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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:RO)
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr ML18039A6031998-11-0404 November 1998 LER 98-004-00:on 981007,primary Containment Allowable Leak Rate Was Exceeded.Caused by Failure of Check Valve to Fully Seat Following Shutdown of Rbbccw Sys for Llrt.Valve Was Retested During Next Refueling Outage.With 981104 Ltr ML18039A5971998-10-28028 October 1998 LER 98-003-00:on 981001,Unit 2 Received Full Automatic Scram from 100% Reactor Power.Caused by Failure of Normally Open Isolation Valve Which Blocked Flow of Stator Cooling Water Through Associated Heat Exchangers.Replaced Failed Valve ML18039A5171998-09-15015 September 1998 LER 98-002-00:on 980816,personnel Observed Both Channels of Rod Block Monitor Sys Bypassed for Cr.Caused by Failure of Gene to Properly Document & Specify Adjustments.Will Implement Necessary Procedure Controls ML18039A3311998-05-0404 May 1998 LER 98-003-00:on 980407,reactor Manually Scrammed to Prevent thermal-hydraulic Instability After Recirculation Pump Runback.Caused by Human Error.Strengthened Controls Associated W/Walkdowns in NEDP-11 ML18039A3141998-04-0909 April 1998 LER 98-002-00:on 980310,ESF Actuation Occurred Due to Failure of Alternate Feeder Breaker Position Switch.Will Continue Testing & Visual Insps on Addl Breaker Position Switches & Will Revise Applicable Maint Instructions ML18039A3101998-04-0707 April 1998 LER 98-001-00:on 980308,ESF Actuations Occurred When 2B RPS Bus Was Transferred to de-energized Source.Caused by Failure of Preparing Clearance to Exercise Proper Attention. 2B RPS Bus Restored to Transformer Source ML18039A3051998-04-0101 April 1998 LER 96-001-00:on 980121,determined That Temp Sensors for Certain HELB May Not Detect All Possible Break Locations. Caused by Differences in Computer Codes Rather than Actual Response.Computer Code Correctly Utilized ML18039A2041997-12-0303 December 1997 LER 97-008-00:on 971104,main Steam Safety/Relief Valves Exceeded TS Setpoint Limit.Caused by Pilot Valve Disc/Seat Bonding.Replaced All 13 Unit 2 Main Steam SRV Pilot Cartridges ML18038B9961997-11-25025 November 1997 LER 97-007-00:on 971028,Unit 2 Automatically Scrammed.Caused by Momentary Pressure Drop in electro-hydraulic Control Sys at Turbine Control Valves.Scram Contactor Replaced ML18038B9931997-11-18018 November 1997 LER 97-006-00:on 971019,declared Unit 2 Hpcis Inoperable. Caused by High Condensate Level in HPCI Turbine Inlet Steam Line Drain Pot.Work Request Initiated ML18038B9861997-11-10010 November 1997 LER 97-005-00:on 971012,ESF Components Were Actuated.Caused by Inadequate Procedure.Cs Pumps Were Secured & Injection Valves Were Closed & Refueling Floor Activities Were Stopped ML18038B9701997-10-0909 October 1997 LER 97-004-00:on 970909,TS Surveillances Were Not Performed During Refueling Outage Timeframe.Caused by Personnel Error. Incorporated Missed Snubber & Vacuum Breaker Surveillances Into Refueling Outage Schedule ML18038B9661997-10-0303 October 1997 LER 97-005-00:on 970824,LCO Was Not Entered When Valve Was Malfunctioning.Caused by Lack of Questioning Attitude by Operations Crew.Involved SROs Were Counseled & Problem Evaluation Rept Will Be Discussed ML18038B9321997-08-0707 August 1997 LER 97-003-00:on 970711,determined That HPCI Turbine Speed Lower than Indicated.Caused by Improper Evaluation of Valve Leak.Work Orders to Troubleshoot HPCI Initiated ML18038B9231997-07-25025 July 1997 LER 97-002-00:on 970626,discovered That Four Surveillance Instructions (Sis) Did Not Fully Test All Relay Logic Combinations.Caused by Personnel Error.Verified Relay Contacts Operable & Revised Applicable SIs.W/970725 Ltr ML18038B8811997-05-14014 May 1997 LER 97-004-00:on 970414,unplanned Manual Start of EDG During Scheduled Redundant Start Test Occurred.Caused by Personnel Error.Edg 3D Shutdown & Returned to pre-event Configuration. W/970514 Ltr ML18038B8801997-05-0808 May 1997 LER 97-002-00:on 970410,HPCI Declared Inoperable.Caused by Personnel Error.Operations Personnel Stopped Instrument Mechanics Testing & Returned HPCI to Standby Readiness. W/970508 Ltr ML18038B8701997-04-29029 April 1997 LER 96-004-02:on 960717,loss of ECCS Division I & Division II Instrumentation Renders ECCS Equipment Inoperable.Caused by Loss of Inverter Output.Failed Components Replaced in Atu Inverter Circuitry & Instrumentation Logic Restored ML18038B8521997-04-0909 April 1997 LER 97-003-00:on 970314,Unit 3 Main Steam SRVs Pilot Cartridges Failed Setpoint Tolerance Bench Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Drifting.Main Steam SRV Pilot replaced.W/970409 Ltr ML18038B8511997-04-0909 April 1997 LER 95-003-02:on 950301,Unit 2 Main Steam SRVs Failed Setpoint Acceptance Tests.Caused by Corrosion Bonding of SRV Pilot Disc/Seat Interface Resulting in Upward Setpoint Drift.Valves Currently Being Retested & Recertified ML18038B8481997-04-0909 April 1997 LER 96-004-01:on 960425,Unit 2 SRV Pilot Cartridges Failed Setpoint Acceptance Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints Deviating.Valves Currently Being Retested & Recertified ML18038B8451997-04-0909 April 1997 LER 96-008-01:on 961101,Unit 2 Main Steam SRV Pilot Cartridges Failed Setpoint Tolerence Bench Tests.Caused by SRV Pilot Disc/Seat Bonding Resulting in SRV Setpoints.Srv Pilot Cartridges replaced.W/970409 Ltr ML18038B8551997-04-0404 April 1997 LER 97-001-00:on 970305,loss of Offsite Power on Unit 3 During Refueling Outage Resulted from Shorted Component. Replaced Relays Involved in Event W/Less Sensitive Relays ML18038B8441997-03-26026 March 1997 LER 95-001-02:on 950123,DG Turbocharger Failure Resulted in Noncompliance W/Ts Lco.Instituted Vibration Monitoring Program for EDG Turbochargers ML18038B8071997-01-15015 January 1997 LER 96-008-00:on 961217,loss of ECCS Division II Instrumentation Caused ECCS Equipment to Be Inoperable. Replaced Cleared Fuse & Shorted SCR ML18038B8041997-01-13013 January 1997 LER 96-007-00 on 961213,engineered Safety Feature Actuations Resulting from Inadequate Planning of step-text Work Order Occurred.Tripped Breaker Reset & LCO Condition Exited ML18038B7931996-12-0404 December 1996 LER 96-006-00:on 961106,loss of ECCS Div 1 Instrumentation Rendered ECCS Equipment Inoperable.Caused by Cleared Fuse in ECCS Div.Fuse Replaced & Addl Testing to Challenge Replacement Fuse performed.W/961204 Ltr ML18038B7921996-11-27027 November 1996 LER 96-008-00:on 961101,MS SR Valves Exceeded TS Required Setpoint Limit as Result of Disc/Seat Bonding.Caused by Corrosion Bonding of SRV Pilot Interface.Replaced All Thirteen Ms SR Valve Pilot cartridges.W/961127 Ltr ML18038B7911996-11-27027 November 1996 LER 96-007-00:on 961029,Unit 2 Scram on Turbine Control Valve Fast Closure Occurred Due to Loss of Excitation to Main Generator.Exciter Brushes Inspected & Replaced & Procedures Revised ML18038B7741996-10-15015 October 1996 LER 96-005-03:on 960915,reactor Scrammed as Required by TSs Due to Trip of Reactor Recirculation Motor Generator Set 3A. Caused by Bus Bar in Generator Armature Circuit Failing. Collector Rings Were replaced.W/961015 Ltr 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML18039A9041999-10-15015 October 1999 LER 99-010-00:on 990917,automatic Reactor Scram on Turbine Stop Valve Closure Occurred.Caused by High Water Level in Main Steam Moisture Separator 2C2.Unit 2C2 Reservoir Level Transmitter & Relays Were Replaced & Tested Satisfactorily ML18039A8981999-10-14014 October 1999 LER 99-009-00:on 990915,manual Reactor Scram Was Noted Due to EHC Leak.Caused by Failure of Stainles Steel Tubing Connection.Removed Damaged Tubing & Connection Plug ML18039A8951999-10-0808 October 1999 LER 99-008-00:on 990905,HPCI Was Inoperable Due to Failed Flow Controller.Caused by Premature Failure of Capacitor 2C3.Replaced Controller & HPCI Sys Was Run IAW Sys Operating Instructions ML18039A8751999-09-30030 September 1999 LER 99-005-00:on 990901,SR for Standby Liquid Control Sampling Was Not Met.Caused by Deficient Procedure for Chemical Addition to Standby Liquid Control.Revised Procedure.With 990930 Ltr ML20217F9671999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML20212E6341999-09-23023 September 1999 Suppl to SE Resolving Error in Original 990802 Se,Clarifying Fact That Licensee Has Not Committed to Retain Those Specific Compensatory Measures That Were Applied to one-time Extension ML20212D3831999-09-20020 September 1999 Safety Evaluation Supporting Proposed Rev to Withdrawal Schedule for First & Third Surveillance Capsules for BFN-3 RPV ML20212B8561999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Browns Ferry Nuclear Plant.With ML18039A8821999-08-31031 August 1999 Increased MSIV Leakage Tech Spec Change Submittal - Seismic Evaluation Rept. ML18039A8391999-08-0606 August 1999 BFN Unit 2 Cycle 10 ASME Section XI NIS-1 & NIS-2 Data Repts. ML20210N1221999-08-0202 August 1999 Safety Evaluation Accepting Licensee Request for Relief from ASME B&PV Code,Section XI Requirements.Request 3-ISI-7, Pertains to Second 10-year Interval ISI for Plant,Unit 3 ML20210R0931999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8201999-07-26026 July 1999 LER 99-004-00:on 990625,facility Core Spray Divisions I & II Inoperable at Same Time Due to Personnel Error.Electrical Supply Breaker to Core Spray Division II Pump 3B Returned to Normal Racked in Position ML18039A8171999-07-20020 July 1999 LER 99-007-00:on 990623,discovered That SR for Monitoring of Primary Containment Oxygen Concentration Had Not Been Met. Caused by Failure of Operators to Adequately Communicate. Required Surveillances Were Performed.With 990720 Ltr ML18039A8161999-07-19019 July 1999 LER 99-006-00:on 990618,noted That Main Steam SRV Exceeded TS Setpoint Tolerance.Caused by Pilot Vlve disc-seat Bonding.Util Replaced All 13 SRV Pilot Cartridges with Cartridges Certified to Be Witin +/-1%.With 990719 Ltr ML20209J0771999-07-16016 July 1999 Safety Evaluation Concluding That Licensee Provided Adequate Information to Resolve ampacity-related Points of Concern Raised in GL 92-08 for BFN & That No Outstanding Issues Re GL 92-08 Ampacity Issues for Browns Ferry NPP Exist ML18039A8121999-07-12012 July 1999 LER 99-005-00:on 990617,ESF Actuation & HPCI Declared Inoperable.Caused by Personnel Error.Reset HPCI & Returned Sys to Operable Status with 25 Minutes.With 990712 Ltr ML20209H4381999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A8101999-06-28028 June 1999 LER 99-004-00:on 990530,safety Features Sys Actuations Occurred Due to RPS Trip.Caused by Failure of MG Set AC Drive Motor Starter Contractor Coil.Licensee Placed 2B RPS Bus on Alternate Feed & Half Scram Was Reset ML20196F8811999-06-23023 June 1999 Safety Evaluation Accepting GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power Operated Gate Valves ML18039A8071999-06-14014 June 1999 LER 99-003-00:on 990515,automatic Reactor Scram Due to Turbine Trip Was Noted.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram ML18039A8021999-06-14014 June 1999 LER 99-002-00:on 990501,SRs for Single CR Withdrawal During Cold SD Were Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Applicable Plant Surveillances.With 990614 Ltr ML18039A8011999-06-14014 June 1999 LER 99-001-00:on 990515,automatic Reactor Scram Occurred Due to Tt.Caused by Failure of Mechanical Trip Cylinder to Latch When Hydraulically Reset.Operations Crew Stabilized Reactor Following Scram.With 990614 Ltr ML20196B8051999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A7791999-05-0606 May 1999 LER 99-003-00:on 990408,declared Plant HPCI Sys Inoperable Due to Loose Wire.Caused by Failure to Properly Tighten Screw at Some Time in Past.Loose Wire Was Tightened ML18039A7761999-04-30030 April 1999 Revised Surveillance Specimen Program Evaluation for TVA Browns Ferry Unit 3. ML20206R0731999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Bfnp.With ML18039A7561999-04-23023 April 1999 Bfnp Risk-Informed Inservice Insp (RI-ISI) Program Submittal. ML18039A7671999-04-0808 April 1999 Rev 0 to TVA-COLR-BF2C11, Browns Ferry Nuclear Plant Unit 2 Cycle 11 Colr. ML18039A7461999-04-0707 April 1999 LER 99-001-00:on 990308,determined That Two Trains of Standby Gas Treatment (SGT) Were Inoperable.Caused by Trip C SGT Blower Motor Breaker.Initiated Shutdown of Plant,Reset C SGT Blower Motor Breaker & Declared Train Operable ML20205N8341999-04-0101 April 1999 Part 21 Rept Re Automatic Switch Co Nuclear Grade Series X206380 & X206832 Solenoid Valves Ordered Without Lubricants That Were Shipped with Std Lubrication to PECO & Tva.Affected Plants Were Notified ML20205F9341999-04-0101 April 1999 Safety Evaluation Authorizing Licensee 990108 Relief Request PV-38,from Requirements of ASME BPV Code Section XI IST Testing,Valve Program for Plant,Units 1,2 & 3 ML20205T5441999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Bfnp.With ML20205S0601999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with Status Change from Previous Update,990331 ML20205S0661999-03-31031 March 1999 Rept on Status of Public Petitions Under 10CFR2.206 with No Status Change from Previous Update,990331, Atlas Corp ML18039A7361999-03-11011 March 1999 Rev 4 to TVA-COLR-BF2C10, Bfnp,Unit 2,Cycle 10 Colr. ML20204C7891999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Browns Ferry Nuclear Plant,Units 1,2 & 3.With ML18039A6951999-02-19019 February 1999 LER 99-002-00:on 990122,LCO Was Not Entered During Calibration Testing of 3D 480 Volt Rmov Board.Caused by Personnel Error.Tva Has Briefed Operations Personnel to Preclude Recurrence of Event.With 990219 Ltr ML18039A6871999-02-12012 February 1999 LER 99-001-00:on 990114,Unit 3 HPCI Was Noted Inoperable. Caused by Oil Leak on Stop Valve.Corrective Maint Was Performed to Repair Oil Leak.With 990212 Ltr ML18039A6931999-02-0303 February 1999 Rev 3 to TVA-COLR-BF2C10, Bfnp Unit 2 Cycle 10 Colr. ML18039A6941999-02-0303 February 1999 Rev 1 to TVA-COLR-BF3C9, Bfnp Unit 3 Cycle 9 Colr. ML18039A6671998-12-31031 December 1998 LER 98-004-00:on 981202,SR Intent Was Not Adequately Implemented.Caused by Procedural Inadequacy.Revised Procedures to Provide Proper SR Implementation.With 981231 Ltr ML18039A6661998-12-31031 December 1998 Ro:On 981215,HRPCRM 2-RM-90-273C Was Declared Inoperable. Caused by Downscale Indication.Containment RM Will Be Utilized as Planned Alternate Method of Monitoring Until Hrpcrm 2-RM-90-273C Can Be Returned to Operable Status ML20199K8951998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Browns Ferry Nuclear Plant.With ML20199F2721998-12-31031 December 1998 ISI Summary Rept (NIS-1), for BFN Unit 3,Cycle 8 Operation ML18039A6471998-12-15015 December 1998 LER 98-007-00:on 981116,unplanned ESF Following Loss of 4kV Unit Board 3B Occurred.Caused by Temporary Energization of Lockout Relay on 4kV Unit Board 3B When Resistor on Relay Monitoring Lamp Circuit Shorted.Replaced Resistor ML18039A6371998-12-0707 December 1998 LER 98-006-00:on 981116,MSSR Valves Exceeded TS Setpoint Tolerance.Caused by Pilot Valve Disc/Seat Bonding. Installed SRV Pressure Switches During Unit 3,cycle 8 Outage.With 981207 Ltr ML20199F2791998-12-0303 December 1998 Bfnp Unit 3 Cycle 8 ASME Section XI NIS-2 Data Rept ML20198D9621998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Bfn,Units 1,2 & 3. with ML18039A6071998-11-12012 November 1998 LER 98-005-00:on 981014,mode Changes Not Allowed by TS 3.0.4 Were Made During Reactor Startup.Caused by TS LCO 3.0.4 Not Being Properly Applied.Training Info Memo Re Proper Application for TS LCO 3.0.4 Was Prepared.With 981112 Ltr 1999-09-30
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NRC FQRM 366 (6-1998)U.s.NUCLEAR REGut AToRY coMMlsslON LICENSEE EVENT REPORT (LER)(See reverse for required number of digits/characters for each block)APPROVED BY OMB NO.3160-0104 EKPIRES oersoaoot Estirruted burden per responso to comply.with the mandatory Informatbn collect'on request: 50 hnL RepoIted lessons kamed are Incorporated into the Ecensing process and fed back to industry.Flward~regarding bunkn estImate to the Records ManagemeIR Bntnch (TA F33), U.S.Iaxdear Reguktoty Commtsskn.
Wasfdngton, OC 205550001, and to the Papework Reduction Project (31500104), CXfice cr Management and Budget.Washington.
OC 20503.If an Information cosection does not dispky a currently vasd OMB control number.the NRC may not conduct or sponsor, and a person Is not required'to respond to, the lnformatkn oaectkxL FACIUTY NAME ill Browns Ferry Nuclear Plant-Unit 2 TITLE (4I Two Trains of Standby Gas Treatment Inoperable DOCKET NUMSBl I2)05000260 PAOE lsl lof 7 EVENT DATE{5)LER NUMBER (6)REPORT DATE (7)OTHER FACILITIES INVOLVED (8)MONTH DAY YEAR YEAR SEOUENTIAL NVMBFR REVISION NUM BER MONTH OAY FACILITY NAME Unit 3 DOCKET NVMBER 05000269 03 08 1999 1999-001-00 04 07 1999 NA DOCKET NUM BER 05000 OPERATING MQDE (9)1 50.73(a){2)(l) 20.2203(a)(2)(v) 20.2201(b) 50.73(6)(2)(II) 50.73(a)(2)(III) 50.73(a)(2)(lvl 20,2203(a)(1)
POWER LEVEL (10)20.2203(a)
(3)(I)'0.2203(a)
(3)(n)20.2203(a)(4) 096 20.2203(a)(2)(il 20.2203(al(2)(II)THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR I): (Chock one or more 50.73(a)(2){vill)50.73(a){2)(x)73.71 OTHER eS>Mxc~FxvsN.
xPx@hxrrx x.'.20.2203(a)(2) jill 20.2203(a)(2)(Iv)50.36(c)(1) 50.36(c)(2)
LICENSEE CONTACT FOR THIS LER (12)50.73(o)(2)(v) 50.73(a)(2)(vil)
Specify In Abstract below or In NAC Form 368A NAME Steve Austin, Senior Licensing Project Manger TELEPHONE NVMBBl (Include Area Code)256.729.2070 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPROS cAUSE SYSTEM COMPONENT MANVFACTURER REPORTABLE TO NPROS SUPPLEMENTAL REPORT EXPECTED (14)YES{If yes, complete EXPECTED SUBMISSION DATE).X No EXPECTED SUBMISSION DATE{16)'ONTH OAY YEAR ABSTRACT (Limit to 1400 spaces, I.e., approximately 1S single.spaced typewritten lines)(16)On March 8, 1999, at approximately 2042 hours0.0236 days <br />0.567 hours <br />0.00338 weeks <br />7.76981e-4 months <br /> Central Standard Time (CST), it was determined that two trains of Standby Gas treatment (SGT)were inoperable.
Prior to the event, on March 8, 1999, at approximately 0518 hours0.006 days <br />0.144 hours <br />8.564815e-4 weeks <br />1.97099e-4 months <br /> CST, B SGT train was removed from service for planned maintenance activities.
The appropriate seven day Technical Specification (TS)Limiting Condition for Operation (LCO)for one inoperable SGT train was entered.At approximately 2038 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.75459e-4 months <br /> CST, B SGT train was placed in service to support planned post maintenance testing activities.
At 2042 hours0.0236 days <br />0.567 hours <br />0.00338 weeks <br />7.76981e-4 months <br /> CST, C SGT was declared inoperable due to a tripped blower motor breaker and, TS LCO 3.0.3 was entered for Units 2 and 3.Operations commenced a TS required shutdown of both operating Units 2 and 3.At 2237 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.511785e-4 months <br /> CST, C SGT was declared operable and TS LCO 3.0.3 was exited.The cause of this event was a trip of the C SGT blower motor breaker.Subsequent testing of the tripped breaker revealed no definitive cause for the trip of the C SGT train blower breaker.This report is submitted in pursuant to 10 CFR 50.73 (a)(2)(i)(B)as any operation or condition prohibited by the plant's Technical Specifications.
9'II04i50052
'I)'1)0407 PDR ADQCK 0500021EIO S PDR NRC FORM 366B{6-1996)
NRC FORM 366A (6-.I998I 0 LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME 1 Browns Ferry Nuclear Plant-Unit 2 OOCKET LER NUMBER 6 YEAR SEQUENTIAL REVISION NUMBER PAGE 3 2 of,7 05000260 1999 001 TEXT ill more spsce is required, use eddi rionsl copies of lVRC Form 366A/I 17)00 PLANT CONDITION(S)
At the time of the event, Unit 1 was shutdown and defueled.Unit 2 was in Mode 1 at 96 percent reactor power, approximately 3160 megawatts thermal, coasting down for a scheduled refueling outage.Unit 3 was in mode 1 at 100 percent reactor power at approximately 3458 megawatts thermal.DESCRIPTION OF EVENT A.Event: On March 8, 1999, at approximately 2042 hours0.0236 days <br />0.567 hours <br />0.00338 weeks <br />7.76981e-4 months <br /> Central Standard Time (CSg, it was determined that two trains of Standby Gas treatment (SGT)[BH]were inoperable.
This required entry into Technical Specification Limiting Condition For Operation 3.0.3 for both Units 2 and 3.Prior to the event;on March 8, 1999, at approximately 0518 hours0.006 days <br />0.144 hours <br />8.564815e-4 weeks <br />1.97099e-4 months <br /> CST, B SGT train was removed from service and declared inoperable for planned maintenance activities.
The appropriate seven day LCO for one inoperable SGT train was entered.At approximately 2038 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.75459e-4 months <br /> CST, B SGT train was started to support planned post maintenance testing.At 2042 hours0.0236 days <br />0.567 hours <br />0.00338 weeks <br />7.76981e-4 months <br /> the Unit 2 operator received alarms, C SGT Train Relative Humidity Heater Temperature High and C SGT Filter Bank Heater Element Power Lost.~The control room also received alarm, SGT Train C Unavailable.
Accordingly, C SGT train was declared inoperable.
Field observations determined that the supply breaker[BKR]for the C SGT train blower[FAN]had tripped.In accordance with plant TS Action Statement for SGT, with two of three SGT trains Inoperable, enter TS LCO 3.0.3.TS LCO 3.0.3 requires in part, when an LCO is not met actions shall be initiated within one hour to place the unit as applicable in: MODE 2 in seven hours, MODE 3 in 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br />;and mode four in 37 hours4.282407e-4 days <br />0.0103 hours <br />6.117725e-5 weeks <br />1.40785e-5 months <br />.At 2141 hours0.0248 days <br />0.595 hours <br />0.00354 weeks <br />8.146505e-4 months <br /> CST, TVA initiated a reduction in reactor power for both Units 2 and 3 in accordance with General Operating Instruction, Unit Shutdown From Power to Cold Shutdown And Reductions ln Power During Power Operations.
Troubleshooting did not identify a cause for the breaker trip.The alarms were caused by the inadvertent operation of the C SGT train heater flow switch, 0-FS-065-0070B
[FS], and the C SGT train breaker trip while B SGT train was operating.
The breaker was reset and the alarms cleared.At 2220 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.4471e-4 months <br /> flow switch 0-FS-065-0070B was declared inoperable.
In accordance with the Browns Ferry Technical Requirements Manual Action statement for SGT instrumentation, when one or more of the required flow instrument channels is inoperable, trip the logic for the inoperable flow switch and start the affected SGT subsystem.
Therefore, C SGT train was placed in operation with the relative humidity heater controls in the'ON'osition to trip the flow switch logic and subsequently declared operable.Hence, TVA exited TS LCO 3.0.3 at approximately 2237 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.511785e-4 months <br /> CST.At 2239 hours0.0259 days <br />0.622 hours <br />0.0037 weeks <br />8.519395e-4 months <br /> TVA made a one hour non-emergency notification to NRC in accordance with 10 CFR 50.72(b)(1)(i)(A) as the initiation of a nuclear plant shutdown required by the plant's Technical Specifications.
Units 2 and 3 were returned to the pre-event thermal power by 2309 hours0.0267 days <br />0.641 hours <br />0.00382 weeks <br />8.785745e-4 months <br /> CST and 2311 hours0.0267 days <br />0.642 hours <br />0.00382 weeks <br />8.793355e-4 months <br /> CST respectfully.
NRC'FORM 366 l6-1998) 0 II g1 NRC FORM 366A I6-19981 LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME 1 DOCKET LER NUMBER 6 PAGE 3 Browns Ferry Nuclear Plant-Unit 2 YEAR SEQUEN TIAL REVISION NUMBER 3 of?05000260 TEXT llf more space is required, use additional copies of NRC Form 366Ai I17I 1999 001 00 On March 9, 1999, at approximately 2036 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.74698e-4 months <br /> CST, B SGT train was declared operable, and the seven day LCO for one inoperable SGT train was exited.This report is submitted pursuant to 10 CFR 50.73(a)(2)(i)(B) as any operation or condition prohibited by the plant's Technical Specifications.
B.Ino erable Structures Com onents orS stems that Contributed to the Event: None.C.Dates and A roximate Times of Ma or Occurrences:
March 8, 1999, at 0518 hours0.006 days <br />0.144 hours <br />8.564815e-4 weeks <br />1.97099e-4 months <br /> CST B SGT train is removed from service for scheduled maintenance.
A seven day LCO for an inoperable SGT train is entered.2038 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.75459e-4 months <br /> CST B SGT train is placed in service.2042 hours0.0236 days <br />0.567 hours <br />0.00338 weeks <br />7.76981e-4 months <br /> CST Received alarm C SGT train Relative Humidity Temperature High, followed by alarm B SGT Train Filter Bank Heater Element Power Lost.Alarm SGT Train C Unavailable was also received.Declared C SGT train inoperable and entered TS LCO 3.0.3 for inoperable B and C SGT, trains.2141 hours0.0248 days <br />0.595 hours <br />0.00354 weeks <br />8.146505e-4 months <br /> CST As required by TS LCO 3.0.3, initiated shutdown of both Units 2 and 3.2237 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.511785e-4 months <br /> CST C SGT is declared operable.TS LCO 3.0.3 is exited.Commenced power ascension back to pre-event thermal power for both Units 2 and 3.2239 hours0.0259 days <br />0.622 hours <br />0.0037 weeks <br />8.519395e-4 months <br /> CST TVA made a one hour Non-emergency notification in accordance with 10 CFR50.72 (b)(1)(i)(A).March 9, 1999, at 2036 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.74698e-4 months <br /> CST Following satisfactory completion of post maintenance testing associated with B SGT train, it was declared operable and the seven day LCO for one inoperable SGT was exited.D.Other S stems or Seconda Functions Affected None.E.Method of Discove NRC FORM 366 I6-199BI The Unit 2 and 3 operators received alarms indicating C SGT Relative Humidity Heater Temperature High and C SGT Filter Bank Heater Element Power Lost, and alarm, SGT Train C Unavailable.
0 NRC FORIVl 366A I6 1998I LICENSEE EYENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME 1 Browns Ferry Nuclear Plant-Unit 2 DOCKET LER NUMBER 6 YEAR SEQUENTIAL REVISION NUMBER PAGE 3 4of7 05000260 TEXT fit moro space is required, use additional copies of NRC Form 386A/(17J 1999 001 00 F.0 erator Actions No operator actions contributed to this event.G.Safet S stem Res onses None.III.CAUSE OF THE EVENT A.Immediate Cause The immediate cause of the event was the trip of the C SGT train blower motor breaker thus, rendering C SGT train inoperable.
This combined with B SGT train being inoperable for planned maintenance activities, left only A SGT train operable, requiring entry into TS LCO 3.0.3.The immediate cause for the alarm associated with the relative humidity heater was calibration of the C SGT fan discharge flow switch (0-FS-65-0070B).
The switch was out of calibration and was actuated by a small amount of back flow from B SGT train.B.Root Cause The root cause for the trip of the C SGT train blower motor breaker could not be identified.
The operator dispatched to the associated motor control center (MCC)tED]noted that the breaker that feeds the C SGT train blower motor had tripped.The operator also noted that no unusual actions were required to close the breaker.This breaker feeds the C SGT train blower motor,(which was not running and had not attempted to start)also supplies the control power transformer for the C SGT train blower, damper, and the relative humidity heater.When the breaker was reported tripped, the MCC breaker cubicle was examined for signs of an electrical fault and no signs were found.A data recorder was connected to the low side of the control power transformer and the control circuit was monitored under conditions similar to the initial event.No unusual values or wave forms were recorded.It was concluded that there were no problems with the control circuit or the transformer.
The breaker was then removed from the MCC and bench tested.The test results verified that the breaker was operating normally and applicable performance parameters were within acceptable limits.The breaker was then disassembled and an internal inspection was performed.
Evidence of overheating was observed in the area of the A phase magnetic trip device.The breaker case was discolored and the varnish on the current coil on the trip device appeared burned.The cause of the overheating was determined to be the bolt that secured the movable contact pig-tail to the current sensing coil being insufficiently torqued.The effects of this heating, may have contributed to reduced reliability of the breaker.NRC FORM 366 l6-1996l il NRC FORM 366A (6-1998)LlCENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FltCILITY NAME 1 Browns'Ferry Nuclear Plant-Unit 2 OOCKET 05000260 LER NUMBER 6 YEAR SEQUENTIAL NUMBER 1999 001 00 PAGE 3 5of7 TEXT llf more spece is required, use additional copies of NRC Form 366Ai l1 7)Following the event, the C SGT blower motor breaker was closed and C SGT train was placed in service March 8, 1999, at 2220 hours0.0257 days <br />0.617 hours <br />0.00367 weeks <br />8.4471e-4 months <br /> CST and operated continuously until 8 SGT was declared operable on March.9, 1999, at 2036 hours0.0236 days <br />0.566 hours <br />0.00337 weeks <br />7.74698e-4 months <br />.This type breaker does not have any history of failure at BFN;therefore, TVA considers this a random event.C.Contributin Factors None.IV.ANALYSIS OF THE EVENT The SGT system exhausts the secondary containment atmosphere to the environment through appropriate
, treatment equipment.
The SGT system consists of three fifty percent filter subsystems each with a designed flow rate of 9000 standard cubic feet per minute (SCFM).Two of the three subsystems are necessary for the SGT system to perform its designed function.Two subsystems will draw down the secondary containment to less than or equal to 0.25 inches of vacuum water gauge.During this evolution, planned activities were in progress in accordance with applicable procedural and Technical Specification requirements.
The appropriate LCO was entered during the planned testing activities which allows 7 days of continued power operation due to 8 SGT train out of service.As soon as the second train of SGT was declared inoperable, the appropriate section of TSs was entered (TS LCO 3.0.3)which required beginning an immediate shutdown.This evolution was performed in accordance with the applicable requirements.
During the time that two SGT were inoperable, 8 SGT remained functional and continued to operate as designed.Once it was determined that SGT C train could be made operable by manually starting, that train was placed in service and TS LCO 3.0.3 was exited.An ITE-Gould Model Type HE3-H050 three phase 600 VAC, molded case circuit breaker, was involved in this event.This breaker contains only a magnetic trip device as opposed to the more conventional configuration where both magnetic and thermal trip devices are included.In this configuration, overload protection for the blower is provided by thermal overload heaters associated with the motor starter energized from the breaker.The magnetic trip functions to clear a fault.The breaker does not actuate on a small overload situation.
The blower breaker is unique since it is the only breaker configured.
with only a magnetic trip device.This type and manufacturer breaker is not utilized in any other application at Browns Ferry Nuclear Plant other than the power feeds to the C SGT train.V.ASSESSMENT OF THE SAFETY CONSEQUENCES The potential safety consequences of the condition described were not significant.
Actions taken during the event placed the plant in the safest possible configuration.
In the event secondary containment isolation is required, the SGT system is required to maintain a negative pressure inside secondary containment at less than of equal to 0.25 inches of waler with a flow equal to the allowable secondary containment inleakage and the design basis margin.As reviousl discussed from March 8, 1999, at 2042 hours0.0236 days <br />0.567 hours <br />0.00338 weeks <br />7.76981e-4 months <br />, when C SGT train was declared ino erable, NRC FORM 366 (6.1998) 0 J NRC FORM 366A"J IS-1998)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME 1 Browns Ferry Nuclear Plant-Unit 2 DOCKET LER NUMBER 6 YEAR SEQUENTIAL REVISION NUMBER PAGE 3 6 of 7 05000260 1999 001 TEXT (If more spece is required, use eddirionel copies of NRC Form 366A/(17)00 B SGT train, although inoperable due to lack of completion of post maintenance surveillance test, functioned until C SGT train was declared operable at 2237 hours0.0259 days <br />0.621 hours <br />0.0037 weeks <br />8.511785e-4 months <br /> CST.During that time that C SGT train was inoperable, B SGT train was in the same alignment as that for operation during required conditions.
The post maintenance surveillance performed on March 9, 1999, was successful, and B SGT train demonstrated that it would, have successfully performed its safety function if called upon.In the unlikely event that SGT B fails to perform its designed function during a Loss-of-Coolant-Accident, potential exfiltration from the reactor building could occur.However, this is not expected to pose a significant increase in the consequences of an accident.One train of SGT is capable of 9000 SCFM.During the previous secondary containment test, two SGT trains maintained a negative 0.25 inches of water on secondary containment with a total flow of 9363 SCFM.Therefore, one SGT train is capable of maintaining the reactor building at a slight negative pressure.The results of the BFN Probabilistic Safety Assessment (PSA)which was submitted to NRC on September 1, 1992, support, this conclusion.
The performance of SGT system is evaluated for a number of severe accident scenarios in the level 2 PSA.The impact of the SGT system on the evaluated source term indicated that SGT system performance is not a dominant fission-product removal mechanism; therefore, postulated reduced,SGT performance is not a significant contributor to the accident consequences for evaluated scenarios.
Accordingly, there were no actual or potential safety consequences as a result of this event.VI.CORRECTIVE ACTIONS A.Immediate Corrective Actions The immediate corrective actions included, the initiation of, shutdown of both Units 2 and 3 due to the unavailability of 2 of the 3 SGT trains (LCO.3.0.3).
The C SGT blower motor breaker was reset, C SGT train was started, RH control heater switch placed in the ON position and the train was declared operable.B.Corrective Actions to Prevent Recurrence The C SGT train blower motor breaker was replaced and 0-FS-065-0070B was calibrated.
VII.ADDITIONAL INFORMATION A.Failed Com onents None.B.Previous LERs on Similar Events LER 50-260/1989-022-01, issued on July 21, 1989, discussed an event where trains A and B of the SGT system were declared inoperable following the discovery that the circuit breakers for their relative humidity control heaters were tripped.The root cause for this event was an inadequate initial design and application of a breaker.The initial design application did not address elevated tern eratures in the circuit breaker location.The ambient tern erature in the NRC FORM 366 (6-1996) 0 j' NRC FORM 366A (6-1998)LICENSEE EVENT REPORT (LER)TEXT CONTINUATION U.S.NUCLEAR REGULATORY COMMISSION FACILITY NAME 1 Browns Ferry Nuclear Plant-Unit 2 DOCKET LER NUMBER 6 YEAR SEQUENTIAL
'REVISION NUMBER PAGE 3 7of7 05000260 TEXT Iif more space is required, use additional copies of NRC Form 366AI l17)1999'01 00 area near the circuit breaker as weil as lack of ventilation in this area lead to this event.This was not a factor in this event and corrective actions taken would not have prevented occurrence of this event.VIII.COMMITMENTS None.Energy Industry Identification System (EIIS)system and component codes are identified in the text with brackets (e.g.,[XXj).NRC FORM 366 l6-1998) 0~k l t l