ENS 40787
ENS Event | |
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16:30 Jun 2, 2004 | |
Title | Plant Shutdown Was Initiated to Comply with Tech Spec. 3.6.1.1. Primary Containment Integrity. |
Event Description | At 1230 hours0.0142 days <br />0.342 hours <br />0.00203 weeks <br />4.68015e-4 months <br /> the service water isolation valve to the Turbine Building Area (1SW26) was declared inoperable due to the inability to close the valve. This condition was identified while investigating a low service water pressure in the turbine building during start up activities from the Salem 1 sixteenth refueling outage.
With 1SW26 inoperable, Technical Specification 3.6.1.1 requires that the inoperable valve be restored to operable within one hour or be in hot standby within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in cold shutdown in the next 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />. Since the valve cannot be restored to operable within the one hour action statement time, PSEG commenced a unit shutdown at 1330 hours0.0154 days <br />0.369 hours <br />0.0022 weeks <br />5.06065e-4 months <br />. It is expected that repairs can be performed while in hot standby conditions. This report complies with the reporting requirements of 10 CFR 50.72 (b)(2)(i). The NRC Resident Inspector was notified of this event by the licensee. |
Where | |
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Salem New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-1.33 h-0.0554 days <br />-0.00792 weeks <br />-0.00182 months <br />) | |
Opened: | Marty Malony 15:10 Jun 2, 2004 |
NRC Officer: | John Mackinnon |
Last Updated: | Jun 2, 2004 |
40787 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (19 %) |
After | Power Operation (9 %) |
WEEKMONTHYEARENS 525812017-02-28T15:00:00028 February 2017 15:00:00
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