LER-1979-103, /03L-0:on 791023,first & Third Seals in Reactor Coolant Pump 1-1-1 Were Not Staging.Caused by Thermal Shocking Which Occurred During Loss of Offsite Power on 791015.Seal Package Refurbished & Reinstalled |
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U.S. NUCLEAR REGULATORY C NRC FORM 366
- 7 77)
LICENSEE EVENT REPORT
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CONTROL BLOCK: l l
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25 26 LICENs TYPE JO 57 C to 1
LICENSE NUMBEM 8 9 LICENSEE CODE 14 15 0 l-l 0 l 3 l 4 l 6 g 1 l 0 l 2 [ 3.l 7 l 9 )@l1 l 1 l 2 l 0 l 7 l 9 j@
CON'T So7R] l L lgl 0 l 5 l 14 75 PEPORT DATE 80
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6d 69 EVENT DATE 60 61 DOCKET NUYdER 7
8 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES hit was found by observa l o l 2 l l 0n 10/23/79 at 0440 hours0.00509 days <br />0.122 hours <br />7.275132e-4 weeks <br />1.6742e-4 months <br />, The reactorg l the first and third seals in Reactor Coolant Pump 1-1-1 were not staging.
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This placed the unit in the l power was reduced, and the pump removed from service.
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4 A flux-flow trip; l Action Statement of T.S. 3.4.1 which requires the high flux and flux-o s
There was no danger to the g
- - l o is l l setpoints be reduced to $78.3% of rated thermal power.
The other three reactor coolantg l o ) 7 ) l health and safety of the public or station personnel.
the reduced power level.
(NP-33-79-120) g
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REPORT No.
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'- J i g o l lThe seal failure is attributed to thermal shocking which occurred during the simultaneous loss of compon j 10/15/79 during which there was 1
- - 1i li j i site power incident on stage seal f aces were severely damaged,
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First LL j n J l ent cooling water and seal injection.
Under Maintenance g
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l the seal package was refurbished and reinstalled.
i i I A 1 1 Work Order 79-3340.
80 7
8 9 DISCOVERY DESCRIPTION STA
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TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-120 DATE OF EVENT: October 23, 1979 FACILITY: Davis-Besse Unit 1 J
IDENTIFICATION OF OCCURRENCE: Reactor Coolant Pump 1-1 seal failure Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MRT) = 1925, and Load (Gross MWE) = 645.
Description of Occurrence:
On October 23,1979 at 0100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br />, it was found by observing cavity pressure that the first and third shaf t seals in Reactor Coolant Pump (RCP) 1-1-1 were not staging. As a precautionary measure, the reactor power was reduced to 70% and RCP l-1-1 was removed from service. This placed the unit in the Action Statement of Technical Specification 3.4.1 which requires the thermal power be reduced and the high flux and flux- /1 flux. flow trip setpoints be reduced to f!78.3% of rated thermal power. The flux-6 flux-flow trip setpoint was reduced to 77.5% of rated power at 0519 hours0.00601 days <br />0.144 hours <br />8.581349e-4 weeks <br />1.974795e-4 months <br /> on October 23, 1979.
" Designation of Apparent Cause of Occurrence: On disassembly of the seal package, it was noted that the first stage seal faces were severely damaged, the second stage faces were cracked, and the third stage faces were not damaged. The middle pressure breakdown device tubing was found plugged with seal material which explains the observed low third stage cavity pressure.
The failure can be attributed to the simultaneous loss of component cooling water and seal injection during the loss of offsite power incident on October 15,1979 (see Licensea Event Report NP-32-79-11).
There was also some thermal shocking of the seals when the makeup pump section was changed over from the makeup tank to the Borated Water Storage Tank during the same trip.
Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. The other three reactor coolant pumps were in operation providing adequate circulation at the reduced reactor power level.
Corrective Action
On October 26, 1979, the maintenance outage began to permit seal repairs. Under Maintenance Work Order-79-3340, the seal package was refurbished and reinstalled. The seals on the other three pumps were also rebuilt.
Station personnel and Babcock and Wilcox are investigating possible methods to minimize thermal shocking.
This is the fif th time that seals have been replaced in RCP l-1-1.
Failure Data:
LER #79-103 1398 078
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| 05000346/LER-1979-001-03, /03L-0 on 790102:monthly Functional Test Not Performed on Reactor Protection Sys Channel 2 within Allowable Time.Caused by Breakdown in Communications Between Testing Personnel & Test Coordinator | /03L-0 on 790102:monthly Functional Test Not Performed on Reactor Protection Sys Channel 2 within Allowable Time.Caused by Breakdown in Communications Between Testing Personnel & Test Coordinator | | | 05000346/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000346/LER-1979-002-03, /03L-1 on 790102:main Steam Valves 106 & 106A Failed to Open,Resulting in Auxiliary Feed Pump Afp 1-1 Being Taken Out of Operation.Caused by Dirt Buildup on Valve Stems as Result of New Const | /03L-1 on 790102:main Steam Valves 106 & 106A Failed to Open,Resulting in Auxiliary Feed Pump Afp 1-1 Being Taken Out of Operation.Caused by Dirt Buildup on Valve Stems as Result of New Const | | | 05000346/LER-1979-002, Forwards LER 79-002/03L-1 | Forwards LER 79-002/03L-1 | | | 05000346/LER-1979-003-03, /03L-0 on 790104:control Room Emergency Ventilation Sys Damper HV5311E Inoperable.Caused by Leaking Pneumatic Operator.New Operator Installed.Damper Operated & Tested for Response Time & Declared Operable | /03L-0 on 790104:control Room Emergency Ventilation Sys Damper HV5311E Inoperable.Caused by Leaking Pneumatic Operator.New Operator Installed.Damper Operated & Tested for Response Time & Declared Operable | | | 05000346/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000346/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000346/LER-1979-004-03, /03L-0 on 790105:failure to Post Guards at Entrance to Containment During Periods of Free Access. Caused by Personnel Error.Special Order 84 Revised to Require Posting of Guards | /03L-0 on 790105:failure to Post Guards at Entrance to Containment During Periods of Free Access. Caused by Personnel Error.Special Order 84 Revised to Require Posting of Guards | | | 05000346/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000346/LER-1979-005-03, /03L-0 on 790106:during Surveillance Testing, Borated Water Storage Tank Level Bistable Was Tripped;Valves DH9A Opened & DH7A Closed.Caused by Component Failure of Output Relay K51A & Instrument Drift | /03L-0 on 790106:during Surveillance Testing, Borated Water Storage Tank Level Bistable Was Tripped;Valves DH9A Opened & DH7A Closed.Caused by Component Failure of Output Relay K51A & Instrument Drift | | | 05000346/LER-1979-006-03, /03L-0:on 790105,reviewer Noted 781228 Record of Continuous Alarm at Contact Data Record Point F018.Panel C4705 Not Reset.Caused by Failure of Indicator Lights on Panel C4705.Panel Reset,Clearing F018.Surveillance Modified | /03L-0:on 790105,reviewer Noted 781228 Record of Continuous Alarm at Contact Data Record Point F018.Panel C4705 Not Reset.Caused by Failure of Indicator Lights on Panel C4705.Panel Reset,Clearing F018.Surveillance Modified | | | 05000346/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000346/LER-1979-007-03, /03L-0 on 790110:during Performance of Surveillance Test,Channel 2 of Containment Hydrogen Analyzer Was Found Inoperable.Caused by Defective Zener Diode in Millivolt Converter | /03L-0 on 790110:during Performance of Surveillance Test,Channel 2 of Containment Hydrogen Analyzer Was Found Inoperable.Caused by Defective Zener Diode in Millivolt Converter | | | 05000346/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000346/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000346/LER-1979-008-03, /03L-0 on 790109:during Surveillance Testing, Containment Recirculation Fan 1-1 Failed to Run.Cause Attributed to Buildup of non-conductive Film on Auxiliary Controller Contacts | /03L-0 on 790109:during Surveillance Testing, Containment Recirculation Fan 1-1 Failed to Run.Cause Attributed to Buildup of non-conductive Film on Auxiliary Controller Contacts | | | 05000346/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000346/LER-1979-009-03, /03L-0:on 790112,power to Vital Bus Y2 Lost. False Integrated Control Sys Signal Resulted in Reactor & Full Steam & Feedwater Rupture Control Sys Trip.Caused by Blown 125 Volt DC Fuse to Inverter | /03L-0:on 790112,power to Vital Bus Y2 Lost. False Integrated Control Sys Signal Resulted in Reactor & Full Steam & Feedwater Rupture Control Sys Trip.Caused by Blown 125 Volt DC Fuse to Inverter | | | 05000346/LER-1979-010-03, /03L-0:on 790112,Sys 7 Data Logger Experienced Core Dump,Voiding Computer Memory Bank Which Rendered Remote Monitoring of Fire Detection Sys Inoperable & Placed Unit in Action Statement of Tech Spec 3.3.3.8.Cause Unknown | /03L-0:on 790112,Sys 7 Data Logger Experienced Core Dump,Voiding Computer Memory Bank Which Rendered Remote Monitoring of Fire Detection Sys Inoperable & Placed Unit in Action Statement of Tech Spec 3.3.3.8.Cause Unknown | | | 05000346/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000346/LER-1979-011-03, /03L-0:on 790115,reactor Coolant Pump 1-2-2 Started W/Incorrect Breaker Alignment,Causing Low Voltage Relays to Trip Which de-energized Both 4.16 Kv Essential Buses C1 & D1.Caused by Personnel Error | /03L-0:on 790115,reactor Coolant Pump 1-2-2 Started W/Incorrect Breaker Alignment,Causing Low Voltage Relays to Trip Which de-energized Both 4.16 Kv Essential Buses C1 & D1.Caused by Personnel Error | | | 05000346/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000346/LER-1979-012-03, /03L-0:on 790116,during Surveillance Testing,Heat Traced Line Temp Measurement Points Below 105 F Limit.Caused by Injection of Makeup (Flush) Water After Boron Injection at Temp Lower than 105 F.Tests Rerun Satisfactorily | /03L-0:on 790116,during Surveillance Testing,Heat Traced Line Temp Measurement Points Below 105 F Limit.Caused by Injection of Makeup (Flush) Water After Boron Injection at Temp Lower than 105 F.Tests Rerun Satisfactorily | | | 05000346/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000346/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000346/LER-1979-013-03, /03L-0:on 790116,when Makeup Pump 1 Started for Surveillance testing,1/2 Inch Nipple at Discharge of Attached Gear Driven Lube Oil Pump Failed,Resulting in Oil Spray Which Required Pump Shutdown | /03L-0:on 790116,when Makeup Pump 1 Started for Surveillance testing,1/2 Inch Nipple at Discharge of Attached Gear Driven Lube Oil Pump Failed,Resulting in Oil Spray Which Required Pump Shutdown | | | 05000346/LER-1979-014-03, /03L-0:on 790116,during Shutdown,Boric Acid Addition Tanks (Baat) Total Vol 3-1/3% Below Tech Spec 3.1.2.9 Requirements.Caused by Reduced Baat Vol After Completion of Required Testing Followed by RCS Boration | /03L-0:on 790116,during Shutdown,Boric Acid Addition Tanks (Baat) Total Vol 3-1/3% Below Tech Spec 3.1.2.9 Requirements.Caused by Reduced Baat Vol After Completion of Required Testing Followed by RCS Boration | | | 05000346/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000346/LER-1979-015-03, /03L-0:on 790117,core Flood Tank 1-2 Isolation Valve CF1A Would Not Close by Remote Operation.Caused by Loose Set Screw.Cracked Pinion Gear & Associated Key Replaced Per Maint Work Order 78-2928 | /03L-0:on 790117,core Flood Tank 1-2 Isolation Valve CF1A Would Not Close by Remote Operation.Caused by Loose Set Screw.Cracked Pinion Gear & Associated Key Replaced Per Maint Work Order 78-2928 | | | 05000346/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000346/LER-1979-016-03, /03L-0:on 790124,emergency Lock Failed Leak Rate Test While Unit in Mode 5.Caused by Loosening of Shaft Seal (Teflon Packing) Due to Routine Use of Escape Lock.Packing Will Be Replaced During Next Convenient Outage | /03L-0:on 790124,emergency Lock Failed Leak Rate Test While Unit in Mode 5.Caused by Loosening of Shaft Seal (Teflon Packing) Due to Routine Use of Escape Lock.Packing Will Be Replaced During Next Convenient Outage | | | 05000346/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000346/LER-1979-017-03, /03L-0:on 790130,photoelectric Smoke Detector Ds 8605-E in Emergency Diesel Generator 1-1 Area Not Functional.Caused by Failure of Detector.New Detector Ordered & Fire Watch Patrol Established in Area | /03L-0:on 790130,photoelectric Smoke Detector Ds 8605-E in Emergency Diesel Generator 1-1 Area Not Functional.Caused by Failure of Detector.New Detector Ordered & Fire Watch Patrol Established in Area | | | 05000346/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000346/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000346/LER-1979-018-03, /03L-0:on 790130,valves SP17A2 & SP17B2 Lifted Below Setpoint Range & Declared Inoperable.Caused by Loose Spindle on Main Steam Line Code Safety Valve SP17A2.Valve SP17A2 Gagged & SP17B2 Tested Satisfactorily | /03L-0:on 790130,valves SP17A2 & SP17B2 Lifted Below Setpoint Range & Declared Inoperable.Caused by Loose Spindle on Main Steam Line Code Safety Valve SP17A2.Valve SP17A2 Gagged & SP17B2 Tested Satisfactorily | | | 05000346/LER-1979-019-03, /03L-0 on 790129:suction & Discharge Valves on Containment Spray Pump Were Closed.Caused by Personnel Error | /03L-0 on 790129:suction & Discharge Valves on Containment Spray Pump Were Closed.Caused by Personnel Error | | | 05000346/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000346/LER-1979-020-03, /03L-0 on 790205:10 of 18 Main Steam Safety Valves Found Outside Setpoint Range.Believed Caused by Changing Ambient Conditions at Valve Locations.Valves Adjusted & Retested Satisfactorily | /03L-0 on 790205:10 of 18 Main Steam Safety Valves Found Outside Setpoint Range.Believed Caused by Changing Ambient Conditions at Valve Locations.Valves Adjusted & Retested Satisfactorily | | | 05000346/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000346/LER-1979-021-03, /03L-0 on 790205:containment High Pressure Alarms Were Received & Safety Features Actuation Sys Channel 2 Erroneously Tripped.Cause Unknown.No Deficiencies Found from Surveillance Tests.Channel Returned to Operation | /03L-0 on 790205:containment High Pressure Alarms Were Received & Safety Features Actuation Sys Channel 2 Erroneously Tripped.Cause Unknown.No Deficiencies Found from Surveillance Tests.Channel Returned to Operation | | | 05000346/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000346/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000346/LER-1979-022-03, /03L-0 on 790208:diesel Fire Pump Battery Electrolyte Level in Four Cells Was Below Top of Cell Plates.Caused by Procedural Error.Levels Restored,Pump Declared Operable & Unit Removed from Action Statement | /03L-0 on 790208:diesel Fire Pump Battery Electrolyte Level in Four Cells Was Below Top of Cell Plates.Caused by Procedural Error.Levels Restored,Pump Declared Operable & Unit Removed from Action Statement | | | 05000346/LER-1979-023, Forwards LER 79-023/01T-0 | Forwards LER 79-023/01T-0 | | | 05000346/LER-1979-023-01, /01T-0 on 790228:Startup Transformer 01 Taken Out of Svc;Surveillance Tests Not Performed within One Hour, Contrary to Tech Spec Requirements.Caused by Personnel Error.Testing Completed as Soon as Error Realized | /01T-0 on 790228:Startup Transformer 01 Taken Out of Svc;Surveillance Tests Not Performed within One Hour, Contrary to Tech Spec Requirements.Caused by Personnel Error.Testing Completed as Soon as Error Realized | | | 05000346/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000346/LER-1979-024-03, /03L-0 on 790214:fire Alarm Panel C4706 Signaled, Indicating Laundry Room Detector DS8630 as Source.Detector Declared Inoperable as No Cause for Signal Found.Cause of Event Undetermined.Possibly Due to Gases or Dust | /03L-0 on 790214:fire Alarm Panel C4706 Signaled, Indicating Laundry Room Detector DS8630 as Source.Detector Declared Inoperable as No Cause for Signal Found.Cause of Event Undetermined.Possibly Due to Gases or Dust | | | 05000346/LER-1979-025-03, /03L-0 on 790213:Ohio Edison Relay Testing Actuated Transfer Trip Receiving Relay & Tripped Switchyard Breakers.Caused by Failure of Util to Notify Toledo Edison Before Performing Relay Testing | /03L-0 on 790213:Ohio Edison Relay Testing Actuated Transfer Trip Receiving Relay & Tripped Switchyard Breakers.Caused by Failure of Util to Notify Toledo Edison Before Performing Relay Testing | | | 05000346/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | |
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