ENS 41670
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ENS Event | |
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03:05 May 6, 2005 | |
Title | Technical Specifications Required Plant Shutdown Began and Then Terminated |
Event Description | Unit shutdown was commenced at 2305 to comply with requirements of technical specification 3.0.3. 14 and 15 Containment Fan Coil Units (CFCU'S), 2 of 5 total CFCU's, had been removed from service to remove silt buildup in their emergency supply piping. While in this configuration, a tubing line supplying service water pressure for control of the 13SW223 (outlet flow control valve) for 13 CFCU developed a leak that rendered that valve and associated CFCU inoperable. With 3 CFCU's inoperable entry into technical specification 3.0.3 was required. A turbine load reduction was commenced at 2305 at 1% per hour. The 15 CFCU was restored to operable status at 2320 and the technical specification 3.0.3 and the load reduction were terminated. 14 CFCU was returned to operable at 2323. Repairs were made on the tubing for 13 CFCU and that was returned to operable status at 0009 on 5/6/05. 11 and 12 CFCU's were operable and in service for the duration of the event. The unit has been returned to 100% rated power.
The only other safety related equipment removed from service at the time of the event was the 13 service water pump for investigation of a reduced flow condition, and had no impact on this event. The licensee notified the NRC Resident Inspector. |
Where | |
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Salem New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-2.55 h-0.106 days <br />-0.0152 weeks <br />-0.00349 months <br />) | |
Opened: | Steve Sauer 00:32 May 6, 2005 |
NRC Officer: | Mike Ripley |
Last Updated: | May 6, 2005 |
41670 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 525812017-02-28T15:00:00028 February 2017 15:00:00
[Table view]10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Technical Specification Shutdown Due to Reactor Coolant System Pressure Boundary Leakage ENS 521292016-07-28T09:41:00028 July 2016 09:41:00 10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Source Range Instruments Reading Improperly During a Reactor Startup ENS 508962015-03-15T16:27:00015 March 2015 16:27:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Due to Failure to Restore Containment Fan Cooler Unit ENS 493002013-08-22T20:26:00022 August 2013 20:26:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit 1 Commenced a Ts Required Shutdown Due to Unidentified Rcs Leakage > 1 Gpm ENS 478742012-04-30T14:18:00030 April 2012 14:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unusual Event Due to a Potential Fire in Containment ENS 470522011-07-15T00:53:00015 July 2011 00:53:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Unusual Event Declared Based on Reactor Coolant Leak Greater than 10 Gpm ENS 442052008-05-12T19:00:00012 May 2008 19:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Shut Down Initiated Due to Inoperable Steam Generator Flow Channels ENS 416702005-05-06T03:05:0006 May 2005 03:05:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specifications Required Plant Shutdown Began and Then Terminated ENS 416162005-04-20T01:52:00020 April 2005 01:52:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specificiation Required Shutdown Related to Pressure Boundary Leakage ENS 408232004-06-17T04:22:00017 June 2004 04:22:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Plant Shutdown Due to Emergency Core Cooling System Inoperable ENS 407872004-06-02T16:30:0002 June 2004 16:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Was Initiated to Comply with Tech Spec. 3.6.1.1. Primary Containment Integrity. ENS 407642004-05-21T17:15:00021 May 2004 17:15:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown ENS 402502003-10-15T20:03:00015 October 2003 20:03:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Feedwater Regulating Valve Issue Forces Initiation of Technical Specification Shutdown 2017-02-28T15:00:00 | |
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