ENS 51563
ENS Event | |
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02:48 Nov 24, 2015 | |
Title | Unusual Event Declared Due to Reactor Coolant System Leakage |
Event Description | At 2148 EST on November 23, 2015, Salem Unit 2 declared an Unusual Event due to reactor coolant system leakage greater than 10 gallons per minute. While performing troubleshooting to determine the source of leakage from the Emergency Core Cooling System high head safety injection piping, a motor operated valve was opened and the high head piping relief valve lifted. Indications in the control room calculated the leak rate at 16 gallons per minute based on the change in Pressurizer level. The leak was terminated when the motor operated valve was closed and the relief valve reseated. The time [duration] of the leak was about one minute."
The licensee notified the NRC Resident Inspector. Notified DHS SWO, FEMA Ops Center, and NICC Watch Officer. E-mailed FEMA NWC and Nuclear SSA.
The licensee terminated the Unusual Event at 0100 EST on 11/24/15. The licensee will be cooling down and depressurizing to mode 5 in order to replace the affected valve. The licensee will be notifying the NRC Resident Inspector as well as the New Jersey State police, Delaware State Police and local emergency dispatch. Notified the R1DO (Dwyer), NRR EO (Morris), IRD MOC (Stapleton), DHS SWO, FEMA Ops enter, and NICC Watch Officer. E-mailed FEMA NWC and Nuclear SSA.
This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D). 'Any event of condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident,' due to inoperability of both trains of the Emergency Core Cooling System high head safety injection systems. The unusual event was exited at 0100 [EST] on November 24th, 2015, when the Emergency Core Cooling System high head safety injection piping inlet valves were closed, ensuring isolation of the relief valve. The criteria for exit was leakage rate was below the 10 GPM rate. The plant is in mode 3 cooling down to mode 5. The licensee notified the states of New Jersey and Delaware, Lower Alloways Township, and the NRC Resident Inspector. Notified the R1DO (Dwyer). |
Where | |
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Salem New Jersey (NRC Region 1) | |
Reporting | |
Emergency class: | Unusual Event |
10 CFR 50.72(a) (1) (i), Emergency Class Declaration 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
LER: | 05000311/LER-2015-003 |
Time - Person (Reporting Time:+-4.12 h-0.172 days <br />-0.0245 weeks <br />-0.00564 months <br />) | |
Opened: | John Osborne 22:41 Nov 23, 2015 |
NRC Officer: | Donald Norwood |
Last Updated: | Nov 24, 2015 |
51563 - NRC Website
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Unit 2 | |
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Reactor critical | Not Critical |
Scram | No |
Before | Hot Standby (0 %) |
After | Hot Standby (0 %) |