ML19318A385: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(StriderTol Bot change)
 
Line 142: Line 142:
15          V-20-26; V-20-27 Core              Valves leaking through            Disassembled valve, lapped seat and disc Spray System                                                          reassembled; tested OK 16          V-26-18                            Failed leak test                  Adjusted stoke; valve then passed leak test 17          l-3 Emergency Service Water Pump    Low discharge pressure            Removed pump Low amperage readings            Cleaneo suction bell & impellers post testing OK 18          "A" CRD Filter                      High AP - needs cleaning          Changed with clean filters 19          "B" CRD Filter                      High AP - needs cleaning          Changed with clean filters 20          "A" CR0 Filter                      High AP - needs cleaning          Changed with clean filters 21          "B"  CRD Filter                    High AP - needs cleaning          Changed with new filters 22          V-26-16                            Not operating properly            Disassembled valve, cleaned shaft, replaced o-rings; reassembled; tested OK 23          "A" CRD Filter                      High AP - needs cleaning          Changed with clean filters 24          "B"  CRD Filter                    High AP - needs cleaning          Changed with clean filters 25          I-4 Emergency Service Water        Discharge check valve stuck open  Freed up hinge pin eyes & cleaned disc Pump                                                                  face; post-test operates OK 26          V-6-1000 instrument air s          Valve leaking                    Tightened body bolts - leaking stopped nitrogen system to drywell i 27          1-2 Fire Diesel                    Cooling water leak                Tightened all fittings - leak stopped 28          V-9-4                              Packing leak                      Adjusted packing to stop leak 29          Fire Protection System - Rx        Packing leak                      Adjusted packing to stop leak' Bldg - 119' El. Sprinkler System isolation Valve 30          1-2 Service Water Pump              Excessive vibration                Rebuilt pump    post-test operate
15          V-20-26; V-20-27 Core              Valves leaking through            Disassembled valve, lapped seat and disc Spray System                                                          reassembled; tested OK 16          V-26-18                            Failed leak test                  Adjusted stoke; valve then passed leak test 17          l-3 Emergency Service Water Pump    Low discharge pressure            Removed pump Low amperage readings            Cleaneo suction bell & impellers post testing OK 18          "A" CRD Filter                      High AP - needs cleaning          Changed with clean filters 19          "B" CRD Filter                      High AP - needs cleaning          Changed with clean filters 20          "A" CR0 Filter                      High AP - needs cleaning          Changed with clean filters 21          "B"  CRD Filter                    High AP - needs cleaning          Changed with new filters 22          V-26-16                            Not operating properly            Disassembled valve, cleaned shaft, replaced o-rings; reassembled; tested OK 23          "A" CRD Filter                      High AP - needs cleaning          Changed with clean filters 24          "B"  CRD Filter                    High AP - needs cleaning          Changed with clean filters 25          I-4 Emergency Service Water        Discharge check valve stuck open  Freed up hinge pin eyes & cleaned disc Pump                                                                  face; post-test operates OK 26          V-6-1000 instrument air s          Valve leaking                    Tightened body bolts - leaking stopped nitrogen system to drywell i 27          1-2 Fire Diesel                    Cooling water leak                Tightened all fittings - leak stopped 28          V-9-4                              Packing leak                      Adjusted packing to stop leak 29          Fire Protection System - Rx        Packing leak                      Adjusted packing to stop leak' Bldg - 119' El. Sprinkler System isolation Valve 30          1-2 Service Water Pump              Excessive vibration                Rebuilt pump    post-test operate


  ;        .
Oystar Crock Section #1 Docket No. 50-219 REFUELING INFORMATION - MAY 1980 Name of Facility: Oyster Creek Station #1 Scheduled date for next refueling shutdown: January 5, 1980 Scheduled date for restart following refueling:      June 11, 1980 Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?
Oystar Crock Section #1 Docket No. 50-219 REFUELING INFORMATION - MAY 1980 Name of Facility: Oyster Creek Station #1 Scheduled date for next refueling shutdown: January 5, 1980 Scheduled date for restart following refueling:      June 11, 1980 Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?
No Technical Specification change relative to the refueling is anticipated.
No Technical Specification change relative to the refueling is anticipated.

Latest revision as of 17:28, 21 February 2020

Monthly Operating Rept for May 1980
ML19318A385
Person / Time
Site: Oyster Creek
Issue date: 06/04/1980
From: Mcclain C
JERSEY CENTRAL POWER & LIGHT CO.
To:
Shared Package
ML19318A383 List:
References
NUDOCS 8006200458
Download: ML19318A385 (10)


Text

. i.

'O AVEPAGE DAILY P20ER LEUEL j

DCCEET 4..... 50-219 4 UNIT. ...... O. C. ?1 REPORT DATE... June 4, i980 CGMPILED BY... C.M. MCCLAIN 3 TztEpsesE. . . 204-455-e74e i

MONTH May i'?80 i

DAY MW DAY Mid 8 1. O. 17. O.

2. O. te. O.
3. O. 19. O.

8 4 G. 20. O.

5. O. 21. O.
6. O. 22. O.

E 7. O. 23. O.

9. O. 24. G.
9. O. 25. O.

I 10. O, 26. O.

it. O. 27. G.

0

12. O. 29. 9.
13. O. 29. O.

'4. O. 30. 9.

. . i

!5. O.

e 9

! 8006200YI3

.i.

1

+. , 2 y , c3 ,-g. r i f :

I e -;q e I a..  ::- o pg y . 5 r;. .;

?f'a' AT', 'REPARED DY...C.M. HCCLAIN 291-455-2740 g

'EPOP'INC 2ERIOD... May 1980 I t! CENSE" TuERMAL POWEP: H 'P '- .. 19M

%, epi _ : re R ATING <. GRGSS MWE ) . . 6'SO DESIGN ELECTPICAL RATING (NET MWE).. 650 i

rm.t Ir1UM DEPENDABLE CAPACITY (GROSS MWE) . 650 MAXIMUN DEPENDABLE CAPACITY (NET MWE).. 620 IF CHANGES OCCUR IM CAPACITY RATING CINCE LAST REPORT, GIVE REASON...

NONE POWER LEVEL TO WHICH RESTRICTED, IF ANY(NET MWE)... NO RESTRICTION I REASON FOR RESTRICTION, IF ANY...

NO RESTRICTION I MONTH YEAR CUMULATIVE HOURS IM PERIOD 744.0 3647.0 9151i.0 4

MCU'S RX CRITICAL 0.0 101.5 68740.8 1 RX RESERVE SHUTDOWN HRS. 0.0 0.0 463.2 HPS, GEN ON LINE 0.0 98.4 67403.9 UT RESERVE SHUTDOWN HRS 0.0 3.0 0.9 I GRCSS THERMAL EMERG'r 3 . T ~' - .. -1026769.9 GROSS ELEC EHERGY 0.0 $3670.0 39935985.0 t

fuc4 L. -

a ci e -wr sit! v, .,t c] v i n -

d 2 0. 4 t C . ,% .o -3ews o, e w.s . a-

.3. L, i sn c. .

e .a. r. ~: L:: . i,i r r e_ i a-

- _ ., -.,.r.

UT AV A ".L AE'ILITY FACTOR 0.0 2.7 73.7 t

UT V'9 CITY # ACTOR MDC

. 0.4 2.1 67.9

. ;T I r.P a C I n caCTaP Deg .. . t .;, , 3 rr.t.

  • c.- -

utr. ;c c , ., p r, . , t.

- .. ,.3. . ,s, s

a. . ,.

O

~^ ' j { [ ' ' . ', i* Mp!

l, j ji'j r.6 { , ( ._j ~~. '"g ] 7,.4 g. T y p <} q # i_ g.  ;, i .O

  • T Y D**lD

]D ' h e s j\\ s M. d a =

w i

i -

POCKET NO. 50-219 __,

UNIT SHUTDOWNS AND FOWER REDUCDONS UNIT NAME Oc #1 DATE I"n a 11: 14An

  • COMPLETED BY C. M. McClain REPORT MONTH Mav - 1980 TELEPHONE 455-8748 "t.o c w

"n.

No. Date k

.$ E g ij

}g }Yj ga:

Licensee Event E,,

mg Cause & Correceive Action to H

bE 5 jif5g R: port # j Prevent Recurrence d

1 800105 S 744.0 C 1 NA ZZ ZZZZ Refueling / Maintenance Outage l

i t

i i

i i 2 3 4 I F: Forced Reason: Method: Exhibit G-Instructions A-Equipment Failure (Explain) 1-Manual for Preparation of Data S: Scheduled B-Maintenance of Test 2 Manual Scram. Entry Sheets for Licensee C-Refueling 3 Automatic Scram. Event Report (LER) File (NUREG-D-Regulatory Restriction 4-Other (Explain) 0161)

E-Operator Training & Ucense Examination

F-Administrative 5 G4)perational Error (Explain)
  • Exhibit I-Sanw Source (9/77) Il-Other (Explain) i

Oystcr Cr ck Stetten #I Dock 3t No. 50-219 OPERATION

SUMMARY

MAY 1980 The plant was shutdown for the entire reporting period for an extended refueling outage. Major activities during the month included installation of the core spray sparger clamps, Installation of the reactor Internals and reactor head, '

and performance of the 10 year code hydrostatic test on the reactor vessel and coolant piping.

Four Reportable Occurrences were identified during the reporting period:

R.O. #80-17 was identified on May 16, 1980 when the one rod Free rod withdrawal block was found to be defeated for three control rod drives by two jumpers and a defective position Indicating probe.

R.O. #80-18 was identified on May 7,1980 when the "as found" setpoint for Reactor High Pressure Scram sensor RE030 was found to be greater than the allowable limit driving performance of routine surveillance test.

R.O. #80-19 was identified on May 17, 1980 when core spray relief ,

valves were discovered to be leaking through during testing as part of 1 j the leak reduction program.

I R.0. #80-21 was identified on May 20, 1980 when it was determined the surveillance required by Technical Specification 4.9.D was not being perfo rmed.

Oystsr Crc k Strtion #1 Docket No. 50-219 .

CORRECTIVE ELECTRICAL MAINTENANCE ON QASL ITEMS FOR THE MONTH OF May 1980 item # Equipment Malfunction Corrective Action 1 Diesel Generator Batteries Degraded battery condition Replaced unacceptable batteries 2 CRD Notch Override Switch Switch stop broken Replaced front plate on switch 3 Scram Relays Checked operation per SIL #308 Relays inspected & tested, all found to be satisfactory.

4 Vital MG Set 1-1 Defective control power trans- Replaced transformer former 5 Vital HG Set 1-1 Defective control power trans- Replaced transformer former 6 Clean-up Demineralizer Inlet Position Indication lights Installed rebuilt gear box Isolation Valve erratic 7 Cleanup Demineralizer Discharge Circuit breaker malfunction Replaced breaker to Condenser Valve during testing 8 Shutdown Cooling Minimum Flow Viv Valve wouldn't open i

Pcge I cf 2 Oystcr Creek Stction #1 Docket No. 50-219 ,

CORRECTIVE INSTRUMENT MAINTENANCE - QASL May 1980 item # Equipment Malfunction Corrective Action I CRD Pressure Transmitter RD04 Defective Unit Replaced obsolete transmitter with compatible unit.

2 SRM Channel 24 Instruments out of calibration Channel 24 LCR recorder span adjusted.

3 SRM Channels 22, 23, 24 Instruments out of calibration Channel 23 s 24 LCR recorder's span adjusted.

.4 lRM 15, detector & drive tube Defective Replaced IRM 16, detector S #4 TIP Machine in shield light Indicated early inspected 5 adjusted to indicate correctly 6 CRD 06-19 Position Indicating Constant fully in signal Replaced P.I.P.

Probe 7 CRD 06-15 Indication Position 12 didn't indicate Connection in drywell tightened.

8 CRD Drive Flow Indicator Constant Indication was less Resoldered potentiometer connections j than 0 flow ,

9 lsolation Amplifiers - plant Defective amplifiers Replaced amplifiers (OP-AMP hodule) monitoring system l

10 Off Gas. Radiation Monitor Continuous downscale alarm Span adjusted to indicate correctly Channel 1 ,

I 11 Torus Level Instruments Redundant Indicators were not Calibrated one transmitter In agreement 12 Shutdown Cooling System Needle on' indicator fell off Replaced needle. Calibrated gage.

Pressure Indicator PS-438 1

1

4 Page 2 cf 2 .

13 "D" Recirc Pump Cooling Water Readings were high & erratic Thermocouple connections reconnected.

Temp. Detector 14 CRD 10-11 Insert Solenoid Valve Loose electrical connection Tightened connector 123 15 Core Spray Sys I, PI 25 Pressure Needle off stem Replaced needle & calibrated gage.

Gage 16 Control Room Event Recorder Not tracing Jumpered across rheostat until new rheostat received 17 Reactor Head Flange Area Remove, inspect, reinstall None required '

Thermocouples(9) as needed a

l 1

J

Prg3 I of_2 Oystcr Creek Stctido #1 Docket No. 50-219 CORRECTIVE HECHANICAL MAINTENANCE ON QASL ITEMS FOR THE MONTH OF MAY 1979 Item # Equipment Malfunction Corrective Action 1 CRD 18-31 V-Ill valve leaking through Replaced Valve 2 V-20-26 (Core Spray) Packing leak Tightened packing bolts

~

3 Biological Shield Failed local leak rate test Installed new o-rings post test -

Stabilizer Hanway #1 passed leak rate test.

4 V-27-364 (Drywell Purge Failed Leak rate test Adjusted linkage and stroke post test -

Isolation Valve) passed leak rate test.

5 V-14-6 "A" Isolation Packing Leak Adjusted packing 6 V-14-30 Emergency Condenser Valves need to be repacked Repacked valves and inspected glands V-14-31 V-14-32 V-14-33 V-14-34 7 CRD System - NC16A Replace broken air piping Replaced all damaged piping with new back-up scram valve stainless steel fittings 8 CRD 38-19 V-107 valve stem damaged Replaced valve stem and handwheel 4

9 CRD 38-39 & 30-19 V-107 valves have damaged Replaced stem and handwheel stem and handwheel 10 CRD 38-19 V-107 valve has damaged stem Replaced stem and handwheel and handwheel 11 "B" CRD Filter High A -needs cleaning Changed filters with clean ones 12 "A" CRD Filter High AP - needs cleaning Installed new filters 13 "A" CRD Filter High AP - needs cleaning Installed new filters 14 "A" CRD Filter High AP - needs cleaning Changed filters with clean ones

. _ - - - _ . . . . - . _ . _ . _ . - - _ _ . _ = =

Ptga 2 of 2 ,

15 V-20-26; V-20-27 Core Valves leaking through Disassembled valve, lapped seat and disc Spray System reassembled; tested OK 16 V-26-18 Failed leak test Adjusted stoke; valve then passed leak test 17 l-3 Emergency Service Water Pump Low discharge pressure Removed pump Low amperage readings Cleaneo suction bell & impellers post testing OK 18 "A" CRD Filter High AP - needs cleaning Changed with clean filters 19 "B" CRD Filter High AP - needs cleaning Changed with clean filters 20 "A" CR0 Filter High AP - needs cleaning Changed with clean filters 21 "B" CRD Filter High AP - needs cleaning Changed with new filters 22 V-26-16 Not operating properly Disassembled valve, cleaned shaft, replaced o-rings; reassembled; tested OK 23 "A" CRD Filter High AP - needs cleaning Changed with clean filters 24 "B" CRD Filter High AP - needs cleaning Changed with clean filters 25 I-4 Emergency Service Water Discharge check valve stuck open Freed up hinge pin eyes & cleaned disc Pump face; post-test operates OK 26 V-6-1000 instrument air s Valve leaking Tightened body bolts - leaking stopped nitrogen system to drywell i 27 1-2 Fire Diesel Cooling water leak Tightened all fittings - leak stopped 28 V-9-4 Packing leak Adjusted packing to stop leak 29 Fire Protection System - Rx Packing leak Adjusted packing to stop leak' Bldg - 119' El. Sprinkler System isolation Valve 30 1-2 Service Water Pump Excessive vibration Rebuilt pump post-test operate

Oystar Crock Section #1 Docket No. 50-219 REFUELING INFORMATION - MAY 1980 Name of Facility: Oyster Creek Station #1 Scheduled date for next refueling shutdown: January 5, 1980 Scheduled date for restart following refueling: June 11, 1980 Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?

No Technical Specification change relative to the refueling is anticipated.

Scheduled date(s) for submitting proposed licensing action and supporting information:

No submittals are scheduled.

important licensing considerations associated with refue1Ing, e.g., new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures:

1. General Electric Fuel Assemblies - Fuel design and performance analysis methods have been approved by NRC. .New operating procedures, if necessary, will be submitted at a later date.
2. Exxon Fuel Assemblles - No major changes have been made, nor are there any anticipated.

i The number of fuel assemblies (a) in the core - 560 (b) in the spent fuel storage pool - 780  :

The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, in number of fuel assemblies:

Present: 1,800 Planned: 2,600 The projected date of the last refueling that can be discharged to the spent fuel pool assuming the present licensed capacity:

The Spring 1987 Outage.

. _ _ _ . . . .. - _. - - . - . . - . . - - --