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{{#Wiki_filter:...U.S. NUCLEAR REGULATORY C NRC FORM 366
{{#Wiki_filter:.       ..
;7 77)LICENSEE EVENT REPORT
U.S. NUCLEAR REGULATORY C NRC FORM 366
~CONTROL BLOCK: l llllll(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
    ;7 77)
.6l 0 l H l D l B l S l 1 l@l 0 l 0 l- l 0 l 0 l N l P l F l- l0 l 3 g[4 l1 11 l1 l 1 g lAT 58lg 1 25 26 LICENs TYPE JO 57 C to 1 LICENSE NUMBEM 8 9 LICENSEE CODE 14 15 0 l- l 0 l 3 l 4 l 6 g 1 l 0 l 2 [ 3.l 7 l 9 )@l1 l 1 l 2 l 0 l 7 l 9 j@
                              ~
CON'T So7R] l L lgl 0 l 5 l
LICENSEE EVENT REPORT
"'14 75 PEPORT DATE 80'O 1 6d 69 EVENT DATE 60 61 DOCKET NUYdER
                  .
*7 8 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES hit was found by observation of seal cavity pressure that
l    l      l    l    l      l                   (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
;l o l 2 l l 0n 10/23/79 at 0440 hours, The reactorg l the first and third seals in Reactor Coolant Pump 1-1-1 were not staging.
CONTROL BLOCK: l 1
o 3 This placed the unit in the l power was reduced, and the pump removed from service.
6 to          1 l 0 l H l D l B l S l 1 l@l 0 l 0 l- l 0 l 0 l N l P l F l-25 l0 26l 3 g[4                                               LICENsl1TYPE 11 JOl1 l 1   glAT 58lg 57 C 14    15                      LICENSE NUMBEM 8 9           LICENSEE CODE CON'T
i o 4 A flux-flow trip; l Action Statement of T.S. 3.4.1 which requires the high flux and flux-
      'O          1
_o s There was no danger to the g- l o is l l setpoints be reduced to $78.3% of rated thermal power.
                                "'
_The other three reactor coolantg l o ) 7 ) l health and safety of the public or station personnel.
So7R]        l L lgl 0 l 5 l 0 l- l 0 l 3 l 4 l 6 g 1 l 0 l 2 [ 3.l 7 l 9 14)@l1 l 1PEPORT              75 l 2 lDATE 0 l 7 l 80 9 j@
the reduced power level.(NP-33-79-120) g- iOisjl pumps provide adequate circulation at 80 7 8 9 C OE CO E SLBC DE COVPONENT CODE SLBC dE SU E}[Tl9]l Cl Bl@ y@ l Xl @ l Pl Ul Ml Pl Xl Xl Q l Xl g ] Q 18 19 20 7 8 9 to 11 12 13 REVISION OCCURRENCE REPORT SEQUE NTI AL CODE TYPE N REPORT No.
6d     69       EVENT DATE
@ y"LER SO l 7l 9l_1l3lyl 0l 3llLlj ._lU EVENT YE AR U(,C mT E_ 21 22 23 24 26 27 28 29 30 31 32 E K N AC ON oN PL ANT*E T HOURS S 8 IT D FOR B.SUPPLIE MAN FACT RER LA._J@l z l@
* 7              8                    60             61               DOCKET NUYdER EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES hit was found by observa                                                                                          ;
LA_J@I A I@10 I3 16 'o I U@lyl@Nl@lW l1 l2 0lg 33 34 3a 36 3/40 di 42 43 44 47 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h
l o l 2 l l 0n 10/23/79 at 0440 hours, The reactorg o        3 l the first and third seals in Reactor Coolant Pump 1-1-1 were not staging.
'- J i g o l lThe seal failure is attributed to thermal shocking which occurred during the loss of off-simultaneous loss of compon j 10/15/79 during which there was 1- 1i li j i site power incident on stage seal f aces were severely damaged,[First LL j n J l ent cooling water and seal injection.
This placed the unit in the i          o      4      l power was reduced, and the pump removed from service.
Under Maintenance g_ [TTTl I second stage f aces were cracked, and the third was not damaged.
A flux-flow trip; o      s    l Action Statement of T.S. 3.4.1 which requires the high flux and flux-
lthe seal package was refurbished and reinstalled.
_
i i I A 1 1 Work Order 79-3340.
There was no danger to the                   g
80 7 8 9 DISCOVERY DESCRIPTION STA% POWER oTHER STATUS IS O RYl Al@lOperator observation l~ Q (_Ej@ l 0 l 6 l 9 l@l NA Ab1VITY Co TENT LOCATION oF RELEASE RELE Aseo cF RELE AsE AuOuNT OF ACTIVITY lb d @ l Z]@l NA llNA 80 44 45)8 9 10 ff PERSONNEL EXPOSURES NUY8ER TYPE DE SCRIPTION 81 el el Ol@lz l-@l NA 8'' ''''2''PERSONNELiN3URiES DESCRtPTION@
- l o is l l setpoints be reduced to $78.3% of rated thermal power.
1 NUUBER~E l el of ol@l NA 80 7 8 9 11 12 i DQ I LOSS OF OR DAYAGE TO FACILITY
_
'.TYPE DESCRIP flON 8 LzJ@l NA 80 7 8 9 to""" g PTIM@7g}1g7Q I M(l I11IIIIiiiItI:
The other three reactor coolantg l o ) 7 ) l health and safety of the public or station personnel.
-I.tlaJ L.31@DE 1%UE l x^68 69 60. &W-N4M, M. M
the reduced power level.                   (NP-33-79-120)                   g
{7 8 9 10 John P. Hartigan pgggg DVR 79-157 N AME OF PREPARER _  
- iOisjl pumps provide adequate circulation at                                                                                                                                           80 7             8 9 COVPONENT CODE                SLBC dE        SU    E C OE                 CO E           SLBC DE
. -_TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-120 DATE OF EVENT: October 23, 1979 FACILITY: Davis-Besse Unit 1 J IDENTIFICATION OF OCCURRENCE: Reactor Coolant Pump 1-1 seal failure Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MRT) = 1925, and Load (Gross MWE) = 645.
  }[Tl9]                                         l Cl Bl@ y@ l Xl @ l Pl Ul Ml Pl Xl Xl Q l Xl g ] Q 12            13 18         19             20 REVISION 9           to           11                                                                       REPORT 7            8                                                                      SEQUE NTI AL                     OCCURRENCE                                      N CODE             TYPE
Description of Occurrence:
                          @ y"LER EVENT YE AR l 7l     9l REPORT No.
On October 23,1979 at 0100 hours, it was found by observing cavity pressure that the first and third shaf t seals in Reactor Coolant Pump (RCP) 1-1-1 were not staging. As a precautionary measure, the reactor power was reduced to 70% and RCP l-1-1 was removed from service. This placed the unit in the Action Statement of Technical Specification 3.4.1 which requires the thermal power be reduced and the high flux and flux- /1 flux . flow trip setpoints be reduced to f!78.3% of rated thermal power. The flux- 6 flux-flow trip setpoint was reduced to 77.5% of rated power at 0519 hours on October 23, 1979." Designation of Apparent Cause of Occurrence: On disassembly of the seal package, it was noted that the first stage seal faces were severely damaged, the second stage faces were cracked, and the third stage faces were not damaged. The middle pressure breakdown device tubing was found plugged with seal material which explains the observed low third stage cavity pressure.
1l      3l        y            l 0l 3l              lLl          j ._l      U U(,C mTSO
The failure can be attributed to the simultaneous loss of component cooling water and seal injection during the loss of offsite power incident on October 15,1979 (see Licensea Event Report NP-32-79-11) .
_
There was also some thermal shocking of the seals when the makeup pump section was changed over from the makeup tank to the Borated Water Storage Tank during the same trip.Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. The other three reactor coolant pumps were in operation providing adequate circulation at the reduced reactor power level.
E 30            31        32 26       27           28       29 E
Corrective Action: On October 26, 1979, the maintenance outage began to permit seal repairs. Under Maintenance Work Order- 79-3340, the seal package was refurbished and reinstalled. The seals on the other three pumps were also rebuilt.
22          23              24
Station personnel and Babcock and Wilcox are investigating possible methods to minimize thermal shocking.
_ 21 B. SUPPLIE          MAN FACT RER oN PL ANT             *E T                     HOURS           S 8 IT D       FOR lW l1 l2 0lg K N AC ON LA._J@l           z l@ LA_J@       3a I36A I@ 3/10 I3 16 'o 40I di              U@             lyl@
This is the fif th time that seals have been replaced in RCP l-1-1.
42              43 Nl@       44            47 33         34 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h
Failure Data:
'- J i g o l lThe seal failure is attributed to thermal shocking which occurred during the simultaneous loss of compon j
  - 1i li j i site power incident on 10/15/79 during which there was 1 First      stage seal f aces were severely damaged,                           [
LL j n J l ent cooling water and seal injection.
Under Maintenance               g
_ [TTTl I second stage f aces were cracked, and the third was not damaged.
l the seal package was refurbished and reinstalled.                                                           80 i i I A 1 1 Work Order 79-3340.
7         8 9                                                                                                                       DISCOVERY DESCRIPTION IS O RY STA                   % POWER                           oTHER STATUS Operator observation                                         l
  ~ Q (_Ej@ l 0 l 6 l 9 l@l NA                                                                                   l Al@l Ab1VITY Co TENT                                                                                                       LOCATION oF RELEASE RELE Aseo cF RELE AsE                         AuOuNT OF ACTIVITY                                                                                                   l l    NA l
b d8 @
              )            9 l Z]@l NA10            ff 44           45 80 PERSONNEL EXPOSURES NUY8ER               TYPE           DE SCRIPTION 8
81
              '
el
                        ' '
el Ol@lz l-@l NA''     '2             ''
PERSONNELiN3URiES
~
NUUBER              DESCRtPTION@                                                                                                                             1 E l 8el9 of ol@l 7                               11       12 NA                                                                                                                        80 LOSS OF OR DAYAGE TO FACILITY                                                                                                                   '       .
TYPE       DESCRIP flON                                                                                                             i DQ                          I 8 LzJ@l 7         8 9           to NA
                                                                                                                                                                        ""         "
80 g
1%UE                  PTIM@                                                               7g}1g7Q I M(                         l     I11IIIIiiiItI:
I.tlaJ8 9L.31@DE           l x^                                                                                                               68 69                           60. &
-
7                          10                                                                                                              W-N4M, M. M                             {
John P. Hartigan                                 pgggg DVR 79-157                 N AME OF PREPARER _
 
_
    . -
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-120 DATE OF EVENT: October 23, 1979 FACILITY: Davis-Besse Unit 1 J
IDENTIFICATION OF OCCURRENCE: Reactor Coolant Pump 1-1 seal failure Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MRT) = 1925, and Load (Gross MWE) = 645.
Description of Occurrence:     On October 23,1979 at 0100 hours, it was found by observing cavity pressure that the first and third shaf t seals in Reactor Coolant Pump (RCP) 1-1-1 were not staging. As a precautionary measure, the reactor power was reduced to 70% and RCP l-1-1 was removed from service. This placed the unit in the Action Statement of Technical Specification 3.4.1 which requires the thermal power be reduced and the high flux and flux- /1 flux . flow trip setpoints be reduced to f!78.3% of rated thermal power. The flux- 6 flux-flow trip setpoint was reduced to 77.5% of rated power at 0519 hours on October 23, 1979.
      " Designation of Apparent Cause of Occurrence: On disassembly of the seal package, it was noted that the first stage seal faces were severely damaged, the second stage faces were cracked, and the third stage faces were not damaged. The middle pressure breakdown device tubing was found plugged with seal material which explains the observed low third stage cavity pressure.       The failure can be attributed to the simultaneous loss of component cooling water and seal injection during the loss of offsite power incident on October 15,1979 (see Licensea Event Report NP-32-79-11) .
There was also some thermal shocking of the seals when the makeup pump section was changed over from the makeup tank to the Borated Water Storage Tank during the same trip.
Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. The other three reactor coolant pumps were in operation providing adequate circulation at the reduced reactor power level.
Corrective Action: On October 26, 1979, the maintenance outage began to permit seal repairs. Under Maintenance Work Order- 79-3340, the seal package was Station refurbished and personnel reinstalled. The seals on the other three pumps were also rebuilt.
and Babcock and Wilcox are investigating possible methods to minimize thermal shocking.
Failure Data:  This is the fif th time that seals have been replaced in RCP l-1-1.
LER #79-103 1398 078}}
LER #79-103 1398 078}}

Revision as of 13:32, 19 October 2019

LER 79-103/03L-0:on 791023,first & Third Seals in Reactor Coolant Pump 1-1-1 Were Not Staging.Caused by Thermal Shocking Which Occurred During Loss of Offsite Power on 791015.Seal Package Refurbished & Reinstalled
ML19210D671
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 11/20/1979
From: Hartigan J
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19210D666 List:
References
LER-79-103-03L, LER-79-103-3L, NUDOCS 7911270441
Download: ML19210D671 (2)


Text

. ..

U.S. NUCLEAR REGULATORY C NRC FORM 366

7 77)

~

LICENSEE EVENT REPORT

.

l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

CONTROL BLOCK: l 1

6 to 1 l 0 l H l D l B l S l 1 l@l 0 l 0 l- l 0 l 0 l N l P l F l-25 l0 26l 3 g[4 LICENsl1TYPE 11 JOl1 l 1 glAT 58lg 57 C 14 15 LICENSE NUMBEM 8 9 LICENSEE CODE CON'T

'O 1

"'

So7R] l L lgl 0 l 5 l 0 l- l 0 l 3 l 4 l 6 g 1 l 0 l 2 [ 3.l 7 l 9 14)@l1 l 1PEPORT 75 l 2 lDATE 0 l 7 l 80 9 j@

6d 69 EVENT DATE

  • 7 8 60 61 DOCKET NUYdER EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES hit was found by observa  ;

l o l 2 l l 0n 10/23/79 at 0440 hours0.00509 days <br />0.122 hours <br />7.275132e-4 weeks <br />1.6742e-4 months <br />, The reactorg o 3 l the first and third seals in Reactor Coolant Pump 1-1-1 were not staging.

This placed the unit in the i o 4 l power was reduced, and the pump removed from service.

A flux-flow trip; o s l Action Statement of T.S. 3.4.1 which requires the high flux and flux-

_

There was no danger to the g

- l o is l l setpoints be reduced to $78.3% of rated thermal power.

_

The other three reactor coolantg l o ) 7 ) l health and safety of the public or station personnel.

the reduced power level. (NP-33-79-120) g

- iOisjl pumps provide adequate circulation at 80 7 8 9 COVPONENT CODE SLBC dE SU E C OE CO E SLBC DE

}[Tl9] l Cl Bl@ y@ l Xl @ l Pl Ul Ml Pl Xl Xl Q l Xl g ] Q 12 13 18 19 20 REVISION 9 to 11 REPORT 7 8 SEQUE NTI AL OCCURRENCE N CODE TYPE

@ y"LER EVENT YE AR l 7l 9l REPORT No.

1l 3l y l 0l 3l lLl j ._l U U(,C mTSO

_

E 30 31 32 26 27 28 29 E

22 23 24

_ 21 B. SUPPLIE MAN FACT RER oN PL ANT *E T HOURS S 8 IT D FOR lW l1 l2 0lg K N AC ON LA._J@l z l@ LA_J@ 3a I36A I@ 3/10 I3 16 'o 40I di U@ lyl@

42 43 Nl@ 44 47 33 34 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS h

'- J i g o l lThe seal failure is attributed to thermal shocking which occurred during the simultaneous loss of compon j

- 1i li j i site power incident on 10/15/79 during which there was 1 First stage seal f aces were severely damaged, [

LL j n J l ent cooling water and seal injection.

Under Maintenance g

_ [TTTl I second stage f aces were cracked, and the third was not damaged.

l the seal package was refurbished and reinstalled. 80 i i I A 1 1 Work Order 79-3340.

7 8 9 DISCOVERY DESCRIPTION IS O RY STA  % POWER oTHER STATUS Operator observation l

~ Q (_Ej@ l 0 l 6 l 9 l@l NA l Al@l Ab1VITY Co TENT LOCATION oF RELEASE RELE Aseo cF RELE AsE AuOuNT OF ACTIVITY l l NA l

b d8 @

) 9 l Z]@l NA10 ff 44 45 80 PERSONNEL EXPOSURES NUY8ER TYPE DE SCRIPTION 8

81

'

el

' '

el Ol@lz l-@l NA '2

PERSONNELiN3URiES

~

NUUBER DESCRtPTION@ 1 E l 8el9 of ol@l 7 11 12 NA 80 LOSS OF OR DAYAGE TO FACILITY ' .

TYPE DESCRIP flON i DQ I 8 LzJ@l 7 8 9 to NA

"" "

80 g

1%UE PTIM@ 7g}1g7Q I M( l I11IIIIiiiItI:

I.tlaJ8 9L.31@DE l x^ 68 69 60. &

-

7 10 W-N4M, M. M {

John P. Hartigan pgggg DVR 79-157 N AME OF PREPARER _

_

. -

TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-120 DATE OF EVENT: October 23, 1979 FACILITY: Davis-Besse Unit 1 J

IDENTIFICATION OF OCCURRENCE: Reactor Coolant Pump 1-1 seal failure Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MRT) = 1925, and Load (Gross MWE) = 645.

Description of Occurrence: On October 23,1979 at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, it was found by observing cavity pressure that the first and third shaf t seals in Reactor Coolant Pump (RCP) 1-1-1 were not staging. As a precautionary measure, the reactor power was reduced to 70% and RCP l-1-1 was removed from service. This placed the unit in the Action Statement of Technical Specification 3.4.1 which requires the thermal power be reduced and the high flux and flux- /1 flux . flow trip setpoints be reduced to f!78.3% of rated thermal power. The flux- 6 flux-flow trip setpoint was reduced to 77.5% of rated power at 0519 hours0.00601 days <br />0.144 hours <br />8.581349e-4 weeks <br />1.974795e-4 months <br /> on October 23, 1979.

" Designation of Apparent Cause of Occurrence: On disassembly of the seal package, it was noted that the first stage seal faces were severely damaged, the second stage faces were cracked, and the third stage faces were not damaged. The middle pressure breakdown device tubing was found plugged with seal material which explains the observed low third stage cavity pressure. The failure can be attributed to the simultaneous loss of component cooling water and seal injection during the loss of offsite power incident on October 15,1979 (see Licensea Event Report NP-32-79-11) .

There was also some thermal shocking of the seals when the makeup pump section was changed over from the makeup tank to the Borated Water Storage Tank during the same trip.

Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. The other three reactor coolant pumps were in operation providing adequate circulation at the reduced reactor power level.

Corrective Action: On October 26, 1979, the maintenance outage began to permit seal repairs. Under Maintenance Work Order- 79-3340, the seal package was Station refurbished and personnel reinstalled. The seals on the other three pumps were also rebuilt.

and Babcock and Wilcox are investigating possible methods to minimize thermal shocking.

Failure Data: This is the fif th time that seals have been replaced in RCP l-1-1.

LER #79-103 1398 078