ENS 40250
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ENS Event | |
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20:03 Oct 15, 2003 | |
Title | Feedwater Regulating Valve Issue Forces Initiation of Technical Specification Shutdown |
Event Description | At 1603 Salem Unit 1 commenced a down power to comply with Technical Specifications. Tech. Spec. 3.0.3. was entered at 1505 when it was determined that the feed regulation valve for the 14 Steam generator (14BF19) was bound at approximately 71% open. This valve is required to close on a feedwater isolation signal. Currently the reactor is at 40% power and lowering with plans to stabilize at 25% prior to taking the unit off line (mode 3) by 2205 tonight.
Unit 1 has no other tech spec equipment out of service. Unit 1 is in two additional shutdown Technical Specifications, both are related to the control room ventilation system which is shared with Unit 2. Unit 2 is in a scheduled refueling outage and one of the Unit 2 emergency intake dampers is disabled (T.S. 3.7.6.1.a). This is a 7 day LCO that expires on 10/22/03. Additionally Unit 2's emergency filtration system is out of service for planned maintenance (T.S 3.7.6.1.a). This is a 30 day LCO that expires on 11/13/03. All other systems on Unit 1 are operating as expected for current plant conditions. The licensee notified the NRC Resident Inspector. |
Where | |
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Salem New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-0.55 h-0.0229 days <br />-0.00327 weeks <br />-7.5339e-4 months <br />) | |
Opened: | Joe Sullivan 19:30 Oct 15, 2003 |
NRC Officer: | Rich Laura |
Last Updated: | Oct 15, 2003 |
40250 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (40 %) |
WEEKMONTHYEARENS 525812017-02-28T15:00:00028 February 2017 15:00:00
[Table view]10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Technical Specification Shutdown Due to Reactor Coolant System Pressure Boundary Leakage ENS 521292016-07-28T09:41:00028 July 2016 09:41:00 10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Source Range Instruments Reading Improperly During a Reactor Startup ENS 508962015-03-15T16:27:00015 March 2015 16:27:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Due to Failure to Restore Containment Fan Cooler Unit ENS 493002013-08-22T20:26:00022 August 2013 20:26:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit 1 Commenced a Ts Required Shutdown Due to Unidentified Rcs Leakage > 1 Gpm ENS 478742012-04-30T14:18:00030 April 2012 14:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unusual Event Due to a Potential Fire in Containment ENS 470522011-07-15T00:53:00015 July 2011 00:53:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Unusual Event Declared Based on Reactor Coolant Leak Greater than 10 Gpm ENS 442052008-05-12T19:00:00012 May 2008 19:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Shut Down Initiated Due to Inoperable Steam Generator Flow Channels ENS 416702005-05-06T03:05:0006 May 2005 03:05:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specifications Required Plant Shutdown Began and Then Terminated ENS 416162005-04-20T01:52:00020 April 2005 01:52:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specificiation Required Shutdown Related to Pressure Boundary Leakage ENS 408232004-06-17T04:22:00017 June 2004 04:22:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Plant Shutdown Due to Emergency Core Cooling System Inoperable ENS 407872004-06-02T16:30:0002 June 2004 16:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Was Initiated to Comply with Tech Spec. 3.6.1.1. Primary Containment Integrity. ENS 407642004-05-21T17:15:00021 May 2004 17:15:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown ENS 402502003-10-15T20:03:00015 October 2003 20:03:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Feedwater Regulating Valve Issue Forces Initiation of Technical Specification Shutdown 2017-02-28T15:00:00 | |
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