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{{#Wiki_filter:~U.S.NUCLEAR REGULATORY COMMISSION NRC DISTRI8UTION FDR PART 50 DOCKET MATERIAL | {{#Wiki_filter:~ U.S. NUCLEAR REGULATORY COMMISSION DOCKET NUMBER FILE NUMBER NRC DISTRI8UTION FDR PART 50 DOCKET MATERIAL INCIDENT REPORT FROM:ROCHESTER GAS & ELEC. CORP. DATE OF J.P.O'REXLLY, DOCUMENT'ATE ROCHESTER, N.Y. | ||
UPDATE LICENSEE EVQP REPORT 1/76-30, 30 DAY ON 12/17/76.CONCERNIg+LXQUPJ"%EARP, FROM THE"A" MIXED.BED SEMINERAL'IZQR I%K'ET~~QIg M k4I II';I)K: NOTE~IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/Jo COLLINS'RANCH CHIEF!W 3 CYS FOR ACTION LIC, ASST'!W/CYS ACRS/CYS 14Ch5%NG S NT | 'L.D. WHITE, JR. ~ RECEIVED Q LETTE R ONOTOAIZED PROP INPUT FOAM NUMBER OF COPIES RECEIVED QOAIGINAL EBUNCLASSIFIED K)CO> Y DESCAIPTION ENCLOSURE 1'TR'RANS THE FOLLOWXNG UBDATE LICENSEE EVENT REPORT /f 76-27, 30 DAY ON 12/16/76 CONCERNING LIQUID COMING THROUGH INSULA ION ON 2" LE'ZDOWN DIVERSION LINE....... | ||
r Qg | I:. ~ | ||
UPDATE LICENSEE EVQP REPORT 1/ 76-30, 30 DAY ON (1P) . 12/17/76. CONCERNIg+LXQUPJ"%EARP, FROM THE "A" MIXED. BED SEMINERAL'IZQR I%K'ET~~QIg M k4I II';I)K: | |||
PLANT NAME' E GINNA 4/ | |||
I" SAB NOTE ~ IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/Jo COLLINS FOR ACTION/INFOFIMATI ON | |||
'RANCH CHIEF! | |||
W 3 CYS FOR ACTION LIC, ASST'! | |||
W /CYS ACRS / CYS 14Ch5%NG S NT INTERNAL DISTRI BUTION | |||
'NRC PDR MIPC | |||
~ SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES BUTLER IIANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS EANAL DISTRIBUTION CON OL NUMBER LPDR: | |||
TIC: | |||
71540052 NAC FORM 105 I2.ld) | |||
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'iI'4'"7/ "'"PW Pi i't.i<IL'/74Ii W'"W ROCHESTER GAS AND ELECTRIC CORPORATlON 89 EAST AVENUE, ROCHESTER,, N.Y. 14649 LEON D. WHITE. JR. TCLCPNONC VICC PACSIDCNT iPCi CONC TIO 54G 2700 May 27, 1977 r | |||
Mr. James P O'Reilly, Director | |||
~ | |||
8 > ge 'Ctt U. S. Nuclear Regulatory Commis%%8 g UN 2 3977~ | |||
Office of inspection and Enforcement Region I | |||
'EI re' ~I g..S. IIIIC'C">RUU5h5kV | |||
>Ncll54rtbe 63 1 Park Avenue King of Prussia, Pennsylvania 19406 | |||
==Subject:== | ==Subject:== | ||
Supplemental reports on Reportable Occurrences: | Supplemental reports on Reportable Occurrences: | ||
76-27 (30-day report)Leak in letdown diversion line 76-30 (30-day report)"A" mixed bed demineralizer inlet piping leak R.E.Qinna Nuclear Power Plant, Unit No.1 Docket No.50-244 | 76-27 (30-day report) Leak in letdown diversion line 76-30 (30-day report) "A" mixed bed demineralizer inlet piping leak R. E. Qinna Nuclear Power Plant, Unit No. 1 Docket No. 50-244 | ||
==Dear Mr. O'Reilly:== | |||
The purpose of this letter is to provide you with corrected component manufacturer information in connection with the subject reports which were submitted January 4 and January 12, 1977 respectively. The attached update reports LER 76-27/30 and LER 76-30/30 provide this information. | |||
Two additional copies of this letter and the attachments are enclosed to conform to the original submittal of LER 76-27/3L and LER 76-30/3L. | |||
Very truly yours, L. D. White Jr. | |||
cc: Dr. Ernst Volgenau (30) | |||
Mr. William G. McDonald (3) | |||
.77g540052. | |||
ao | |||
~4 | |||
~ \ | |||
J I | |||
I" ' | |||
d | |||
$ | |||
LER 76-27/30 Update Report Previous Report Date 1/4/77 CONTROL BLOCK: | |||
Q.IOENSEE EVENT REPORT | |||
+ | |||
fPLEASE PAINT ALL REQVIREO IiNFORIViATION) | |||
LICENSEE UCENSE EVENT NAME UCENSE NUMBER TYPE TYPE | |||
[op~j N Y R B G 1 0 0 0 0 0 0 0 0 0 O 1 1 1' ~03 | |||
~ | |||
7 89 14 15 25 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE REPORT DATE 0 | |||
7 | |||
[oO~]corn 8 57 58 0 | |||
59 L | |||
60 61 0 5 0 2 4 4 68 69 1 2 1 6 7 6 74 '50 5 2 7 7 7 80 EVENT DESCRIPTION gg During normal rounds operator noticed liquid coming through insulation on 2" letdown 7 8 9 80 tOQ3) diversion line ~ Upon return to steady state letdown condition, line was isolated ~ | |||
7 89 80 (Reportable Occurrence 76-27, 30-day) . | |||
7 8 9 80 toom 7 8 9 80 tm 7 8 9 PA VIE 80 | |||
. SYSTEM CAUSE COMPONENT COMPONENT CODE CODE COMPONENT CODE SUPPUER MANUFACTURER VGIATION | |||
[ocvj ~CG B P I P B X X ~N B 1 3 0 N 7 8 9 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION A pinhole leak was found fn socket weld between pipe and elbow. Weld was built up 7 8 9 80 | |||
~09 in area of leak, and a visual inspection performed upon return of system to service ver 7 8 9 80 Q~g ified leak was stopped. This section of line was (cont'd. under Additional Factors) 7 89 80 FACILITY METHOD OF STATUS % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION gg8 7 9 B ~io 10 o | |||
12 13 NA 44 b | |||
45 46 0 erator makin rounds FORM OF | |||
. 80 AMOUNT OF ACTIVITY LOCATION OF RELEASE 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES 7 89 11 12 13 80 PEFISONNEL INJURIES NUMBER DESCRIPTION | |||
~4 ~oo o NA 7 8 9 . 11 12 80 OFFSITE CONSEQUENCES NA 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION | |||
~16 NA 7 89 10 80 PUBLICITY 7 89 80 ADDITIONAL FACTORS | |||
[J>QB (cont'd. from Cause Description) replaced during refueling shutdown to remove weld 7 89 80 Qg 7 89 which had been leaking. CAR llllwas issued to document this corrective action. | |||
80 NAME: ames Witte/D. Hamelink pgONE', 7 1 6/546-2 700, ext. 29 1 -2 1 5 GPO 661 6 61 | |||
~ . g~ 4 ~ | |||
1 | |||
'P | |||
/ | |||
~ v h | |||
~ l e LER 76-30/30 UDdate Report Previous Report Date 1/12/77 CONTROL BLOCK | |||
~ ICENSEE EVENT REPORT fPLEAGE PRINT ALL RECIUIRED INFORMATION) 1 6 UCENSEE LICENSE EVENT NAME LICENSE NUMBEA TYPE 'TYPE Qg09 N Y R E G 1 0 0 0 0 0 4 LBO~J | |||
~ | |||
7 14 15 25 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE AEPOAT DATE | |||
~cl cowl 0 L 0 5 0 0 2 4 4 1 2 1 7 7 0 5 2 7 7 7 7 8 57 58 59 60 61 68 69 74 75 80 I | |||
EVENT DESCRIPTION During normal rounds an operator discovered liquid leaking from the "A" mixed bed 7 8 9 80 demineralizer inlet pipe . (Reportable Occurrence 76-30, 30-day) . | |||
7 09 80 t00j4 7 8 9 80 Jog 7 0 9 80 | |||
[0DQ 7 09 PAVE 80 SYSTEM CAUSE COMPONENT COMPONENT MANUFACTUREA | |||
~IB CODE CODE COMPONENT CODE SUPPUER VIOIATKIN tocC>~ILcGCa P I P E x x N B 1 3 0 N 7 8 9 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION Q~g Pinhole leak in weld between pipe and elbow. Hole was ground out and repaired using 7 0 9 80 | |||
[pgg] proper welding procedure. The piping was visually inspected for leakage after return 7 8 9 80 Q~g to service. CAR 1114 was issued for this event. | |||
7 89 METHOD OF 80 FACILITY STATUS POWER OTHER STATUS DISCOVERY ~ DISCOVERY DESCRIPTION 7 | |||
Eg 0 | |||
LEJ 9 | |||
~io 10 o | |||
12 13 NA 44 45 b | |||
46 0 erator makin rounds FOAM OF 80 ACTIVITY COATENT AELEASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE Qg H sj NA 7 8 9 10 11 44 45 00 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Pg~oo 7 8 9 o B 12 13 NA 11 80 PERSONNEL INJURIES NUMBER DESCRIPTION fig ~00 0 NA 7 09 ~ | |||
11 12 80 OFFSITE CONSEQUENCES Qg NA 7 09 00 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION Q~g s 7 09 10 80 PUBLICITY Q~~] ~ e ~ i +II'lI Ej | |||
$ Pl, 7 89 80 ADDITIONAL FACTORS l,lJ ~ | |||
NA 7 89 80 7 09 80 NAME: , Dave Hamelink PHDNL.". | |||
- | |||
7 1 6/5 4 6 2 7 0 0, ex t ~ | |||
- | |||
29 1 2 15 GPO 8 | |||
\ ~ | |||
) f | |||
<~a g -. | |||
ee), | |||
~IPIQ g | |||
( | |||
~~~~~"~~0 0~3~~~~~ | |||
03A)zygo}} | |||
Revision as of 02:23, 21 October 2019
ML18142B229 | |
Person / Time | |
---|---|
Site: | Ginna |
Issue date: | 05/27/1977 |
From: | White L Rochester Gas & Electric Corp |
To: | O'Reilly J NRC/IE, NRC Region 1 |
References | |
LER 1976-027-03 | |
Download: ML18142B229 (8) | |
Text
~ U.S. NUCLEAR REGULATORY COMMISSION DOCKET NUMBER FILE NUMBER NRC DISTRI8UTION FDR PART 50 DOCKET MATERIAL INCIDENT REPORT FROM:ROCHESTER GAS & ELEC. CORP. DATE OF J.P.O'REXLLY, DOCUMENT'ATE ROCHESTER, N.Y.
'L.D. WHITE, JR. ~ RECEIVED Q LETTE R ONOTOAIZED PROP INPUT FOAM NUMBER OF COPIES RECEIVED QOAIGINAL EBUNCLASSIFIED K)CO> Y DESCAIPTION ENCLOSURE 1'TR'RANS THE FOLLOWXNG UBDATE LICENSEE EVENT REPORT /f 76-27, 30 DAY ON 12/16/76 CONCERNING LIQUID COMING THROUGH INSULA ION ON 2" LE'ZDOWN DIVERSION LINE.......
I:. ~
UPDATE LICENSEE EVQP REPORT 1/ 76-30, 30 DAY ON (1P) . 12/17/76. CONCERNIg+LXQUPJ"%EARP, FROM THE "A" MIXED. BED SEMINERAL'IZQR I%K'ET~~QIg M k4I II';I)K:
PLANT NAME' E GINNA 4/
I" SAB NOTE ~ IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/Jo COLLINS FOR ACTION/INFOFIMATI ON
'RANCH CHIEF!
W 3 CYS FOR ACTION LIC, ASST'!
W /CYS ACRS / CYS 14Ch5%NG S NT INTERNAL DISTRI BUTION
'NRC PDR MIPC
~ SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES BUTLER IIANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS EANAL DISTRIBUTION CON OL NUMBER LPDR:
TIC:
71540052 NAC FORM 105 I2.ld)
o
~ o o ~ ~
~ ~ ~ o ~ o a ~
o g Io ll
,
'gV o o ~ o ~ o ~ ~
oo I
~)II~
r Qg rake PI ~
~ 0 ~
'iI'4'"7/ "'"PW Pi i't.i<IL'/74Ii W'"W ROCHESTER GAS AND ELECTRIC CORPORATlON 89 EAST AVENUE, ROCHESTER,, N.Y. 14649 LEON D. WHITE. JR. TCLCPNONC VICC PACSIDCNT iPCi CONC TIO 54G 2700 May 27, 1977 r
Mr. James P O'Reilly, Director
~
8 > ge 'Ctt U. S. Nuclear Regulatory Commis%%8 g UN 2 3977~
Office of inspection and Enforcement Region I
'EI re' ~I g..S. IIIIC'C">RUU5h5kV
>Ncll54rtbe 63 1 Park Avenue King of Prussia, Pennsylvania 19406
Subject:
Supplemental reports on Reportable Occurrences:
76-27 (30-day report) Leak in letdown diversion line 76-30 (30-day report) "A" mixed bed demineralizer inlet piping leak R. E. Qinna Nuclear Power Plant, Unit No. 1 Docket No. 50-244
Dear Mr. O'Reilly:
The purpose of this letter is to provide you with corrected component manufacturer information in connection with the subject reports which were submitted January 4 and January 12, 1977 respectively. The attached update reports LER 76-27/30 and LER 76-30/30 provide this information.
Two additional copies of this letter and the attachments are enclosed to conform to the original submittal of LER 76-27/3L and LER 76-30/3L.
Very truly yours, L. D. White Jr.
cc: Dr. Ernst Volgenau (30)
Mr. William G. McDonald (3)
.77g540052.
ao
~4
~ \
J I
I" '
d
$
LER 76-27/30 Update Report Previous Report Date 1/4/77 CONTROL BLOCK:
Q.IOENSEE EVENT REPORT
+
fPLEASE PAINT ALL REQVIREO IiNFORIViATION)
LICENSEE UCENSE EVENT NAME UCENSE NUMBER TYPE TYPE
[op~j N Y R B G 1 0 0 0 0 0 0 0 0 0 O 1 1 1' ~03
~
7 89 14 15 25 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE REPORT DATE 0
7
[oO~]corn 8 57 58 0
59 L
60 61 0 5 0 2 4 4 68 69 1 2 1 6 7 6 74 '50 5 2 7 7 7 80 EVENT DESCRIPTION gg During normal rounds operator noticed liquid coming through insulation on 2" letdown 7 8 9 80 tOQ3) diversion line ~ Upon return to steady state letdown condition, line was isolated ~
7 89 80 (Reportable Occurrence 76-27, 30-day) .
7 8 9 80 toom 7 8 9 80 tm 7 8 9 PA VIE 80
. SYSTEM CAUSE COMPONENT COMPONENT CODE CODE COMPONENT CODE SUPPUER MANUFACTURER VGIATION
[ocvj ~CG B P I P B X X ~N B 1 3 0 N 7 8 9 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION A pinhole leak was found fn socket weld between pipe and elbow. Weld was built up 7 8 9 80
~09 in area of leak, and a visual inspection performed upon return of system to service ver 7 8 9 80 Q~g ified leak was stopped. This section of line was (cont'd. under Additional Factors) 7 89 80 FACILITY METHOD OF STATUS % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION gg8 7 9 B ~io 10 o
12 13 NA 44 b
45 46 0 erator makin rounds FORM OF
. 80 AMOUNT OF ACTIVITY LOCATION OF RELEASE 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES 7 89 11 12 13 80 PEFISONNEL INJURIES NUMBER DESCRIPTION
~4 ~oo o NA 7 8 9 . 11 12 80 OFFSITE CONSEQUENCES NA 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION
~16 NA 7 89 10 80 PUBLICITY 7 89 80 ADDITIONAL FACTORS
[J>QB (cont'd. from Cause Description) replaced during refueling shutdown to remove weld 7 89 80 Qg 7 89 which had been leaking. CAR llllwas issued to document this corrective action.
80 NAME: ames Witte/D. Hamelink pgONE', 7 1 6/546-2 700, ext. 29 1 -2 1 5 GPO 661 6 61
~ . g~ 4 ~
1
'P
/
~ v h
~ l e LER 76-30/30 UDdate Report Previous Report Date 1/12/77 CONTROL BLOCK
~ ICENSEE EVENT REPORT fPLEAGE PRINT ALL RECIUIRED INFORMATION) 1 6 UCENSEE LICENSE EVENT NAME LICENSE NUMBEA TYPE 'TYPE Qg09 N Y R E G 1 0 0 0 0 0 4 LBO~J
~
7 14 15 25 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE AEPOAT DATE
~cl cowl 0 L 0 5 0 0 2 4 4 1 2 1 7 7 0 5 2 7 7 7 7 8 57 58 59 60 61 68 69 74 75 80 I
EVENT DESCRIPTION During normal rounds an operator discovered liquid leaking from the "A" mixed bed 7 8 9 80 demineralizer inlet pipe . (Reportable Occurrence 76-30, 30-day) .
7 09 80 t00j4 7 8 9 80 Jog 7 0 9 80
[0DQ 7 09 PAVE 80 SYSTEM CAUSE COMPONENT COMPONENT MANUFACTUREA
~IB CODE CODE COMPONENT CODE SUPPUER VIOIATKIN tocC>~ILcGCa P I P E x x N B 1 3 0 N 7 8 9 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION Q~g Pinhole leak in weld between pipe and elbow. Hole was ground out and repaired using 7 0 9 80
[pgg] proper welding procedure. The piping was visually inspected for leakage after return 7 8 9 80 Q~g to service. CAR 1114 was issued for this event.
7 89 METHOD OF 80 FACILITY STATUS POWER OTHER STATUS DISCOVERY ~ DISCOVERY DESCRIPTION 7
Eg 0
LEJ 9
~io 10 o
12 13 NA 44 45 b
46 0 erator makin rounds FOAM OF 80 ACTIVITY COATENT AELEASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE Qg H sj NA 7 8 9 10 11 44 45 00 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Pg~oo 7 8 9 o B 12 13 NA 11 80 PERSONNEL INJURIES NUMBER DESCRIPTION fig ~00 0 NA 7 09 ~
11 12 80 OFFSITE CONSEQUENCES Qg NA 7 09 00 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION Q~g s 7 09 10 80 PUBLICITY Q~~] ~ e ~ i +II'lI Ej
$ Pl, 7 89 80 ADDITIONAL FACTORS l,lJ ~
NA 7 89 80 7 09 80 NAME: , Dave Hamelink PHDNL.".
-
7 1 6/5 4 6 2 7 0 0, ex t ~
-
29 1 2 15 GPO 8
\ ~
) f
<~a g -.
ee),
~IPIQ g
(
~~~~~"~~0 0~3~~~~~
03A)zygo