicators: New
 
===Requirements for Calibration===
and Decay Correction
 
05/30/2002


Eye Applicators: New                                  Commission medical licensees
===All U.S. Nuclear Regulatory===
Commission medical licensees


Requirements for Calibration                          that use strontium-90 (Sr-90) eye
that use strontium-90 (Sr-90) eye


and Decay Correction                                  applicators.
applicators.


Note:           NRC generic communications may be received in electronic format shortly after they are
Note:
NRC generic communications may be received in electronic format shortly after they are


issued by subscribing to the NRC listserver as follows:
issued by subscribing to the NRC listserver as follows:
                To subscribe send an e-mail to <listproc@nrc.gov >, no subject, and the following
To subscribe send an e-mail to <listproc@nrc.gov >, no subject, and the following


command in the message portion:
command in the message portion:
                                    subscribe gc-nrr firstname lastname
subscribe gc-nrr firstname lastname}}
 
______________________________________________________________________________________
OL = Operating License
 
CP = Construction Permit}}


{{Information notice-Nav}}
{{Information notice-Nav}}

Latest revision as of 17:51, 16 January 2025

Manual Reactor Trip and Steam Generator Water Level Setpoint Uncertainties
ML021820008
Person / Time
Site: Diablo Canyon 
Issue date: 06/28/2002
From: Beckner W
NRC/NRR/DRIP/RORP
To:
Dozier J, NRR/RLSB 415-1014
References
TAC M4812 IN-02-010, Suppl 1
Download: ML021820008 (15)


UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, DC 20555-0001

June 28, 2002

NRC INFORMATION NOTICE 2002-10, SUPPLEMENT 1:

DIABLO CANYON MANUAL

REACTOR TRIP AND STEAM

GENERATOR WATER LEVEL

SETPOINT UNCERTAINTIES

ADDRESSEES

All holders of operating licenses for nuclear power reactors, except those who have

permanently ceased operations and have certified that fuel has been permanently removed

from the reactor.

PURPOSE

The U.S. Nuclear Regulatory Commission (NRC) is issuing this supplement to give addressees

further information about the manual reactor trip of Diablo Canyon Unit 2 which resulted from a

failure of the main feedwater regulating valve, non-conservative steam generator setpoints and

contributing causes, and other licensee actions relating to these events. This supplement

provides information that became available after the issuance of the original information notice

(IN). The NRC expects that recipients will review the information for applicability to their

facilities and consider taking actions, as appropriate. However, this supplement does not

contain any NRC requirements and does not require any specific action or written response.

BACKGROUND

Diablo Canyon Nuclear Power Plant reported a manual reactor trip of Unit 2 which resulted from

a loss of main feedwater to a steam generator (LER 2-2002-002-00) and that the narrow-range

steam generator water level instrumentation did not respond as expected to initiate an

automatic reactor trip and emergency feedwater actuation on low-low water level in the steam

generator (LER 1-2002-001-00). The NRC issued IN 2002-10 on March 7, 2002, to inform

licensees of this event. Following the issuance of the original IN, the NRC staff conducted a

Special Inspection at Diablo Canyon, as well as a public meeting with Westinghouse. In

addition, Diablo Canyon has completed its Licensee Event Reports (LERs), Westinghouse has

issued five Nuclear Safety Advisory Letters (NSALs) relating to this phenomenon or the

presence of the void content of the two phase mixture above the mid-deck plate, and other

facilities have generated reports under Title 10, Section 50.72, of the Code of Federal

Regulations (10 CFR 50.72).

DESCRIPTION OF CIRCUMSTANCES

On February 9, 2002, with Unit 2 at full power, main feedwater regulating valve

(MFRV) FW-2-FCV-540 failed in the closed position, resulting in a rapid decrease in the water

ML021820008

IN 2002-10 Sup 1 level of Steam Generator 2-4. The indicated narrow-range water level decreased to 7.5 percent

and leveled out. Operators tripped the Unit 2 reactor within approximately 1 minute after the

main feedwater regulating valve closed. On February 14, 2002, after the Unit 2 restart but while

still investigating the event, the licensee identified a potentially unanalyzed condition involving

the narrow-range steam generator water level instrumentation. The licensee determined that

during the plant transient, the actual water level in steam generator 2-4 fell below the 7.2- percent narrow-range trip setpoint for engineered safety feature and reactor trip actuations

before operators manually tripped the reactor. The steam generator vendor attributed this

water-level discrepancy to a previously unaccounted for differential pressure created by steam

flow past the mid-deck plate in the moisture separator section of the steam generator. This

differential pressure phenomenon caused the steam generator narrow-range instruments to

indicate a higher-than-actual water level. Thus, the steam generator narrow-range water level

low-low setpoint was non-conservative during the loss of normal feedwater transient.

Physical Phenomenon and System Description

Steam generators designed by Westinghouse incorporate two-stage moisture separation. The

first stage uses centrifugal separators, and the second stage uses chevron-type separators. A

mid-deck divider plate separates the two stages. The steam generator water level

instrumentation uses differential pressure instruments with two ranges, a wide-range non- safety-related instrument and three or four (depending on plant) narrow-range safety-related

instruments. The wide-range instrument spans essentially the entire length of the downcomer

region, while the narrow-range instruments span only the upper 25 percent of the wide-range to

cover the normal operating band. The upper taps for all four instruments are located above the

mid-deck plate, while the lower taps are all located below this plate.

In the event at Diablo Canyon, the holes in the mid-deck, which were designed to allow

moisture removed from the second-stage separators to flow back into the downcomers, acted

as orifices which restricted steam flow and allowed pressure differences with water levels

below the mid-deck region. At higher steam flow rates with a decreasing steam generator

water level, steam exiting the first stage separators along with the moisture being separated

was enough to build up pressure below the plate that was not acting above the plate. Since the

upper steam generator water level instrument taps were connected above the plate, a pressure

difference acted on the four instruments and provided a bias that caused the instruments to

indicate a higher-than-actual level. For the limiting safety setting of the low-low steam

generator water level setpoint, this bias acts in the non-conservative direction. The magnitude

of the bias drops as the steam flow decreases.

Post Trip Analysis

Following this event, the NRC completed an onsite special team inspection at Diablo Canyon

Nuclear Power Plant. The inspection examined the events surrounding the Unit 2 reactor trip

on February 9, 2002, as they relate to safety and compliance with the Commissions rules and

regulations and the conditions of the Diablo Canyon license. The inspection consisted of

examining procedures and records, and interviewing station personnel and staff members, as

well as the reactor plant contractor. The NRCs Special Inspection Team also developed a

detailed sequence of events and organizational response time line which is summarized in the

Overview and Sequence of Events Attachment 2 to this IN.

IN 2002-10 Sup 1 This event provided an unusual challenge to the licensee in that it involved an unrecognized

phenomenon. Many plant events involve equipment behaving in an unexpected manner, but

the failure mechanisms are usually well-understood. However, a well-structured corrective

action process should still be effective under these circumstances by being sufficiently rigorous

to recognize conditions that are adverse to quality and then treating them according to their

safety significance. From a review of the post trip review, the NRCs Special Inspection Team

concluded that the licensees process was narrowly focused on finding, understanding, and

correcting the cause of the trip. While the stations post-trip analysis procedure contained steps

to review plant behavior before, during, and after the event, this was effectively not performed.

The cause of the event was readily apparent without the need to analyze plant parameters.

However, by not performing a methodical review of the plants behavior and comparing it to the

behavior expected under those conditions, the licensee failed to recognize that an automatic

plant trip and ESF actuation of auxiliary feedwater did not occur when required. Had this been

recognized, the licensee would probably have delayed restarting the plant until after the cause

and implications were understood.

The licensees review of the anomalous steam generator water level attempted to explain why

wide-range indication did not track with narrow-range indication, which was thought to have

indicated accurately. The NRCs Special Inspection Team concluded that the licensees theory

and supporting data were not compared with other available but conflicting indications. The

licensee calculated that the event would have resulted in loss of approximately 75 percent of

the initial water mass in the affected steam generator, and should have caused the wide-range

level to be 20 percent of the actual level. The licensee did not note that the bottom of the

narrow-range corresponds to approximately 75 percent wide-range level, so the narrow-range

instruments should have been expected to be reading off scale low. Also, when auxiliary

feedwater actuated, narrow-range level instruments did not show increasing level until after

some delay, confirming that actual level was well below the narrow-range.

In addressing the wide-range instrument question, it was clear that the licensee was not fully

satisfied that the issue was well-understood. However, rather than clarify the issue

immediately, the licensee used a station administrative process that required resolution of the

issue within 30 days, and declared the problem to be an issue needing validation to determine

impact on operability. The NRCs Special Inspection Team concluded that this process was not

integrated with the stations operability determination process, and could permit an issue that

was thought to relate to an operability question to be studied for 30 days before addressing the

operability question. Although this issue was resolved in 4 days, this approach was considered

to be contrary to Generic Letter 91-18, which provided guidance on the need to perform prompt

operability assessments.

The following paragraphs present examples of corrective actions from other licensees:

Callaway

Callaway reported (EN 38740) that based on an assessment of its steam generator narrow- range low-low level trip setpoints, the existing low-low level trip at 14.8 percent did not account

for the uncertainties associated with the differential pressure created by the steam flow past the

mid-deck plate in the moisture separator section of the steam generator. A plant power

reduction was commenced at 4:58 p.m. on February 28, 2002, to decrease reactor power to

below 30 percent where engineering calculations indicate that the steam generator mid-deck

plate differential pressure condition will no longer result in a non-conservative setpoint.

IN 2002-10 Sup 1 Salem

Similar to Callaway, the low-low level trip at 9 percent did not account for the uncertainties and

Salem reduced power to 38 percent.

Sequoyah

Sequoyah personnel also performed an assessment and determined that the existing 10.7 percent low-low level trip setpoint did not account for the uncertainties associated with the

differential pressure created by the steam flow past the mid-deck plate in the moisture

separator section of the steam generator. As a conservative measure, after Westinghouse

identified this issue via NSAL 02-3, Sequoyah actuated the environmental allowance monitor

(EAM) on Friday, February 15, 2002. This feature changed the steam generator low-low level

reactor trip setpoint from 10.7 percent to 15 percent. Since the known steam generator channel

uncertainty was 8.3 percent with a narrow-range span uncertainty of 5.3 percent, Sequoyah

determined that operating with the EAMs continuously actuated would allow continued

operation.

Callaway, Salem, and Sequoyah have since recalibrated the low-low water level setpoints for

the steam generator with the additional margin to account for this newly identified error. The

licensees completed this instrument recalibration before increasing the plants power level to full

reactor power.

Conclusion

The event described in this IN highlights the potential impact of steam generator water level

setpoint errors. These errors could delay the expected automatic reactor trip and emergency

feedwater actuation. The IN identifies additional accident analyses and systems associated

with the mid-deck plate phenomenon and highlights the importance of a thorough post-trip

analysis prior to restart. The IN also provides some of the corrective actions taken because of

this event and provides information sources for further investigation.

IN 2002-10 Sup 1 This information notice does not require any specific action or written response. If you have

any questions about the information in this notice, please contact any of the technical contacts

listed below or the appropriate project manager from the NRCs Office of Nuclear Reactor

Regulation (NRR).

/RA/

William D. Beckner, Program Director

Operating Reactor Improvements Program

Division of Regulatory Improvement Programs

Office of Nuclear Reactor Regulation

Technical contacts:

Jerry Dozier, NRR

Neil OKeefe, Region IV

(301) 415-1014

(361) 972-2507 Email: jxd@nrc.gov

Email: nfo@nrc.gov

Hukam Garg, NRR

(301) 415-2929 Email: hcg@nrc.gov

Attachments:

1. List of References

2. Overview and Sequence of Events

3. List of Recently Issued NRC Information Notices

IN 2002-10 Sup 1 This information notice does not require any specific action or written response. If you have

any questions about the information in this notice, please contact any of the technical contacts

listed below or the appropriate project manager from the NRCs Office of Nuclear Reactor

Regulation (NRR).

/RA/

William D. Beckner, Program Director

Operating Reactor Improvements Program

Division of Regulatory Improvement Programs

Office of Nuclear Reactor Regulation

Technical contacts:

Jerry Dozier, NRR

Neil OKeefe, Region IV

(301) 415-1014

(361) 972-2507 Email: jxd@nrc.gov

Email: nfo@nrc.gov

Hukam Garg, NRR

(301) 415-2929 Email: hcg@nrc.gov

Attachments:

1. List of References

2. Overview and Sequence of Events

3. List of Recently Issued NRC Information Notices

DISTRIBUTION:

ADAMS

IN File

ADAMS ACCESSION #:

  • See previous concurrence

DOCUMENT NAME: G:RORP\\OES\\Dozier\\in2002-10s1shortversion.wpd

OFFICE RSE:RORP:DRIP TECH EDITOR

RSE:RIII

RSE:DE:EEIB

NAME

IJDozier

NOKeefe*

HGarg*

DATE

06 /03/2002

06/03/2002

06/03/2002

06/25/2002 OFFICE BC:DE:EEIB

SC:OES:RORP:DRIP

PD:RORP:DRIP

NAME

JCalvo*

TReis

WDBeckner

DATE

06/25/2002

06/27/2002

06/28/2002

OFFICIAL RECORD COPY

Attachment 1

IN 2002-10 Sup 1 REFERENCES

LER 1-2002-001-00, Technical Specification Violation Due to Non-Conservative Steam

Generator Narrow-Range Water Level Instrumentation, Diablo Canyon Nuclear Power Plant, April 15, 2002.

LER 2-2002-002-00, Unit 2 Manual Reactor Trip Due to Loss of Main Feedwater to a Steam

Generator, Diablo Canyon Nuclear Power Plant, April 10, 2002.

NRC Special Team Inspection Reports 50-275/02-07 and 50-323/02-07 for Diablo Canyon

Nuclear Power Plant, April 8, 2002.

NRC Information Notice 2002-10, Non-Conservative Water Level Setpoints on Steam

Generators, March 7, 2002.

Westinghouse Nuclear Safety Advisory Letter NSAL-02-3, Steam Generator Mid-Deck Plate

Pressure Loss Issue, February 15, 2002.

Westinghouse Nuclear Safety Advisory Letter NSAL-02-3, Rev. 1, Steam Generator Mid-Deck

Plate Pressure Loss Issue, April 8, 2002.

Westinghouse Nuclear Safety Advisory Letter NSAL-02-4, Maximum Reliable Indicated Steam

Generator Water Level, February 19, 2002.

Westinghouse Nuclear Safety Advisory Letter NSAL-02-5, Steam Generator Water Level

Control Uncertainty Issue, February 19, 2002.

Westinghouse Steam Generator Water Level Uncertainty Issues Handout from NRC Public

Meeting in Rockville, Maryland, March 20, 2002.

Event Report 38697, Technical Specification Required Shutdown of Both Units Because

Steam Generator Water Level Instrument Channels are Inoperable Due to a Non-Conservative

Water Level Low-Low Setpoint, Diablo Canyon Nuclear Power Plant, February 14, 2002.

Event Report 38713, Safe Shutdown Capability Impacted by Non-Conservative SG NR

Setpoint, Sequoyah Nuclear Power Plant, February 20, 2002.

Event Report 38740, Safe Shutdown Capability Impacted by Non-Conservative SG NR

Setpoint, Callaway Nuclear Power Plant, February 28, 2002.

Event Report 38702, Discovery of a Non-Conservative Low-Low Level Trip Setpoint Due to a

Differential Pressure Phenomenon that Causes Steam Generator Narrow-Range Level

Channels to Read Higher Than Actual Water Level at High Steam Flows, Salem, February 15,

2002.

Attachment 2

IN 2002-10 Sup 1 Overview and Sequence of Events

This section discusses applicable events and actions before, during, and following the failure of

steam generator feedwater regulating valve number 4.

In 1989, Diablo Canyon revised the steam generator narrow-range low-low level trip setpoint in

accordance with License Amendment 34 for Unit 1 and Amendment 33 for Unit 2. The nuclear

steam supply system (NSSS) vendor (Westinghouse) provided the analysis to reduce the low- low trip setpoint in topical report, WCAP-11784, Calculation of Steam Generator Level Low and

Low-Low Trip Setpoints With Use of a Rosemount 1154 Transmitter. The licensee reduced

the setpoint from 15 to 7.2 percent narrow-range on May 10, 1989, for Unit 1, and on April 12,

1989, for Unit 2. However, the licensee did not factor the mid-deck plate differential pressure

into the narrow-range low-low level trip setpoint at this time because the mid-deck phenomenon

was unknown.

In 1998, Westinghouse recognized the mid-deck phenomenon while evaluating the design of

new (replacement) steam generators using computer modeling tools that were not available

during the design review for the original steam generators. Westinghouse began accounting

for this bias in the setpoint calculation during design work for replacement steam generators.

Westinghouse began assessing the potential impact of the mid-deck plate for original model

steam generators in late 1999. Westinghouse was planning to issue Nuclear Safety Advisory

Letters about the mid-deck phenomenon at about the time of the Diablo Canyon manual reactor

trip.

On February 9, 2002, the Main Feed Regulating Valve (MFRV) FW-2-FCV-540 failed closed, stopping the feedwater flow to steam generator 2-4. After a failed attempt to reopen the MFRV,

operators initiated a manual reactor trip. The cause of the MFRV failure was excess current in

the coil of an Asco model L206-381-6F solenoid valve (SV), which in turn caused the failure of a

power fuse and forced the MFRV to close.

During discussions with the resident inspectors after the event, the operations manager and

shift supervision expressed skepticism that the steam generator level dropped as low as

observed by the steam generator wide-range instrument during the trip. The shift technical

advisor confirmed that the wide-range level indication reached 10 percent. Diablo Canyons

Engineering Services reported that steam generator structural integrity was not affected by low

wide-range level. Engineering Services preliminarily concluded that dynamic processes

contributed to inaccurate wide-range level indication. Later that night, during a conference call

with the NRC staff to discuss the licensees plans for the restart of Unit 2, the licensee reviewed

its corrective actions for the feedwater regulating valve and other failed components. The NRC

staff expressed concern that wide-range indicated level was abnormally low for this transient.

The licensee explained its theory that the actual level was higher because of the difference

between the transient conditions (hot, dynamic) and the calibration conditions (cold, static).

The licensee believed that the steam generator narrow-range level response was normal, and

the wide-range level indication was overly conservative but did not impact operator response to

such an indication. The NRC decided to conduct follow up activities on level anomalies. The

Plant Staff Review Committee reviewed the results of the trip event response team investigation

and readiness for restart. The steam generator wide-range water level anomaly issue was

Attachment 2

IN 2002-10 Sup 1 discussed and determined not to be a restart issue. The issue was classified as an issue

needing validation to determine impact on operability (INVDIO). The Station Director granted

permission to restart the plant.

Unit 2 was restarted the next day (February 10, 2002). The licensee continued its investigation

of the Unit 2 steam generator response during the transient. Diablo Canyon personnel sent

plant trip data to Westinghouse for review. The licensee began to focus on steam generator

narrow-range indication as a potential concern. During a conference call between the licensee

and Westinghouse on February 14, 2002, Westinghouse informed the licensee about a new

process measurement error term related to mid-deck plate differential pressure that had not

been included in the existing setpoint analysis. Operators in both units declared all channels of

narrow-range level instrumentation inoperable and entered Technical Specification 3.0.3.

Operations issued a shift order to manually trip the reactor on loss of feedwater flow. Operators

in both units began reducing power to less than 60-percent thermal power to restore the

narrow-range instruments to an operable condition and exit Technical Specification 3.0.3. On

the basis of information received from Westinghouse, the licensee promptly completed an

operability assessment which concluded that the existing trip setpoint at a 7.2 percent narrow- range level remained operable at or below 60-percent reactor power. Operators stopped power

reductions at 60-percent power. This action had to be taken because the failure to correct this

condition prior to restart resulted in Unit 2 changing Modes (Mode 3 to 2 to 1) with the reactor

trip system and engineered safety system steam generator water level low-low instrumentation

inoperable and subsequent operation of Units 1 and 2 (Mode 1) in a condition prohibited by

Technical Specification 3.3.1. This Technical Specification requires that the reactor trip system

instrumentation for steam generator level low-low be operable for Modes 1 and 2 and the

engineered safety feature actuation instrumentation steam generator water level-low-low be

operable in Modes 1, 2, and 3.

On February 15, 2002, the licensee implemented setpoint changes on both units to raise the

steam generator low-low setpoint to 15 percent. After implementation, operators increased

power to 100 percent in both units. Westinghouse issued NSAL 02-3, Steam Generator Mid- Deck Plate Pressure Loss Issue on February 19, 2002. That NSAL warned plants with

Westinghouse-designed steam generators that the error source has not been accounted for

and has potentially adverse effects on steam generator level low-low uncertainty calculations as

a bias in the indicated high direction. Westinghouse further warned that for plants for which

Westinghouse maintains the calculation of record, this pressure drop effect may require a

maximum decrease of approximately 9 percent (in percent narrow-range span) in the safety

analysis limit (SAL) for establishing the low-low steam generator water level reactor trip for the

loss of normal feedwater (LONF) transient or the loss of offsite power (LOOP) transient to

compensate for this bias. NSAL 02-3 added additional transients to consider, such as the

steamline break mass and energy release, and for plants with feed line check valves inside

containment, the feedline break transient, to compensate for this described bias. Revision 1 to

the NSAL 02-3 also provided updated information regarding the steam generator water level

mid-deck plate pressure loss issue. Specifically, Westinghouse revised the NSAL to address

the impact of this issue on the feedwater line break analysis (when feedwater check valves

were located inside containment), the ATWS mitigation system actuation circuitry system, and

steamline break mass and energy release calculations. Westinghouse subsequently issued

NSAL 02-4, Maximum Reliable Indicated Steam Generator Water Level, and NSAL 02-5, Steam Generator Water Level Control System Uncertainty Issue on February 19, 2002.

Revision 1 to NSAL 02-5 was written to clarify the need to calculate the steam generator water

Attachment 2

IN 2002-10 Sup 1 level uncertainties at normal operating level, including the impact, if any, of the mid-deck plate

pressure differential and to compare the uncertainties used in the initial condition of the safety

analyses to determine if they remain bounding. NSAL 02-5, Rev. 1, also discusses the

potential impact on safety analyses performed at reactor power levels other than 100 percent

and the impact of steam generator water level uncertainty on LOCA mass and energy release.

These letters covered other effects of the same physical phenomenon as Nuclear Safety

Advisory Letter 02-3 and the void content of the two phase mixture above the mid-deck plate

(NSAL 02-4). Westinghouse also held a workshop with industry representatives on

February 28, 2002 and a public meeting with the NRC staff on March 20, 2002.

In its LER, Diablo Canyon indicated that it will submit a license amendment request to revise

the Technical Specifications to account for the mid-deck plate differential pressure in the steam

generator narrow-range low-low level protection setpoints.

______________________________________________________________________________________

OL = Operating License

CP = Construction Permit

Attachment 3

IN 2002-10 Sup 1 LIST OF RECENTLY ISSUED

NRC INFORMATION NOTICES

_____________________________________________________________________________________

Information

Date of

Notice No.

Subject

Issuance

Issued to

_____________________________________________________________________________________

2002-22

Degraded Bearing Surfaces in

GM/EMD Emergency Diesel

Generators

06/28/2002

All holders of operating licenses

for pressurized- or boiling-water

nuclear power reactors, including

those that have ceased

operations but have fuel on site.

2002-21 Axial Outside-Diameter

Cracking Affecting Thermally

Treated Alloy 600 Steam

Generator Tubing

06/25/2002

All holders of operating licenses

for pressurized-water reactors

(PWRs), except those who have

permanently ceased operations

and have certified that fuel has

been permanently removed from

the reactor.

2002-19

Medical Misadministrations

Caused By Failure to Properly

Perform Tests on Dose

Calibrators for Beta-and Low- Energy Photon-Emitting

Radionuclides

06/14/2002

All nuclear pharmacies and

medical licensees.

2002-18

Effect of Adding Gas Into

Water Storage Tanks on the

Net Positive Suction Head For

Pumps

06/06/2002

All holders of operating licenses

for nuclear power reactors, except those who have

permanently ceased operations

and have certified that fuel has

been permanently removed from

the reactor.

2002-17 Medical Use of Strontium-90

Eye Applicators: New

Requirements for Calibration

and Decay Correction

05/30/2002

All U.S. Nuclear Regulatory

Commission medical licensees

that use strontium-90 (Sr-90) eye

applicators.

Note:

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