ENS 44205
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ENS Event | |
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19:00 May 12, 2008 | |
Title | Shut Down Initiated Due to Inoperable Steam Generator Flow Channels |
Event Description | This 4-hour notification is being made to report that Salem Unit 2 has initiated a manual reactor shutdown in accordance with [Technical Specification] 3.0.3. The shutdown was initiated due to all eight steam generator steam flow channels being declared inoperable at 1500 on 5/12/08. All eight steam flow channels were indicating lower than actual steam flow such that the high steam flow coincident with low steam pressure or low-low Tave would not occur within the allowable values specified in the technical specifications. Salem Unit 2 is currently in Mode 1. Reactor Coolant System Temperature is 551 degrees Fahrenheit with pressure @ 2235 PSIG. Salem Unit 2 has no other shutdown Tech. Spec. action statements in effect. Prior to the initiating event Salem Unit 2 was raising power at 1/2 % per hour after 2R16 refueling outage.
All ECCS and ESF Systems are available. No personnel injuries have occurred as a result of the shutdown. No radiological release due to this event. 21 service water pump is cleared and tagged for strainer replacement. 21A and 23B circulating water pumps are cleared and tagged for maintenance. The licensee notified the NRC Resident Inspector. |
Where | |
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Salem New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+1.8 h0.075 days <br />0.0107 weeks <br />0.00247 months <br />) | |
Opened: | Gary Meekins 20:48 May 12, 2008 |
NRC Officer: | Pete Snyder |
Last Updated: | May 12, 2008 |
44205 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (84 %) |
After | Power Operation (20 %) |
WEEKMONTHYEARENS 525812017-02-28T15:00:00028 February 2017 15:00:00
[Table view]10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Technical Specification Shutdown Due to Reactor Coolant System Pressure Boundary Leakage ENS 521292016-07-28T09:41:00028 July 2016 09:41:00 10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Source Range Instruments Reading Improperly During a Reactor Startup ENS 508962015-03-15T16:27:00015 March 2015 16:27:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Due to Failure to Restore Containment Fan Cooler Unit ENS 493002013-08-22T20:26:00022 August 2013 20:26:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit 1 Commenced a Ts Required Shutdown Due to Unidentified Rcs Leakage > 1 Gpm ENS 478742012-04-30T14:18:00030 April 2012 14:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unusual Event Due to a Potential Fire in Containment ENS 470522011-07-15T00:53:00015 July 2011 00:53:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Unusual Event Declared Based on Reactor Coolant Leak Greater than 10 Gpm ENS 442052008-05-12T19:00:00012 May 2008 19:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Shut Down Initiated Due to Inoperable Steam Generator Flow Channels ENS 416702005-05-06T03:05:0006 May 2005 03:05:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specifications Required Plant Shutdown Began and Then Terminated ENS 416162005-04-20T01:52:00020 April 2005 01:52:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specificiation Required Shutdown Related to Pressure Boundary Leakage ENS 408232004-06-17T04:22:00017 June 2004 04:22:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Plant Shutdown Due to Emergency Core Cooling System Inoperable ENS 407872004-06-02T16:30:0002 June 2004 16:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Plant Shutdown Was Initiated to Comply with Tech Spec. 3.6.1.1. Primary Containment Integrity. ENS 407642004-05-21T17:15:00021 May 2004 17:15:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown ENS 402502003-10-15T20:03:00015 October 2003 20:03:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Feedwater Regulating Valve Issue Forces Initiation of Technical Specification Shutdown 2017-02-28T15:00:00 | |
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