ENS 47874: Difference between revisions

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| event date = 04/30/2012 10:18 EDT
| event date = 04/30/2012 10:18 EDT
| last update date = 04/30/2012
| last update date = 04/30/2012
| title = Unusual Event Due To A Potential Fire In Containment
| title = Unusual Event Due to a Potential Fire in Containment
| event text = Performing an I&C functional [test] caused an inadvertent Safety Injection signal resulting in a reactor trip/safety injection.  All safety systems responded as designed for a safety injection.  Electrical systems are aligned to normal offsite power sources.  All fire alarms have been validated by the Fire Protection Department as invalid alarms and confirmed that no fire event in the protected area.
| event text = Performing an I&C functional [test] caused an inadvertent Safety Injection signal resulting in a reactor trip/safety injection.  All safety systems responded as designed for a safety injection.  Electrical systems are aligned to normal offsite power sources.  All fire alarms have been validated by the Fire Protection Department as invalid alarms and confirmed that no fire event in the protected area.
The reactor trip was successful and all rods [fully] inserted.  Decay heat removal is via auxiliary feedwater through the atmospheric [steam] dumps.  Unknown at this time is the cause of the inadvertent safety injection signal.  No injuries occurred as a result of this event.
The reactor trip was successful and all rods [fully] inserted.  Decay heat removal is via auxiliary feedwater through the atmospheric [steam] dumps.  Unknown at this time is the cause of the inadvertent safety injection signal.  No injuries occurred as a result of this event.

Latest revision as of 21:04, 1 March 2018

ENS 47874 +/-
Where
Salem PSEG icon.png
New Jersey (NRC Region 1)
Reporting
Emergency class: Unusual Event
10 CFR 50.72(a) (1) (i), Emergency Class Declaration

10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge

10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Time - Person (Reporting Time:+-3.55 h-0.148 days <br />-0.0211 weeks <br />-0.00486 months <br />)
Opened: Scott Riddell
10:45 Apr 30, 2012
NRC Officer: Charles Teal
Last Updated: Apr 30, 2012
47874 - NRC Website
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