Information Notice 2002-10, Manual Reactor Trip and Steam Generator Water Level Setpoint Uncertainties: Difference between revisions
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{{#Wiki_filter:UNITED | {{#Wiki_filter:UNITED STATES | ||
NUCLEAR REGULATORY COMMISSION | |||
OFFICE OF NUCLEAR REACTOR REGULATION | |||
WASHINGTON, DC 20555-0001 June 28, 2002 NRC INFORMATION NOTICE 2002-10, SUPPLEMENT 1: DIABLO CANYON MANUAL | |||
REACTOR TRIP AND STEAM | |||
GENERATOR WATER LEVEL | |||
SETPOINT UNCERTAINTIES | SETPOINT UNCERTAINTIES | ||
==ADDRESSEES== | ==ADDRESSEES== | ||
All holders of operating licenses for nuclear power reactors, except those who | All holders of operating licenses for nuclear power reactors, except those who have | ||
permanently ceased operations and have certified that fuel has been permanently removed | |||
from the reactor. | from the reactor. | ||
==PURPOSE== | ==PURPOSE== | ||
The U.S. Nuclear Regulatory Commission (NRC) is issuing this supplement to give | The U.S. Nuclear Regulatory Commission (NRC) is issuing this supplement to give addressees | ||
further information about the manual reactor trip of Diablo Canyon Unit 2 which resulted from a | |||
failure of the main feedwater regulating valve, non-conservative steam generator setpoints and | failure of the main feedwater regulating valve, non-conservative steam generator setpoints and | ||
contributing causes, and other licensee actions relating to these events. | contributing causes, and other licensee actions relating to these events. This supplement | ||
provides information that became available after the issuance of the original information notice | provides information that became available after the issuance of the original information notice | ||
(IN). | (IN). The NRC expects that recipients will review the information for applicability to their | ||
facilities and consider taking actions, as appropriate. | facilities and consider taking actions, as appropriate. However, this supplement does not | ||
contain any NRC requirements and does not require any specific action or written response. | contain any NRC requirements and does not require any specific action or written response. | ||
==BACKGROUND== | ==BACKGROUND== | ||
Diablo Canyon Nuclear Power Plant reported a manual reactor trip of Unit 2 which resulted | Diablo Canyon Nuclear Power Plant reported a manual reactor trip of Unit 2 which resulted from | ||
a loss of main feedwater to a steam generator (LER 2-2002-002-00) and that the narrow-range | |||
steam generator water level instrumentation did not respond as expected to initiate an | steam generator water level instrumentation did not respond as expected to initiate an | ||
| Line 47: | Line 62: | ||
automatic reactor trip and emergency feedwater actuation on low-low water level in the steam | automatic reactor trip and emergency feedwater actuation on low-low water level in the steam | ||
generator (LER 1-2002-001-00). | generator (LER 1-2002-001-00). The NRC issued IN 2002-10 on March 7, 2002, to inform | ||
licensees of this event. | licensees of this event. Following the issuance of the original IN, the NRC staff conducted a | ||
Special Inspection at Diablo Canyon, as well as a public meeting with Westinghouse. | Special Inspection at Diablo Canyon, as well as a public meeting with Westinghouse. In | ||
addition, Diablo Canyon has completed its Licensee Event Reports (LERs), Westinghouse has | addition, Diablo Canyon has completed its Licensee Event Reports (LERs), Westinghouse has | ||
| Line 59: | Line 74: | ||
presence of the void content of the two phase mixture above the mid-deck plate, and other | presence of the void content of the two phase mixture above the mid-deck plate, and other | ||
facilities have generated reports under Title 10, Section 50.72, of the Code of | facilities have generated reports under Title 10, Section 50.72, of the Code of Federal | ||
Regulations (10 CFR 50.72). | |||
==DESCRIPTION OF CIRCUMSTANCES== | ==DESCRIPTION OF CIRCUMSTANCES== | ||
On February 9, 2002, with Unit 2 at full power, main feedwater regulating valve(MFRV) FW-2-FCV-540 failed in the closed position, resulting in a rapid decrease in the | On February 9, 2002, with Unit 2 at full power, main feedwater regulating valve | ||
(MFRV) FW-2-FCV-540 failed in the closed position, resulting in a rapid decrease in the water | |||
main feedwater regulating valve closed. | ML021820008 | ||
IN 2002-10 Sup 1 level of Steam Generator 2-4. The indicated narrow-range water level decreased to 7.5 percent | |||
and leveled out. Operators tripped the Unit 2 reactor within approximately 1 minute after the | |||
main feedwater regulating valve closed. On February 14, 2002, after the Unit 2 restart but while | |||
still investigating the event, the licensee identified a potentially unanalyzed condition involving | still investigating the event, the licensee identified a potentially unanalyzed condition involving | ||
the narrow-range steam generator water level instrumentation. | the narrow-range steam generator water level instrumentation. The licensee determined that | ||
during the plant transient, the actual water level in steam generator 2-4 fell below the 7.2- percent narrow-range trip setpoint for engineered safety feature and reactor trip actuations | during the plant transient, the actual water level in steam generator 2-4 fell below the 7.2- percent narrow-range trip setpoint for engineered safety feature and reactor trip actuations | ||
before operators manually tripped the reactor. | before operators manually tripped the reactor. The steam generator vendor attributed this | ||
water-level discrepancy to a previously unaccounted for differential pressure created by steam | water-level discrepancy to a previously unaccounted for differential pressure created by steam | ||
flow past the mid-deck plate in the moisture separator section of the steam generator. | flow past the mid-deck plate in the moisture separator section of the steam generator. This | ||
differential pressure phenomenon caused the steam generator narrow-range instruments to | differential pressure phenomenon caused the steam generator narrow-range instruments to | ||
indicate a higher-than-actual water level. | indicate a higher-than-actual water level. Thus, the steam generator narrow-range water level | ||
low-low setpoint was non-conservative during the loss of normal feedwater transient. | low-low setpoint was non-conservative during the loss of normal feedwater transient. | ||
mid-deck divider plate separates the two stages. | ===Physical Phenomenon and System Description=== | ||
Steam generators designed by Westinghouse incorporate two-stage moisture separation. The | |||
first stage uses centrifugal separators, and the second stage uses chevron-type separators. A | |||
mid-deck divider plate separates the two stages. The steam generator water level | |||
instrumentation uses differential pressure instruments with two ranges, a wide-range non- safety-related instrument and three or four (depending on plant) narrow-range safety-related | instrumentation uses differential pressure instruments with two ranges, a wide-range non- safety-related instrument and three or four (depending on plant) narrow-range safety-related | ||
instruments. | instruments. The wide-range instrument spans essentially the entire length of the downcomer | ||
region, while the narrow-range instruments span only the upper 25 percent of the wide-range to | region, while the narrow-range instruments span only the upper 25 percent of the wide-range to | ||
cover the normal operating band. | cover the normal operating band. The upper taps for all four instruments are located above the | ||
mid-deck plate, while the lower taps are all located below this plate. | |||
In the event at Diablo Canyon, the holes in the mid-deck, which were designed to allow | |||
moisture removed from the second-stage separators to flow back into the downcomers, acted | |||
as orifices which restricted steam flow and allowed pressure differences with water levels | as orifices which restricted steam flow and allowed pressure differences with water levels | ||
below the mid-deck region. | below the mid-deck region. At higher steam flow rates with a decreasing steam generator | ||
water level, steam exiting the first stage separators along with the moisture being separated | water level, steam exiting the first stage separators along with the moisture being separated | ||
was enough to build up pressure below the plate that was not acting above the plate. | was enough to build up pressure below the plate that was not acting above the plate. Since the | ||
upper steam generator water level instrument taps were connected above the plate, a pressure | upper steam generator water level instrument taps were connected above the plate, a pressure | ||
| Line 108: | Line 142: | ||
difference acted on the four instruments and provided a bias that caused the instruments to | difference acted on the four instruments and provided a bias that caused the instruments to | ||
indicate a higher-than-actual level. | indicate a higher-than-actual level. For the limiting safety setting of the low-low steam | ||
generator water level setpoint, this bias acts in the non-conservative direction. | generator water level setpoint, this bias acts in the non-conservative direction. The magnitude | ||
of the bias drops as the steam flow decreases. | of the bias drops as the steam flow decreases. | ||
===Post Trip Analysis=== | |||
Following this event, the NRC completed an onsite special team inspection at Diablo Canyon | |||
regulations and the conditions of the Diablo Canyon license. | Nuclear Power Plant. The inspection examined the events surrounding the Unit 2 reactor trip | ||
on February 9, 2002, as they relate to safety and compliance with the Commissions rules and | |||
regulations and the conditions of the Diablo Canyon license. The inspection consisted of | |||
examining procedures and records, and interviewing station personnel and staff members, as | examining procedures and records, and interviewing station personnel and staff members, as | ||
well as the reactor plant contractor. | well as the reactor plant contractor. The NRCs Special Inspection Team also developed a | ||
detailed sequence of events and organizational response time line which is summarized in the | detailed sequence of events and organizational response time line which is summarized in the | ||
Overview and Sequence of Events Attachment 2 to this IN. | |||
IN 2002-10 Sup 1 This event provided an unusual challenge to the licensee in that it involved an | IN 2002-10 Sup 1 This event provided an unusual challenge to the licensee in that it involved an unrecognized | ||
the failure mechanisms are usually well-understood. | phenomenon. Many plant events involve equipment behaving in an unexpected manner, but | ||
the failure mechanisms are usually well-understood. However, a well-structured corrective | |||
action process should still be effective under these circumstances by being sufficiently rigorous | action process should still be effective under these circumstances by being sufficiently rigorous | ||
| Line 134: | Line 175: | ||
to recognize conditions that are adverse to quality and then treating them according to their | to recognize conditions that are adverse to quality and then treating them according to their | ||
safety significance. | safety significance. From a review of the post trip review, the NRCs Special Inspection Team | ||
concluded that the licensees process was narrowly focused on finding, understanding, and | |||
correcting the cause of the trip. While the stations post-trip analysis procedure contained steps | |||
to review plant behavior before, during, and after the event, this was effectively not performed. | |||
The cause of the event was readily apparent without the need to analyze plant parameters. | The cause of the event was readily apparent without the need to analyze plant parameters. | ||
However, by not performing a methodical review of the | However, by not performing a methodical review of the plants behavior and comparing it to the | ||
behavior expected under those conditions, the licensee failed to recognize that an automatic | |||
plant trip and ESF actuation of auxiliary feedwater did not occur when required. | plant trip and ESF actuation of auxiliary feedwater did not occur when required. Had this been | ||
recognized, the licensee would probably have delayed restarting the plant until after the cause | recognized, the licensee would probably have delayed restarting the plant until after the cause | ||
and implications were understood. | and implications were understood. | ||
The licensees review of the anomalous steam generator water level attempted to explain why | |||
wide-range indication did not track with narrow-range indication, which was thought to have | |||
indicated accurately. The NRCs Special Inspection Team concluded that the licensees theory | |||
and supporting data were not compared with other available but conflicting indications. The | |||
licensee calculated that the event would have resulted in loss of approximately 75 percent of | licensee calculated that the event would have resulted in loss of approximately 75 percent of | ||
| Line 166: | Line 207: | ||
the initial water mass in the affected steam generator, and should have caused the wide-range | the initial water mass in the affected steam generator, and should have caused the wide-range | ||
level to be 20 percent of the actual level. | level to be 20 percent of the actual level. The licensee did not note that the bottom of the | ||
narrow-range corresponds to approximately 75 percent wide-range level, so the narrow-range | narrow-range corresponds to approximately 75 percent wide-range level, so the narrow-range | ||
instruments should have been expected to be reading off scale low. | instruments should have been expected to be reading off scale low. Also, when auxiliary | ||
feedwater actuated, narrow-range level instruments did not show increasing level until after | feedwater actuated, narrow-range level instruments did not show increasing level until after | ||
some delay, confirming that actual level was well below the narrow-range.In addressing the wide-range instrument question, it was clear that the licensee was not | some delay, confirming that actual level was well below the narrow-range. | ||
In addressing the wide-range instrument question, it was clear that the licensee was not fully | |||
satisfied that the issue was well-understood. However, rather than clarify the issue | |||
immediately, the licensee used a station administrative process that required resolution of the | immediately, the licensee used a station administrative process that required resolution of the | ||
| Line 180: | Line 225: | ||
issue within 30 days, and declared the problem to be an issue needing validation to determine | issue within 30 days, and declared the problem to be an issue needing validation to determine | ||
impact on operability. | impact on operability. The NRCs Special Inspection Team concluded that this process was not | ||
integrated with the stations operability determination process, and could permit an issue that | |||
was thought to relate to an operability question to be studied for 30 days before addressing the | |||
operability question. Although this issue was resolved in 4 days, this approach was considered | operability question. Although this issue was resolved in 4 days, this approach was considered | ||
| Line 190: | Line 235: | ||
to be contrary to Generic Letter 91-18, which provided guidance on the need to perform prompt | to be contrary to Generic Letter 91-18, which provided guidance on the need to perform prompt | ||
operability assessments. The following paragraphs present examples of corrective actions from other licensees: | operability assessments. | ||
The following paragraphs present examples of corrective actions from other licensees: | |||
Callaway | |||
Callaway reported (EN 38740) that based on an assessment of its steam generator narrow- range low-low level trip setpoints, the existing low-low level trip at 14.8 percent did not account | |||
for the uncertainties associated with the differential pressure created by the steam flow past the | for the uncertainties associated with the differential pressure created by the steam flow past the | ||
mid-deck plate in the moisture separator section of the steam generator. | mid-deck plate in the moisture separator section of the steam generator. A plant power | ||
reduction was commenced at 4:58 p.m. on February 28, 2002, to decrease reactor power to | reduction was commenced at 4:58 p.m. on February 28, 2002, to decrease reactor power to | ||
| Line 202: | Line 252: | ||
plate differential pressure condition will no longer result in a non-conservative setpoint. | plate differential pressure condition will no longer result in a non-conservative setpoint. | ||
IN 2002-10 Sup 1 | IN 2002-10 Sup 1 Salem | ||
Similar to Callaway, the low-low level trip at 9 percent did not account for the uncertainties and | |||
Salem reduced power to 38 percent. | |||
Sequoyah | |||
Sequoyah personnel also performed an assessment and determined that the existing 10.7 percent low-low level trip setpoint did not account for the uncertainties associated with the | |||
differential pressure created by the steam flow past the mid-deck plate in the moisture | differential pressure created by the steam flow past the mid-deck plate in the moisture | ||
separator section of the steam generator. | separator section of the steam generator. As a conservative measure, after Westinghouse | ||
identified this issue via NSAL 02-3, Sequoyah actuated the environmental allowance monitor | identified this issue via NSAL 02-3, Sequoyah actuated the environmental allowance monitor | ||
(EAM) on Friday, February 15, 2002. | (EAM) on Friday, February 15, 2002. This feature changed the steam generator low-low level | ||
reactor trip setpoint from 10.7 percent to 15 percent. | reactor trip setpoint from 10.7 percent to 15 percent. Since the known steam generator channel | ||
uncertainty was 8.3 percent with a narrow-range span uncertainty of 5.3 percent, Sequoyah | uncertainty was 8.3 percent with a narrow-range span uncertainty of 5.3 percent, Sequoyah | ||
| Line 218: | Line 276: | ||
determined that operating with the EAMs continuously actuated would allow continued | determined that operating with the EAMs continuously actuated would allow continued | ||
operation. Callaway, Salem, and Sequoyah have since recalibrated the low-low water level setpoints | operation. | ||
Callaway, Salem, and Sequoyah have since recalibrated the low-low water level setpoints for | |||
the steam generator with the additional margin to account for this newly identified error. The | |||
licensees completed this instrument recalibration before increasing the plants | licensees completed this instrument recalibration before increasing the plants power level to full | ||
reactor power. | |||
feedwater actuation. | Conclusion | ||
The event described in this IN highlights the potential impact of steam generator water level | |||
setpoint errors. These errors could delay the expected automatic reactor trip and emergency | |||
feedwater actuation. The IN identifies additional accident analyses and systems associated | |||
with the mid-deck plate phenomenon and highlights the importance of a thorough post-trip | with the mid-deck plate phenomenon and highlights the importance of a thorough post-trip | ||
analysis prior to restart. | analysis prior to restart. The IN also provides some of the corrective actions taken because of | ||
this event and provides information sources for further investigation. | this event and provides information sources for further investigation. | ||
IN 2002-10 Sup 1 This information notice does not require any specific action or written response. | IN 2002-10 Sup 1 This information notice does not require any specific action or written response. If you have | ||
any questions about the information in this notice, please contact any of the technical contacts | |||
listed below or the appropriate project manager from the NRCs Office of Nuclear Reactor | |||
Regulation (NRR). | |||
/RA/ | |||
William D. Beckner, Program Director | |||
Operating Reactor Improvements Program | |||
Division of Regulatory Improvement Programs | Division of Regulatory Improvement Programs | ||
Office of Nuclear Reactor | Office of Nuclear Reactor Regulation | ||
Technical contacts: Jerry Dozier, NRR Neil OKeefe, Region IV | |||
(301) 415-1014 (361) 972-2507 Email: jxd@nrc.gov Email: nfo@nrc.gov | |||
Hukam Garg, NRR | |||
(301) 415-2929 Email: hcg@nrc.gov | |||
Attachments: | |||
1. List of References | |||
2. Overview and Sequence of Events | |||
3. List of Recently Issued NRC Information Notices | |||
IN 2002-10 Sup 1 This information notice does not require any specific action or written response. If you have | |||
any questions about the information in this notice, please contact any of the technical contacts | |||
listed below or the appropriate project manager from the NRCs Office of Nuclear Reactor | |||
Regulation (NRR). | |||
/RA/ | |||
William D. Beckner, Program Director | |||
Operating Reactor Improvements Program | |||
Division of Regulatory Improvement Programs | Division of Regulatory Improvement Programs | ||
Office of Nuclear Reactor | Office of Nuclear Reactor Regulation | ||
Technical contacts: Jerry Dozier, NRR Neil OKeefe, Region IV | |||
(301) 415-1014 (361) 972-2507 Email: jxd@nrc.gov Email: nfo@nrc.gov | |||
Hukam Garg, NRR | |||
(301) 415-2929 Email: hcg@nrc.gov | |||
Attachments: | |||
1. List of References | |||
2. Overview and Sequence of Events | |||
3. List of Recently Issued NRC Information Notices | |||
DISTRIBUTION: | |||
ADAMS | |||
IN File | |||
ADAMS ACCESSION #: *See previous concurrence | |||
DOCUMENT NAME: G:RORP\OES\Dozier\in2002-10s1shortversion.wpd | |||
OFFICE RSE:RORP:DRIP TECH EDITOR RSE:RIII RSE:DE:EEIB | |||
NAME IJDozier NOKeefe* HGarg* | |||
DATE 06 /03/2002 06/03/2002 06/03/2002 06/25/2002 OFFICE BC:DE:EEIB SC:OES:RORP:DRIP PD:RORP:DRIP | |||
NAME JCalvo* TReis WDBeckner | |||
DATE 06/25/2002 06/27/2002 06/28/2002 OFFICIAL RECORD COPY | |||
1989, for Unit 2. | |||
Attachment 1 IN 2002-10 Sup 1 REFERENCES | |||
LER 1-2002-001-00, Technical Specification Violation Due to Non-Conservative Steam | |||
Generator Narrow-Range Water Level Instrumentation, Diablo Canyon Nuclear Power Plant, April 15, 2002. | |||
LER 2-2002-002-00, Unit 2 Manual Reactor Trip Due to Loss of Main Feedwater to a Steam | |||
Generator, Diablo Canyon Nuclear Power Plant, April 10, 2002. | |||
NRC Special Team Inspection Reports 50-275/02-07 and 50-323/02-07 for Diablo Canyon | |||
Nuclear Power Plant, April 8, 2002. | |||
NRC Information Notice 2002-10, Non-Conservative Water Level Setpoints on Steam | |||
Generators, March 7, 2002. | |||
Westinghouse Nuclear Safety Advisory Letter NSAL-02-3, Steam Generator Mid-Deck Plate | |||
Pressure Loss Issue, February 15, 2002. | |||
Westinghouse Nuclear Safety Advisory Letter NSAL-02-3, Rev. 1, Steam Generator Mid-Deck | |||
Plate Pressure Loss Issue, April 8, 2002. | |||
Westinghouse Nuclear Safety Advisory Letter NSAL-02-4, Maximum Reliable Indicated Steam | |||
Generator Water Level, February 19, 2002. | |||
Westinghouse Nuclear Safety Advisory Letter NSAL-02-5, Steam Generator Water Level | |||
Control Uncertainty Issue, February 19, 2002. | |||
Westinghouse Steam Generator Water Level Uncertainty Issues Handout from NRC Public | |||
Meeting in Rockville, Maryland, March 20, 2002. | |||
Event Report 38697, Technical Specification Required Shutdown of Both Units Because | |||
Steam Generator Water Level Instrument Channels are Inoperable Due to a Non-Conservative | |||
Water Level Low-Low Setpoint, Diablo Canyon Nuclear Power Plant, February 14, 2002. | |||
Event Report 38713, Safe Shutdown Capability Impacted by Non-Conservative SG NR | |||
Setpoint, Sequoyah Nuclear Power Plant, February 20, 2002. | |||
Event Report 38740, Safe Shutdown Capability Impacted by Non-Conservative SG NR | |||
Setpoint, Callaway Nuclear Power Plant, February 28, 2002. | |||
Event Report 38702, Discovery of a Non-Conservative Low-Low Level Trip Setpoint Due to a | |||
Differential Pressure Phenomenon that Causes Steam Generator Narrow-Range Level | |||
Channels to Read Higher Than Actual Water Level at High Steam Flows, Salem, February 15, | |||
2002. | |||
Attachment 2 IN 2002-10 Sup 1 Overview and Sequence of Events | |||
This section discusses applicable events and actions before, during, and following the failure of | |||
steam generator feedwater regulating valve number 4. | |||
In 1989, Diablo Canyon revised the steam generator narrow-range low-low level trip setpoint in | |||
accordance with License Amendment 34 for Unit 1 and Amendment 33 for Unit 2. The nuclear | |||
steam supply system (NSSS) vendor (Westinghouse) provided the analysis to reduce the low- low trip setpoint in topical report, WCAP-11784, Calculation of Steam Generator Level Low and | |||
Low-Low Trip Setpoints With Use of a Rosemount 1154 Transmitter. The licensee reduced | |||
the setpoint from 15 to 7.2 percent narrow-range on May 10, 1989, for Unit 1, and on April 12, | |||
1989, for Unit 2. However, the licensee did not factor the mid-deck plate differential pressure | |||
into the narrow-range low-low level trip setpoint at this time because the mid-deck phenomenon | into the narrow-range low-low level trip setpoint at this time because the mid-deck phenomenon | ||
was unknown.In 1998, Westinghouse recognized the mid-deck phenomenon while evaluating the design | was unknown. | ||
In 1998, Westinghouse recognized the mid-deck phenomenon while evaluating the design of | |||
new (replacement) steam generators using computer modeling tools that were not available | |||
during the design review for the original steam generators. | during the design review for the original steam generators. Westinghouse began accounting | ||
for this bias in the setpoint calculation during design work for replacement steam generators. | for this bias in the setpoint calculation during design work for replacement steam generators. | ||
| Line 301: | Line 472: | ||
Westinghouse began assessing the potential impact of the mid-deck plate for original model | Westinghouse began assessing the potential impact of the mid-deck plate for original model | ||
steam generators in late 1999. | steam generators in late 1999. Westinghouse was planning to issue Nuclear Safety Advisory | ||
Letters about the mid-deck phenomenon at about the time of the Diablo Canyon manual reactor | Letters about the mid-deck phenomenon at about the time of the Diablo Canyon manual reactor | ||
trip.On February 9, 2002, the Main Feed Regulating Valve (MFRV) FW-2-FCV-540 failed closed,stopping the feedwater flow to steam generator 2-4. | trip. | ||
operators initiated a manual reactor trip. | |||
On February 9, 2002, the Main Feed Regulating Valve (MFRV) FW-2-FCV-540 failed closed, stopping the feedwater flow to steam generator 2-4. After a failed attempt to reopen the MFRV, | |||
operators initiated a manual reactor trip. The cause of the MFRV failure was excess current in | |||
the coil of an Asco model L206-381-6F solenoid valve (SV), which in turn caused the failure of a | the coil of an Asco model L206-381-6F solenoid valve (SV), which in turn caused the failure of a | ||
power fuse and forced the MFRV to close. | power fuse and forced the MFRV to close. | ||
During discussions with the resident inspectors after the event, the operations manager and | |||
shift supervision expressed skepticism that the steam generator level dropped as low as | |||
observed by the steam generator wide-range instrument during the trip. The shift technical | |||
wide-range level. | advisor confirmed that the wide-range level indication reached 10 percent. Diablo Canyons | ||
Engineering Services reported that steam generator structural integrity was not affected by low | |||
wide-range level. Engineering Services preliminarily concluded that dynamic processes | |||
contributed to inaccurate wide-range level indication. Later that night, during a conference call | |||
with the NRC staff to discuss the licensees plans for the restart of Unit 2, the licensee reviewed | |||
its corrective actions for the feedwater regulating valve and other failed components. The NRC | |||
staff expressed concern that wide-range indicated level was abnormally low for this transient. | staff expressed concern that wide-range indicated level was abnormally low for this transient. | ||
| Line 336: | Line 513: | ||
the wide-range level indication was overly conservative but did not impact operator response to | the wide-range level indication was overly conservative but did not impact operator response to | ||
such an indication. | such an indication. The NRC decided to conduct follow up activities on level anomalies. The | ||
Plant Staff Review Committee reviewed the results of the trip event response team investigation | Plant Staff Review Committee reviewed the results of the trip event response team investigation | ||
and readiness for restart. | and readiness for restart. The steam generator wide-range water level anomaly issue was | ||
Attachment | Attachment 2 IN 2002-10 Sup 1 discussed and determined not to be a restart issue. The issue was classified as an issue | ||
needing validation to determine impact on operability (INVDIO). The Station Director granted | |||
plant | permission to restart the plant. | ||
narrow-range indication as a potential concern. | Unit 2 was restarted the next day (February 10, 2002). The licensee continued its investigation | ||
of the Unit 2 steam generator response during the transient. Diablo Canyon personnel sent | |||
plant trip data to Westinghouse for review. The licensee began to focus on steam generator | |||
narrow-range indication as a potential concern. During a conference call between the licensee | |||
and Westinghouse on February 14, 2002, Westinghouse informed the licensee about a new | and Westinghouse on February 14, 2002, Westinghouse informed the licensee about a new | ||
| Line 354: | Line 537: | ||
process measurement error term related to mid-deck plate differential pressure that had not | process measurement error term related to mid-deck plate differential pressure that had not | ||
been included in the existing setpoint analysis. | been included in the existing setpoint analysis. Operators in both units declared all channels of | ||
narrow-range level instrumentation inoperable and entered Technical Specification 3.0.3. | narrow-range level instrumentation inoperable and entered Technical Specification 3.0.3. | ||
Operations issued a shift order to manually trip the reactor on loss of feedwater flow. | Operations issued a shift order to manually trip the reactor on loss of feedwater flow. Operators | ||
in both units began reducing power to less than 60-percent thermal power to restore the | in both units began reducing power to less than 60-percent thermal power to restore the | ||
narrow-range instruments to an operable condition and exit Technical Specification 3.0.3. | narrow-range instruments to an operable condition and exit Technical Specification 3.0.3. On | ||
the basis of information received from Westinghouse, the licensee promptly completed an | the basis of information received from Westinghouse, the licensee promptly completed an | ||
operability assessment which concluded that the existing trip setpoint at a 7.2 percent narrow- range level remained operable at or below 60-percent reactor power. | operability assessment which concluded that the existing trip setpoint at a 7.2 percent narrow- range level remained operable at or below 60-percent reactor power. Operators stopped power | ||
reductions at 60-percent power. | reductions at 60-percent power. This action had to be taken because the failure to correct this | ||
condition prior to restart resulted in Unit 2 changing Modes (Mode 3 to 2 to 1) with the reactor | condition prior to restart resulted in Unit 2 changing Modes (Mode 3 to 2 to 1) with the reactor | ||
| Line 376: | Line 559: | ||
inoperable and subsequent operation of Units 1 and 2 (Mode 1) in a condition prohibited by | inoperable and subsequent operation of Units 1 and 2 (Mode 1) in a condition prohibited by | ||
Technical Specification 3.3.1. | Technical Specification 3.3.1. This Technical Specification requires that the reactor trip system | ||
instrumentation for steam generator level low-low be operable for Modes 1 and 2 and the | instrumentation for steam generator level low-low be operable for Modes 1 and 2 and the | ||
| Line 382: | Line 565: | ||
engineered safety feature actuation instrumentation steam generator water level-low-low be | engineered safety feature actuation instrumentation steam generator water level-low-low be | ||
operable in Modes 1, 2, and 3. | operable in Modes 1, 2, and 3. | ||
On February 15, 2002, the licensee implemented setpoint changes on both units to raise the | |||
steam generator low-low setpoint to 15 percent. After implementation, operators increased | |||
power to 100 percent in both units. | power to 100 percent in both units. Westinghouse issued NSAL 02-3, Steam Generator Mid- Deck Plate Pressure Loss Issue on February 19, 2002. That NSAL warned plants with | ||
Westinghouse-designed steam generators that the error source has not been accounted for | |||
and has potentially adverse effects on steam generator level low-low uncertainty calculations as | and has potentially adverse effects on steam generator level low-low uncertainty calculations as | ||
a bias in the indicated high direction. | a bias in the indicated high direction. Westinghouse further warned that for plants for which | ||
Westinghouse maintains the calculation of record, this pressure drop effect may require a | Westinghouse maintains the calculation of record, this pressure drop effect may require a | ||
maximum decrease of | maximum decrease of approximately 9 percent (in percent narrow-range span) in the safety | ||
analysis limit (SAL) for establishing the low-low steam generator water level reactor trip for the | analysis limit (SAL) for establishing the low-low steam generator water level reactor trip for the | ||
| Line 400: | Line 587: | ||
loss of normal feedwater (LONF) transient or the loss of offsite power (LOOP) transient to | loss of normal feedwater (LONF) transient or the loss of offsite power (LOOP) transient to | ||
compensate for this bias. | compensate for this bias. NSAL 02-3 added additional transients to consider, such as the | ||
steamline break mass and energy release, and for plants with feed line check valves inside | steamline break mass and energy release, and for plants with feed line check valves inside | ||
containment, the feedline break transient, to compensate for this described bias. | containment, the feedline break transient, to compensate for this described bias. Revision 1 to | ||
the NSAL 02-3 also provided updated information regarding the steam generator water level | the NSAL 02-3 also provided updated information regarding the steam generator water level | ||
mid-deck plate pressure loss issue. | mid-deck plate pressure loss issue. Specifically, Westinghouse revised the NSAL to address | ||
the impact of this issue on the feedwater line break analysis (when feedwater check valves | the impact of this issue on the feedwater line break analysis (when feedwater check valves | ||
| Line 414: | Line 601: | ||
were located inside containment), the ATWS mitigation system actuation circuitry system, and | were located inside containment), the ATWS mitigation system actuation circuitry system, and | ||
steamline break mass and energy release calculations. | steamline break mass and energy release calculations. Westinghouse subsequently issued | ||
NSAL 02-4, | NSAL 02-4, Maximum Reliable Indicated Steam Generator Water Level, and NSAL 02-5, Steam Generator Water Level Control System Uncertainty Issue on February 19, 2002. | ||
Revision 1 to NSAL 02-5 was written to clarify the need to calculate the steam generator water | |||
Attachment | Attachment 2 IN 2002-10 Sup 1 level uncertainties at normal operating level, including the impact, if any, of the mid-deck plate | ||
analyses to determine if they remain bounding. | pressure differential and to compare the uncertainties used in the initial condition of the safety | ||
analyses to determine if they remain bounding. NSAL 02-5, Rev. 1, also discusses the | |||
potential impact on safety analyses performed at reactor power levels other than 100 percent | potential impact on safety analyses performed at reactor power levels other than 100 percent | ||
| Line 432: | Line 621: | ||
Advisory Letter 02-3 and the void content of the two phase mixture above the mid-deck plate | Advisory Letter 02-3 and the void content of the two phase mixture above the mid-deck plate | ||
(NSAL 02-4). | (NSAL 02-4). Westinghouse also held a workshop with industry representatives on | ||
February 28, 2002 and a public meeting with the NRC staff on March 20, 2002. | |||
In its LER, Diablo Canyon indicated that it will submit a license amendment request to revise | |||
the Technical Specifications to account for the mid-deck plate differential pressure in the steam | |||
generator narrow-range low-low level protection setpoints. | generator narrow-range low-low level protection setpoints. | ||
Attachment 3 IN 2002-10 Sup 1 LIST OF RECENTLY ISSUED | |||
NRC INFORMATION NOTICES | |||
_____________________________________________________________________________________ | |||
Information Date of | |||
Notice No. Subject Issuance Issued to | |||
_____________________________________________________________________________________ | |||
2002-22 Degraded Bearing Surfaces in 06/28/2002 All holders of operating licenses | |||
GM/EMD Emergency Diesel for pressurized- or boiling-water | |||
nuclear power reactors, including | Generators nuclear power reactors, including | ||
those that have ceased | those that have ceased | ||
operations but have fuel on site.2002- | operations but have fuel on site. | ||
2002-21 Axial Outside-Diameter 06/25/2002 All holders of operating licenses | |||
Cracking Affecting Thermally for pressurized-water reactors | |||
(PWRs), except those who have | Treated Alloy 600 Steam (PWRs), except those who have | ||
permanently ceased operations | Generator Tubing permanently ceased operations | ||
and have certified that fuel has | and have certified that fuel has | ||
| Line 466: | Line 663: | ||
been permanently removed from | been permanently removed from | ||
the reactor.2002- | the reactor. | ||
2002-19 Medical Misadministrations 06/14/2002 All nuclear pharmacies and | |||
Caused By Failure to Properly medical licensees. | |||
Perform Tests on Dose | |||
Calibrators for Beta-and Low- Energy Photon-Emitting | Calibrators for Beta-and Low- Energy Photon-Emitting | ||
Radionuclides | |||
2002-18 Effect of Adding Gas Into 06/06/2002 All holders of operating licenses | |||
permanently ceased operations | Water Storage Tanks on the for nuclear power reactors, Net Positive Suction Head For except those who have | ||
Pumps permanently ceased operations | |||
and have certified that fuel has | and have certified that fuel has | ||
| Line 482: | Line 685: | ||
been permanently removed from | been permanently removed from | ||
the reactor.2002- | the reactor. | ||
2002-17 Medical Use of Strontium-90 05/30/2002 All U.S. Nuclear Regulatory | |||
Eye Applicators: New Commission medical licensees | |||
Requirements for Calibration that use strontium-90 (Sr-90) eye | |||
and Decay Correction applicators. | |||
Note: NRC generic communications may be received in electronic format shortly after they are | |||
issued by subscribing to the NRC listserver as follows: | |||
To subscribe send an e-mail to <listproc@nrc.gov >, no subject, and the following | |||
command in the message portion: | |||
subscribe gc-nrr firstname lastname | |||
______________________________________________________________________________________ | |||
OL = Operating License | |||
CP = Construction Permit}} | |||
{{Information notice-Nav}} | {{Information notice-Nav}} | ||
Revision as of 05:16, 24 November 2019
| ML021820008 | |
| Person / Time | |
|---|---|
| Site: | Diablo Canyon |
| Issue date: | 06/28/2002 |
| From: | Beckner W NRC/NRR/DRIP/RORP |
| To: | |
| Dozier J, NRR/RLSB 415-1014 | |
| References | |
| TAC M4812 IN-02-010, Suppl 1 | |
| Download: ML021820008 (15) | |
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, DC 20555-0001 June 28, 2002 NRC INFORMATION NOTICE 2002-10, SUPPLEMENT 1: DIABLO CANYON MANUAL REACTOR TRIP AND STEAM
GENERATOR WATER LEVEL
SETPOINT UNCERTAINTIES
ADDRESSEES
All holders of operating licenses for nuclear power reactors, except those who have
permanently ceased operations and have certified that fuel has been permanently removed
from the reactor.
PURPOSE
The U.S. Nuclear Regulatory Commission (NRC) is issuing this supplement to give addressees
further information about the manual reactor trip of Diablo Canyon Unit 2 which resulted from a
failure of the main feedwater regulating valve, non-conservative steam generator setpoints and
contributing causes, and other licensee actions relating to these events. This supplement
provides information that became available after the issuance of the original information notice
(IN). The NRC expects that recipients will review the information for applicability to their
facilities and consider taking actions, as appropriate. However, this supplement does not
contain any NRC requirements and does not require any specific action or written response.
BACKGROUND
Diablo Canyon Nuclear Power Plant reported a manual reactor trip of Unit 2 which resulted from
a loss of main feedwater to a steam generator (LER 2-2002-002-00) and that the narrow-range
steam generator water level instrumentation did not respond as expected to initiate an
automatic reactor trip and emergency feedwater actuation on low-low water level in the steam
generator (LER 1-2002-001-00). The NRC issued IN 2002-10 on March 7, 2002, to inform
licensees of this event. Following the issuance of the original IN, the NRC staff conducted a
Special Inspection at Diablo Canyon, as well as a public meeting with Westinghouse. In
addition, Diablo Canyon has completed its Licensee Event Reports (LERs), Westinghouse has
issued five Nuclear Safety Advisory Letters (NSALs) relating to this phenomenon or the
presence of the void content of the two phase mixture above the mid-deck plate, and other
facilities have generated reports under Title 10, Section 50.72, of the Code of Federal
Regulations (10 CFR 50.72).
DESCRIPTION OF CIRCUMSTANCES
On February 9, 2002, with Unit 2 at full power, main feedwater regulating valve
(MFRV) FW-2-FCV-540 failed in the closed position, resulting in a rapid decrease in the water
IN 2002-10 Sup 1 level of Steam Generator 2-4. The indicated narrow-range water level decreased to 7.5 percent
and leveled out. Operators tripped the Unit 2 reactor within approximately 1 minute after the
main feedwater regulating valve closed. On February 14, 2002, after the Unit 2 restart but while
still investigating the event, the licensee identified a potentially unanalyzed condition involving
the narrow-range steam generator water level instrumentation. The licensee determined that
during the plant transient, the actual water level in steam generator 2-4 fell below the 7.2- percent narrow-range trip setpoint for engineered safety feature and reactor trip actuations
before operators manually tripped the reactor. The steam generator vendor attributed this
water-level discrepancy to a previously unaccounted for differential pressure created by steam
flow past the mid-deck plate in the moisture separator section of the steam generator. This
differential pressure phenomenon caused the steam generator narrow-range instruments to
indicate a higher-than-actual water level. Thus, the steam generator narrow-range water level
low-low setpoint was non-conservative during the loss of normal feedwater transient.
Physical Phenomenon and System Description
Steam generators designed by Westinghouse incorporate two-stage moisture separation. The
first stage uses centrifugal separators, and the second stage uses chevron-type separators. A
mid-deck divider plate separates the two stages. The steam generator water level
instrumentation uses differential pressure instruments with two ranges, a wide-range non- safety-related instrument and three or four (depending on plant) narrow-range safety-related
instruments. The wide-range instrument spans essentially the entire length of the downcomer
region, while the narrow-range instruments span only the upper 25 percent of the wide-range to
cover the normal operating band. The upper taps for all four instruments are located above the
mid-deck plate, while the lower taps are all located below this plate.
In the event at Diablo Canyon, the holes in the mid-deck, which were designed to allow
moisture removed from the second-stage separators to flow back into the downcomers, acted
as orifices which restricted steam flow and allowed pressure differences with water levels
below the mid-deck region. At higher steam flow rates with a decreasing steam generator
water level, steam exiting the first stage separators along with the moisture being separated
was enough to build up pressure below the plate that was not acting above the plate. Since the
upper steam generator water level instrument taps were connected above the plate, a pressure
difference acted on the four instruments and provided a bias that caused the instruments to
indicate a higher-than-actual level. For the limiting safety setting of the low-low steam
generator water level setpoint, this bias acts in the non-conservative direction. The magnitude
of the bias drops as the steam flow decreases.
Post Trip Analysis
Following this event, the NRC completed an onsite special team inspection at Diablo Canyon
Nuclear Power Plant. The inspection examined the events surrounding the Unit 2 reactor trip
on February 9, 2002, as they relate to safety and compliance with the Commissions rules and
regulations and the conditions of the Diablo Canyon license. The inspection consisted of
examining procedures and records, and interviewing station personnel and staff members, as
well as the reactor plant contractor. The NRCs Special Inspection Team also developed a
detailed sequence of events and organizational response time line which is summarized in the
Overview and Sequence of Events Attachment 2 to this IN.
IN 2002-10 Sup 1 This event provided an unusual challenge to the licensee in that it involved an unrecognized
phenomenon. Many plant events involve equipment behaving in an unexpected manner, but
the failure mechanisms are usually well-understood. However, a well-structured corrective
action process should still be effective under these circumstances by being sufficiently rigorous
to recognize conditions that are adverse to quality and then treating them according to their
safety significance. From a review of the post trip review, the NRCs Special Inspection Team
concluded that the licensees process was narrowly focused on finding, understanding, and
correcting the cause of the trip. While the stations post-trip analysis procedure contained steps
to review plant behavior before, during, and after the event, this was effectively not performed.
The cause of the event was readily apparent without the need to analyze plant parameters.
However, by not performing a methodical review of the plants behavior and comparing it to the
behavior expected under those conditions, the licensee failed to recognize that an automatic
plant trip and ESF actuation of auxiliary feedwater did not occur when required. Had this been
recognized, the licensee would probably have delayed restarting the plant until after the cause
and implications were understood.
The licensees review of the anomalous steam generator water level attempted to explain why
wide-range indication did not track with narrow-range indication, which was thought to have
indicated accurately. The NRCs Special Inspection Team concluded that the licensees theory
and supporting data were not compared with other available but conflicting indications. The
licensee calculated that the event would have resulted in loss of approximately 75 percent of
the initial water mass in the affected steam generator, and should have caused the wide-range
level to be 20 percent of the actual level. The licensee did not note that the bottom of the
narrow-range corresponds to approximately 75 percent wide-range level, so the narrow-range
instruments should have been expected to be reading off scale low. Also, when auxiliary
feedwater actuated, narrow-range level instruments did not show increasing level until after
some delay, confirming that actual level was well below the narrow-range.
In addressing the wide-range instrument question, it was clear that the licensee was not fully
satisfied that the issue was well-understood. However, rather than clarify the issue
immediately, the licensee used a station administrative process that required resolution of the
issue within 30 days, and declared the problem to be an issue needing validation to determine
impact on operability. The NRCs Special Inspection Team concluded that this process was not
integrated with the stations operability determination process, and could permit an issue that
was thought to relate to an operability question to be studied for 30 days before addressing the
operability question. Although this issue was resolved in 4 days, this approach was considered
to be contrary to Generic Letter 91-18, which provided guidance on the need to perform prompt
The following paragraphs present examples of corrective actions from other licensees:
Callaway
Callaway reported (EN 38740) that based on an assessment of its steam generator narrow- range low-low level trip setpoints, the existing low-low level trip at 14.8 percent did not account
for the uncertainties associated with the differential pressure created by the steam flow past the
mid-deck plate in the moisture separator section of the steam generator. A plant power
reduction was commenced at 4:58 p.m. on February 28, 2002, to decrease reactor power to
below 30 percent where engineering calculations indicate that the steam generator mid-deck
plate differential pressure condition will no longer result in a non-conservative setpoint.
IN 2002-10 Sup 1 Salem
Similar to Callaway, the low-low level trip at 9 percent did not account for the uncertainties and
Salem reduced power to 38 percent.
Sequoyah
Sequoyah personnel also performed an assessment and determined that the existing 10.7 percent low-low level trip setpoint did not account for the uncertainties associated with the
differential pressure created by the steam flow past the mid-deck plate in the moisture
separator section of the steam generator. As a conservative measure, after Westinghouse
identified this issue via NSAL 02-3, Sequoyah actuated the environmental allowance monitor
(EAM) on Friday, February 15, 2002. This feature changed the steam generator low-low level
reactor trip setpoint from 10.7 percent to 15 percent. Since the known steam generator channel
uncertainty was 8.3 percent with a narrow-range span uncertainty of 5.3 percent, Sequoyah
determined that operating with the EAMs continuously actuated would allow continued
operation.
Callaway, Salem, and Sequoyah have since recalibrated the low-low water level setpoints for
the steam generator with the additional margin to account for this newly identified error. The
licensees completed this instrument recalibration before increasing the plants power level to full
reactor power.
Conclusion
The event described in this IN highlights the potential impact of steam generator water level
setpoint errors. These errors could delay the expected automatic reactor trip and emergency
feedwater actuation. The IN identifies additional accident analyses and systems associated
with the mid-deck plate phenomenon and highlights the importance of a thorough post-trip
analysis prior to restart. The IN also provides some of the corrective actions taken because of
this event and provides information sources for further investigation.
IN 2002-10 Sup 1 This information notice does not require any specific action or written response. If you have
any questions about the information in this notice, please contact any of the technical contacts
listed below or the appropriate project manager from the NRCs Office of Nuclear Reactor
Regulation (NRR).
/RA/
William D. Beckner, Program Director
Operating Reactor Improvements Program
Division of Regulatory Improvement Programs
Office of Nuclear Reactor Regulation
Technical contacts: Jerry Dozier, NRR Neil OKeefe, Region IV
(301) 415-1014 (361) 972-2507 Email: jxd@nrc.gov Email: nfo@nrc.gov
Hukam Garg, NRR
(301) 415-2929 Email: hcg@nrc.gov
Attachments:
1. List of References
2. Overview and Sequence of Events
3. List of Recently Issued NRC Information Notices
IN 2002-10 Sup 1 This information notice does not require any specific action or written response. If you have
any questions about the information in this notice, please contact any of the technical contacts
listed below or the appropriate project manager from the NRCs Office of Nuclear Reactor
Regulation (NRR).
/RA/
William D. Beckner, Program Director
Operating Reactor Improvements Program
Division of Regulatory Improvement Programs
Office of Nuclear Reactor Regulation
Technical contacts: Jerry Dozier, NRR Neil OKeefe, Region IV
(301) 415-1014 (361) 972-2507 Email: jxd@nrc.gov Email: nfo@nrc.gov
Hukam Garg, NRR
(301) 415-2929 Email: hcg@nrc.gov
Attachments:
1. List of References
2. Overview and Sequence of Events
3. List of Recently Issued NRC Information Notices
DISTRIBUTION:
IN File
ADAMS ACCESSION #: *See previous concurrence
DOCUMENT NAME: G:RORP\OES\Dozier\in2002-10s1shortversion.wpd
OFFICE RSE:RORP:DRIP TECH EDITOR RSE:RIII RSE:DE:EEIB
NAME IJDozier NOKeefe* HGarg*
DATE 06 /03/2002 06/03/2002 06/03/2002 06/25/2002 OFFICE BC:DE:EEIB SC:OES:RORP:DRIP PD:RORP:DRIP
NAME JCalvo* TReis WDBeckner
DATE 06/25/2002 06/27/2002 06/28/2002 OFFICIAL RECORD COPY
Attachment 1 IN 2002-10 Sup 1 REFERENCES
LER 1-2002-001-00, Technical Specification Violation Due to Non-Conservative Steam
Generator Narrow-Range Water Level Instrumentation, Diablo Canyon Nuclear Power Plant, April 15, 2002.
LER 2-2002-002-00, Unit 2 Manual Reactor Trip Due to Loss of Main Feedwater to a Steam
Generator, Diablo Canyon Nuclear Power Plant, April 10, 2002.
NRC Special Team Inspection Reports 50-275/02-07 and 50-323/02-07 for Diablo Canyon
Nuclear Power Plant, April 8, 2002.
NRC Information Notice 2002-10, Non-Conservative Water Level Setpoints on Steam
Generators, March 7, 2002.
Westinghouse Nuclear Safety Advisory Letter NSAL-02-3, Steam Generator Mid-Deck Plate
Pressure Loss Issue, February 15, 2002.
Westinghouse Nuclear Safety Advisory Letter NSAL-02-3, Rev. 1, Steam Generator Mid-Deck
Plate Pressure Loss Issue, April 8, 2002.
Westinghouse Nuclear Safety Advisory Letter NSAL-02-4, Maximum Reliable Indicated Steam
Generator Water Level, February 19, 2002.
Westinghouse Nuclear Safety Advisory Letter NSAL-02-5, Steam Generator Water Level
Control Uncertainty Issue, February 19, 2002.
Westinghouse Steam Generator Water Level Uncertainty Issues Handout from NRC Public
Meeting in Rockville, Maryland, March 20, 2002.
Event Report 38697, Technical Specification Required Shutdown of Both Units Because
Steam Generator Water Level Instrument Channels are Inoperable Due to a Non-Conservative
Water Level Low-Low Setpoint, Diablo Canyon Nuclear Power Plant, February 14, 2002.
Event Report 38713, Safe Shutdown Capability Impacted by Non-Conservative SG NR
Setpoint, Sequoyah Nuclear Power Plant, February 20, 2002.
Event Report 38740, Safe Shutdown Capability Impacted by Non-Conservative SG NR
Setpoint, Callaway Nuclear Power Plant, February 28, 2002.
Event Report 38702, Discovery of a Non-Conservative Low-Low Level Trip Setpoint Due to a
Differential Pressure Phenomenon that Causes Steam Generator Narrow-Range Level
Channels to Read Higher Than Actual Water Level at High Steam Flows, Salem, February 15,
2002.
Attachment 2 IN 2002-10 Sup 1 Overview and Sequence of Events
This section discusses applicable events and actions before, during, and following the failure of
steam generator feedwater regulating valve number 4.
In 1989, Diablo Canyon revised the steam generator narrow-range low-low level trip setpoint in
accordance with License Amendment 34 for Unit 1 and Amendment 33 for Unit 2. The nuclear
steam supply system (NSSS) vendor (Westinghouse) provided the analysis to reduce the low- low trip setpoint in topical report, WCAP-11784, Calculation of Steam Generator Level Low and
Low-Low Trip Setpoints With Use of a Rosemount 1154 Transmitter. The licensee reduced
the setpoint from 15 to 7.2 percent narrow-range on May 10, 1989, for Unit 1, and on April 12,
1989, for Unit 2. However, the licensee did not factor the mid-deck plate differential pressure
into the narrow-range low-low level trip setpoint at this time because the mid-deck phenomenon
was unknown.
In 1998, Westinghouse recognized the mid-deck phenomenon while evaluating the design of
new (replacement) steam generators using computer modeling tools that were not available
during the design review for the original steam generators. Westinghouse began accounting
for this bias in the setpoint calculation during design work for replacement steam generators.
Westinghouse began assessing the potential impact of the mid-deck plate for original model
steam generators in late 1999. Westinghouse was planning to issue Nuclear Safety Advisory
Letters about the mid-deck phenomenon at about the time of the Diablo Canyon manual reactor
trip.
On February 9, 2002, the Main Feed Regulating Valve (MFRV) FW-2-FCV-540 failed closed, stopping the feedwater flow to steam generator 2-4. After a failed attempt to reopen the MFRV,
operators initiated a manual reactor trip. The cause of the MFRV failure was excess current in
the coil of an Asco model L206-381-6F solenoid valve (SV), which in turn caused the failure of a
power fuse and forced the MFRV to close.
During discussions with the resident inspectors after the event, the operations manager and
shift supervision expressed skepticism that the steam generator level dropped as low as
observed by the steam generator wide-range instrument during the trip. The shift technical
advisor confirmed that the wide-range level indication reached 10 percent. Diablo Canyons
Engineering Services reported that steam generator structural integrity was not affected by low
wide-range level. Engineering Services preliminarily concluded that dynamic processes
contributed to inaccurate wide-range level indication. Later that night, during a conference call
with the NRC staff to discuss the licensees plans for the restart of Unit 2, the licensee reviewed
its corrective actions for the feedwater regulating valve and other failed components. The NRC
staff expressed concern that wide-range indicated level was abnormally low for this transient.
The licensee explained its theory that the actual level was higher because of the difference
between the transient conditions (hot, dynamic) and the calibration conditions (cold, static).
The licensee believed that the steam generator narrow-range level response was normal, and
the wide-range level indication was overly conservative but did not impact operator response to
such an indication. The NRC decided to conduct follow up activities on level anomalies. The
Plant Staff Review Committee reviewed the results of the trip event response team investigation
and readiness for restart. The steam generator wide-range water level anomaly issue was
Attachment 2 IN 2002-10 Sup 1 discussed and determined not to be a restart issue. The issue was classified as an issue
needing validation to determine impact on operability (INVDIO). The Station Director granted
permission to restart the plant.
Unit 2 was restarted the next day (February 10, 2002). The licensee continued its investigation
of the Unit 2 steam generator response during the transient. Diablo Canyon personnel sent
plant trip data to Westinghouse for review. The licensee began to focus on steam generator
narrow-range indication as a potential concern. During a conference call between the licensee
and Westinghouse on February 14, 2002, Westinghouse informed the licensee about a new
process measurement error term related to mid-deck plate differential pressure that had not
been included in the existing setpoint analysis. Operators in both units declared all channels of
narrow-range level instrumentation inoperable and entered Technical Specification 3.0.3.
Operations issued a shift order to manually trip the reactor on loss of feedwater flow. Operators
in both units began reducing power to less than 60-percent thermal power to restore the
narrow-range instruments to an operable condition and exit Technical Specification 3.0.3. On
the basis of information received from Westinghouse, the licensee promptly completed an
operability assessment which concluded that the existing trip setpoint at a 7.2 percent narrow- range level remained operable at or below 60-percent reactor power. Operators stopped power
reductions at 60-percent power. This action had to be taken because the failure to correct this
condition prior to restart resulted in Unit 2 changing Modes (Mode 3 to 2 to 1) with the reactor
trip system and engineered safety system steam generator water level low-low instrumentation
inoperable and subsequent operation of Units 1 and 2 (Mode 1) in a condition prohibited by
Technical Specification 3.3.1. This Technical Specification requires that the reactor trip system
instrumentation for steam generator level low-low be operable for Modes 1 and 2 and the
engineered safety feature actuation instrumentation steam generator water level-low-low be
operable in Modes 1, 2, and 3.
On February 15, 2002, the licensee implemented setpoint changes on both units to raise the
steam generator low-low setpoint to 15 percent. After implementation, operators increased
power to 100 percent in both units. Westinghouse issued NSAL 02-3, Steam Generator Mid- Deck Plate Pressure Loss Issue on February 19, 2002. That NSAL warned plants with
Westinghouse-designed steam generators that the error source has not been accounted for
and has potentially adverse effects on steam generator level low-low uncertainty calculations as
a bias in the indicated high direction. Westinghouse further warned that for plants for which
Westinghouse maintains the calculation of record, this pressure drop effect may require a
maximum decrease of approximately 9 percent (in percent narrow-range span) in the safety
analysis limit (SAL) for establishing the low-low steam generator water level reactor trip for the
loss of normal feedwater (LONF) transient or the loss of offsite power (LOOP) transient to
compensate for this bias. NSAL 02-3 added additional transients to consider, such as the
steamline break mass and energy release, and for plants with feed line check valves inside
containment, the feedline break transient, to compensate for this described bias. Revision 1 to
the NSAL 02-3 also provided updated information regarding the steam generator water level
mid-deck plate pressure loss issue. Specifically, Westinghouse revised the NSAL to address
the impact of this issue on the feedwater line break analysis (when feedwater check valves
were located inside containment), the ATWS mitigation system actuation circuitry system, and
steamline break mass and energy release calculations. Westinghouse subsequently issued
NSAL 02-4, Maximum Reliable Indicated Steam Generator Water Level, and NSAL 02-5, Steam Generator Water Level Control System Uncertainty Issue on February 19, 2002.
Revision 1 to NSAL 02-5 was written to clarify the need to calculate the steam generator water
Attachment 2 IN 2002-10 Sup 1 level uncertainties at normal operating level, including the impact, if any, of the mid-deck plate
pressure differential and to compare the uncertainties used in the initial condition of the safety
analyses to determine if they remain bounding. NSAL 02-5, Rev. 1, also discusses the
potential impact on safety analyses performed at reactor power levels other than 100 percent
and the impact of steam generator water level uncertainty on LOCA mass and energy release.
These letters covered other effects of the same physical phenomenon as Nuclear Safety
Advisory Letter 02-3 and the void content of the two phase mixture above the mid-deck plate
(NSAL 02-4). Westinghouse also held a workshop with industry representatives on
February 28, 2002 and a public meeting with the NRC staff on March 20, 2002.
In its LER, Diablo Canyon indicated that it will submit a license amendment request to revise
the Technical Specifications to account for the mid-deck plate differential pressure in the steam
generator narrow-range low-low level protection setpoints.
Attachment 3 IN 2002-10 Sup 1 LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
_____________________________________________________________________________________
Information Date of
Notice No. Subject Issuance Issued to
_____________________________________________________________________________________
2002-22 Degraded Bearing Surfaces in 06/28/2002 All holders of operating licenses
GM/EMD Emergency Diesel for pressurized- or boiling-water
Generators nuclear power reactors, including
those that have ceased
operations but have fuel on site.
2002-21 Axial Outside-Diameter 06/25/2002 All holders of operating licenses
Cracking Affecting Thermally for pressurized-water reactors
Treated Alloy 600 Steam (PWRs), except those who have
Generator Tubing permanently ceased operations
and have certified that fuel has
been permanently removed from
the reactor.
2002-19 Medical Misadministrations 06/14/2002 All nuclear pharmacies and
Caused By Failure to Properly medical licensees.
Perform Tests on Dose
Calibrators for Beta-and Low- Energy Photon-Emitting
Radionuclides
2002-18 Effect of Adding Gas Into 06/06/2002 All holders of operating licenses
Water Storage Tanks on the for nuclear power reactors, Net Positive Suction Head For except those who have
Pumps permanently ceased operations
and have certified that fuel has
been permanently removed from
the reactor.
2002-17 Medical Use of Strontium-90 05/30/2002 All U.S. Nuclear Regulatory
Eye Applicators: New Commission medical licensees
Requirements for Calibration that use strontium-90 (Sr-90) eye
and Decay Correction applicators.
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OL = Operating License
CP = Construction Permit