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| FORWARD (See for required ni.iiber of CC>>4MENTS REGARDING BURDEN ESTIMATE TO THE reverse INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 digits/characters for each block) U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON D 20555-0001, AND TO THE PAPERWORK REDUCTION FACILITY 11A1E (1) DOCKET IUllER (2) PAGE (3) SAUM GENERATING STATION UNIT 1 05000272 1 OF 4 TITLE (4) Operation of Positive | | FORWARD (See for required ni.iiber of CC>>4MENTS REGARDING BURDEN ESTIMATE TO THE reverse INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 digits/characters for each block) U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON D 20555-0001, AND TO THE PAPERWORK REDUCTION FACILITY 11A1E (1) DOCKET IUllER (2) PAGE (3) SAUM GENERATING STATION UNIT 1 05000272 1 OF 4 TITLE (4) Operation of Positive |
| !\1ItP rurµg a Safety Injection could have Resulted in lOCFRl.00 am 19 nose Limit Criteria EVENT DATE f5> LEI lllllER f6 REPCJIT DATE f7> OTHER FACILITIES llMJLVED fB> YEAR I SEQUENTIAL REVISI FACILITY NAME DOCKET NUMBER MONTH DAY YEAR ON MONTH DAY YEAR NUMBER NUMBER SAUM UNIT 2 05000311 FACILITY NAME DOCKET NUMBER 12 11 76 95 -027 -00 11 27 95 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE RECIJIREMENTS OF 10 CFR §: (Check one or more ctn MOOE (9) | | !\1ItP rurµg a Safety Injection could have Resulted in lOCFRl.00 am 19 nose Limit Criteria EVENT DATE f5> LEI lllllER f6 REPCJIT DATE f7> OTHER FACILITIES llMJLVED fB> YEAR I SEQUENTIAL REVISI FACILITY NAME DOCKET NUMBER MONTH DAY YEAR ON MONTH DAY YEAR NUMBER NUMBER SAUM UNIT 2 05000311 FACILITY NAME DOCKET NUMBER 12 11 76 95 -027 -00 11 27 95 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE RECIJIREMENTS OF 10 CFR §: (Check one or more ctn MOOE (9) |
| * 20.2201(b) 20.2203(a)(2)(V) x 50. 73(a)(2)( i) 50. 73(a)(2)(vi ii POER 20.2203(a)(1) 20.2203(a)(3)(i) | | * 20.2201(b) 20.2203(a)(2)(V) x 50. 73(a)(2)( i) 50. 73(a)(2)(vi ii POER 20.2203(a)(1) 20.2203(a)(3)(i) |
| : 50. 73(a)(2)( ii) 50. 73(a)(2)(x) | | : 50. 73(a)(2)( ii) 50. 73(a)(2)(x) |
| LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 73.71 illl!lllllllllll1l1'll1ll 20.2203(a)(2)(ii) 20.2203(a)(4) | | LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 73.71 illl!lllllllllll1l1'll1ll 20.2203(a)(2)(ii) 20.2203(a)(4) |
| : 50. 73(a)(2)( iv) OTHER 20.2203(a)(2)Ciii) 50.36(c)(1) | | : 50. 73(a)(2)( iv) OTHER 20.2203(a)(2)Ciii) 50.36(c)(1) |
| : 50. 73(a)(2)(v) in Abstract 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2)(vii) below or in NRC Form 366A LICENSEE CDITACT FOR THIS LER 12) NAME TELEPHONE NUMBER (Include Area Code) Mr. D. Shtnnaker, Specialist EngineerinJ SUpervisor 609-339-1852 CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE ll1itl 1 lif 11111 CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NP RDS TO NPRDS I SUPPLEMENTAL REPORT EXPECTED C14> EXPECTED MONTH DAY YEAR 'YES XINO SUIMI SS Ull (If yes, EXPECTED SUBMISSION DATE). DATE (15) ABSTRACT CL imit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) On October 26, 1995 it was detennined that doses durinJ a IOCA could have exceeded the plant licensirg basis due to inacx::urate assunptions in the dose calculations. | | : 50. 73(a)(2)(v) in Abstract 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2)(vii) below or in NRC Form 366A LICENSEE CDITACT FOR THIS LER 12) NAME TELEPHONE NUMBER (Include Area Code) Mr. D. Shtnnaker, Specialist EngineerinJ SUpervisor 609-339-1852 CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE ll1itl 1 lif 11111 CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NP RDS TO NPRDS I SUPPLEMENTAL REPORT EXPECTED C14> EXPECTED MONTH DAY YEAR 'YES XINO SUIMI SS Ull (If yes, EXPECTED SUBMISSION DATE). DATE (15) ABSTRACT CL imit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) On October 26, 1995 it was detennined that doses durinJ a IOCA could have exceeded the plant licensirg basis due to inacx::urate assunptions in the dose calculations. |
| '!he previous acx:::ident analysis was perf onned assunrin:J the PDP trips after an safety injection signal am that the exhaust fran the Auxiliacy Buildirg passes through a dlarcoal filter durirg the cold leg recirculation of a IOCA. '!he positive displacement | | '!he previous acx:::ident analysis was perf onned assunrin:J the PDP trips after an safety injection signal am that the exhaust fran the Auxiliacy Buildirg passes through a dlarcoal filter durirg the cold leg recirculation of a IOCA. '!he positive displacement |
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| Oct:cber 26, 1995 <XlNDITIONS PRIOR 'ID OCXl.JRRENCE unit 1: unit 2: Defueled, 000 % Reactor Power M:Jde 5, 000 % Reactor Power '!here -were no structures, caiponents, or systems that were inoperable at the start of the event that caitrib.rt:.ed to the event. DESOUPr!ON OF OCCURRENCE On Oct:cber 26, 1995 it was determined that doses durinJ a Loss Of Coolant Aa::ident (I.OCA) oculd potentially exceed the lOCFRlOO site bourrlacy dose limit am GOC 19 control roan dose limit. Previa.is analyses assrmv;,d that the positive displacement pmp (PDP) in the Olemical am Volume Control (OTC) system tripped after a safety injection (SI) signal. However, it was determined that the PDP only trips concurrent with a loss of offsite J;XJWer after a safety injection signal. DlrIDJ the cold leg recirculation i;ilase of a I.OCA, q;>eration of the PDP results in leakage of contaminated water past the PDP seals. '!he PDP seal leakage increases the total contaminated leakage to the Auxiliary BuildinJ. | | Oct:cber 26, 1995 <XlNDITIONS PRIOR 'ID OCXl.JRRENCE unit 1: unit 2: Defueled, 000 % Reactor Power M:Jde 5, 000 % Reactor Power '!here -were no structures, caiponents, or systems that were inoperable at the start of the event that caitrib.rt:.ed to the event. DESOUPr!ON OF OCCURRENCE On Oct:cber 26, 1995 it was determined that doses durinJ a Loss Of Coolant Aa::ident (I.OCA) oculd potentially exceed the lOCFRlOO site bourrlacy dose limit am GOC 19 control roan dose limit. Previa.is analyses assrmv;,d that the positive displacement pmp (PDP) in the Olemical am Volume Control (OTC) system tripped after a safety injection (SI) signal. However, it was determined that the PDP only trips concurrent with a loss of offsite J;XJWer after a safety injection signal. DlrIDJ the cold leg recirculation i;ilase of a I.OCA, q;>eration of the PDP results in leakage of contaminated water past the PDP seals. '!he PDP seal leakage increases the total contaminated leakage to the Auxiliary BuildinJ. |
| '!he UFSAR accident analyses were perfonned assurniig the PDP trips after an safety injection signal am do not consider contaminated leakage from the PDP seals. DlrIDJ a I.OCA, the charcoal. | | '!he UFSAR accident analyses were perfonned assurniig the PDP trips after an safety injection signal am do not consider contaminated leakage from the PDP seals. DlrIDJ a I.OCA, the charcoal. |
| filter for the Auxiliary Buildin;J Ventilation (ABV) system is not autana.tically aligned but nust be aligned by an operator fram the control roan. In the UFSAR accident analysis, it is assumed that the exhaust from the ABV system passes through the charcoal filter durinJ the recirculation | | filter for the Auxiliary Buildin;J Ventilation (ABV) system is not autana.tically aligned but nust be aligned by an operator fram the control roan. In the UFSAR accident analysis, it is assumed that the exhaust from the ABV system passes through the charcoal filter durinJ the recirculation |
| :Eilase of the I.OCA. Without the dlarcoal. | | :Eilase of the I.OCA. Without the dlarcoal. |
| filtration, calculated doses durinJ a I.OCA are significantly greater with PDP seal leakage am may exceed the lOCFRlOO site bourrlacy dose limits am the G1X! 19 control roam limit. NRC FORM 366A (4-'I:> | | filtration, calculated doses durinJ a I.OCA are significantly greater with PDP seal leakage am may exceed the lOCFRlOO site bourrlacy dose limits am the G1X! 19 control roam limit. NRC FORM 366A (4-'I:> |
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| Awareness of this I.ER aided in the identification of the PDP operation possibly exceeding the lOCFRlOO am GOC dose limits. '!\<<> IERs in 1995 identified incidents | | Awareness of this I.ER aided in the identification of the PDP operation possibly exceeding the lOCFRlOO am GOC dose limits. '!\<<> IERs in 1995 identified incidents |
| 'Where the UFSAR am the ac:x::ident analysis were in conflict. | | 'Where the UFSAR am the ac:x::ident analysis were in conflict. |
| I.ER 272/95-011-00 identified that a discrepancy existed between the UFSAR am the steam line break analysis for the oontairnnent penetration area. I.ER 272/95-016-00 identified a discrepancy | | I.ER 272/95-011-00 identified that a discrepancy existed between the UFSAR am the steam line break analysis for the oontairnnent penetration area. I.ER 272/95-016-00 identified a discrepancy |
| :involvi.rg the oontairnnent structure duri.rg a steam Line Break Analysis ani a Design Basis I.DCA. Both IERs are similar to this I.ER in that a discrepancy existed between the ac:x::ident analysis am the UFSAR. SAFEIY SIGNIFICANCE | | :involvi.rg the oontairnnent structure duri.rg a steam Line Break Analysis ani a Design Basis I.DCA. Both IERs are similar to this I.ER in that a discrepancy existed between the ac:x::ident analysis am the UFSAR. SAFEIY SIGNIFICANCE |
| '1he operation of the PDP after a lOCA has a direct i.npact on the potential for off-site release of radioactivity. | | '1he operation of the PDP after a lOCA has a direct i.npact on the potential for off-site release of radioactivity. |
| 'lhe deficiency in the design basis could have resulted in site bcumary ani control roan doses exceeding licen.si.rg basis limits duri.rg a lOCA at either Salem Unit. A review of the Westin:]house evaluation revealed that an offsite dose in excess of the lOCFRlOO am GOC 19 limits ooold have ocx:urred a.ssumin;J a IDCA am an mifiltered release (dlarcoal filter not on-line). | | 'lhe deficiency in the design basis could have resulted in site bcumary ani control roan doses exceeding licen.si.rg basis limits duri.rg a lOCA at either Salem Unit. A review of the Westin:]house evaluation revealed that an offsite dose in excess of the lOCFRlOO am GOC 19 limits ooold have ocx:urred a.ssumin;J a IDCA am an mifiltered release (dlarcoal filter not on-line). |
| '!he design basis sairce tenn values are considered to be conservatively high. Based on the sam:e tenn definition aooepted for the Mvanoed Light water Reactor design, the NRC ani the in:iustry are evaluatin_J the use of ioore :realistic source tenn predictions. | | '!he design basis sairce tenn values are considered to be conservatively high. Based on the sam:e tenn definition aooepted for the Mvanoed Light water Reactor design, the NRC ani the in:iustry are evaluatin_J the use of ioore :realistic source tenn predictions. |
| Use of the m:>re :realistic source tenn values in analyzi.rg the operation of the PDP during an SI inlicate that the 10 CFRlOO ani GOC 19 criteria would not likely have been exceeded if an event had occurred. | | Use of the m:>re :realistic source tenn values in analyzi.rg the operation of the PDP during an SI inlicate that the 10 CFRlOO ani GOC 19 criteria would not likely have been exceeded if an event had occurred. |
| : 1. '1he EDPs were revised to include steps for manually triwi.rg the PDP prior to ocmnerx::i.ng cold leg recirculation. | | : 1. '1he EDPs were revised to include steps for manually triwi.rg the PDP prior to ocmnerx::i.ng cold leg recirculation. |
| : 2. Perfonn a ccmprehensive review of the UFSAR ClJapter 15 ac:x::ident analysis to better ensure the consistency between the design assumptions, am plant configuration am operation. | | : 2. Perfonn a ccmprehensive review of the UFSAR ClJapter 15 ac:x::ident analysis to better ensure the consistency between the design assumptions, am plant configuration am operation. |
| : 3. Identify am d<x:ument all sources of contaminated leakage, incluclir¥] | | : 3. Identify am d<x:ument all sources of contaminated leakage, incluclir¥] |
| a secured PDP, into the .Auxiliary Building.duri.ng a IDCA am incorporate* | | a secured PDP, into the .Auxiliary Building.duri.ng a IDCA am incorporate* |
| in dose calculations. | | in dose calculations. |
| : 4. Review open items identified in the MN system CBDs to ensure that all issues that could inpa.ct the plant licensing basis have been addressed to ensure no safety concems exist post :restart. | | : 4. Review open items identified in the MN system CBDs to ensure that all issues that could inpa.ct the plant licensing basis have been addressed to ensure no safety concems exist post :restart. |
| Also, identify inprovements to the MN system aOO,lor revisions to the EDPs necessary to ensure corrplianc:e with lOCFRlOO limit am GOC 19 limit. Incorporate changes into the i.npacted docurmmtation, inch.r:li.rg the UFSAR. Items 2-4 will be ccmpleted prior to restart. NRC FORM 366A (4*95) -. ---;* :-..}} | | Also, identify inprovements to the MN system aOO,lor revisions to the EDPs necessary to ensure corrplianc:e with lOCFRlOO limit am GOC 19 limit. Incorporate changes into the i.npacted docurmmtation, inch.r:li.rg the UFSAR. Items 2-4 will be ccmpleted prior to restart. NRC FORM 366A (4*95) -. ---;* :-..}} |
Similar Documents at Salem |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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- Public SeNice Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit NOV 2 4 1995 LR-N95207 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
LICENSEE EVENT REPORT 272/95-027-00 SALEM GENERATING STATION -UNIT 1 FACILITY OPERATING LICENSE NO. DPR-70 DOCKET NO. 50-272 This Licensee Event Report entitled "Operation of Positive Displacement Pump During a Safety Injection Could Have Resulted in Exceeding lOCFRlOO and GDC 19 Dose Criteria" is being submitted pursuant to the requirements of the Code of Federal Regulations 10CFR50. 73 (a) (2) (i) . SORC Mtg.95-140 Attachment DVH/tcp C Distribution LER File 9602070146 951127 PDR ADOCK 05000272 S PDR Sincerely, @A-Cla'?:lc.
Warren General Manager -Salem Operations The power is in yDUr hands. 95-2168 REV. 6 94
.. *
- Attachment A PSE&G Commitments for LER 272/95-027 The following items represent PSE&G commitments made to the Nuclear Regulatory Commission related to LER 272/95-027-00.
The commitments are as follows: Perform a comprehensive review of the UFSAR Chapter 15 accident analysis to better ensure the consistency between the design assumptions, and plant configuration or operation.
Identify and document all sources of contaminated leakage, including a secured PDP, into the Auxiliary Building during a LOCA and incorporate in dose calculations.
Review open items identified in the ABV system CBDs to ensure that all issues that could impact the plant licensing basis have been addressed to ensure no safety concerns exist post restart. Also, identify improvements to the ABV system and/or revisions to the EOPs necessary to ensure compliance with lOCFRlOO limit and GDC 19 limit. Incorporate changes into the impacted documentation, including the UFSAR. The above items will be completed prior to restart. -
- NRC FORM 366 U.S. IU:LEAR REGIJLATORY aHllSSUlll APPROVED BY Dm m. 3150-0104 (4*95> . EXPIRES 04/30/98 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COLLECTION REQUEST: 50.0 HRS. LICENSEE EVENT REPORT (LER) REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED BACK TO INDUSTRY.
FORWARD (See for required ni.iiber of CC>>4MENTS REGARDING BURDEN ESTIMATE TO THE reverse INFORMATION AND RECORDS MANAGEMENT BRANCH (T-6 digits/characters for each block) U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON D 20555-0001, AND TO THE PAPERWORK REDUCTION FACILITY 11A1E (1) DOCKET IUllER (2) PAGE (3) SAUM GENERATING STATION UNIT 1 05000272 1 OF 4 TITLE (4) Operation of Positive
!\1ItP rurµg a Safety Injection could have Resulted in lOCFRl.00 am 19 nose Limit Criteria EVENT DATE f5> LEI lllllER f6 REPCJIT DATE f7> OTHER FACILITIES llMJLVED fB> YEAR I SEQUENTIAL REVISI FACILITY NAME DOCKET NUMBER MONTH DAY YEAR ON MONTH DAY YEAR NUMBER NUMBER SAUM UNIT 2 05000311 FACILITY NAME DOCKET NUMBER 12 11 76 95 -027 -00 11 27 95 05000 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE RECIJIREMENTS OF 10 CFR §: (Check one or more ctn MOOE (9)
- 20.2201(b) 20.2203(a)(2)(V) x 50. 73(a)(2)( i) 50. 73(a)(2)(vi ii POER 20.2203(a)(1) 20.2203(a)(3)(i)
- 50. 73(a)(2)( ii) 50. 73(a)(2)(x)
LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 73.71 illl!lllllllllll1l1'll1ll 20.2203(a)(2)(ii) 20.2203(a)(4)
- 50. 73(a)(2)( iv) OTHER 20.2203(a)(2)Ciii) 50.36(c)(1)
- 50. 73(a)(2)(v) in Abstract 20.2203(a)(2)(iv) 50.36(c)(2) 50.73(a)(2)(vii) below or in NRC Form 366A LICENSEE CDITACT FOR THIS LER 12) NAME TELEPHONE NUMBER (Include Area Code) Mr. D. Shtnnaker, Specialist EngineerinJ SUpervisor 609-339-1852 CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE ll1itl 1 lif 11111 CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NP RDS TO NPRDS I SUPPLEMENTAL REPORT EXPECTED C14> EXPECTED MONTH DAY YEAR 'YES XINO SUIMI SS Ull (If yes, EXPECTED SUBMISSION DATE). DATE (15) ABSTRACT CL imit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) On October 26, 1995 it was detennined that doses durinJ a IOCA could have exceeded the plant licensirg basis due to inacx::urate assunptions in the dose calculations.
'!he previous acx:::ident analysis was perf onned assunrin:J the PDP trips after an safety injection signal am that the exhaust fran the Auxiliacy Buildirg passes through a dlarcoal filter durirg the cold leg recirculation of a IOCA. '!he positive displacement
?IIIP in the Cllemical am Volmne Control system only trips corx::urrent with a loss of offsite pc:Mer after a safety injection signal. In addition, the Auxiliaey Buildirg Ventilation dlarcoal filtration is not autanatically aligned in acx:::ident c::omitions.
Withalt the dlarcoal filtration, the calculated site doses due to leakage of the PDP seals durirg a IOCA are significantly greater than the doses in the UFSAR ani may exceed the lOCFRl.00 site boun:lary dose limits arrl the GOC 19 control roam limits. 'lhe Energency q>eratirg Procedures were r:evised in August 1994 to manually trip the PDP prior to enterirg cold leg recirculation.
'!his event is reportable in accordance with lOCFR 73(a) (2) (ii) I any event that resulted in a comition that was outside the design basis of the plant. NRC FORM 366 (4-95)
- U.S. llJClEAI REGULATORY COIUSSION LICENSEE EVENT REPORT (LER) TEXT CDNl'INUATION FACILITY NAME (1> DOCKET LER 11.11BER (6) PAGE Cl) YEAR I SEQUENTIAL I REV NUMBER NUMBER 2 OF 4 05000272 SAIBM GENERATING S'm'l'ION UNIT 1 95 -027 -00 TEXT (If more space is required.
use additional copies of NRC Form 366A) (17) PIAN'!' AND SYSTEM IDENI'IFICATION Westin;Jhouse
-Pressurized Water Reactor Positive Displacement Pl.mp , Cllemical
& Volume Control System (OTC) {CB/P}*
- Energy :rmust.ry Identification System (EIIS) codes am caaponent furx::tion identifier codes Cl£P?ar in the text as {SS/CT:C}.
IDENI'IFICATION OF OCXIJRRENCE EVent rate: Unit 1: Decanber 11, 1976 (Initial Plant Critically)
Unit 2: August 2, 1980 (Initial Plant Critically) rate Determined to be Reportable:
Oct:cber 26, 1995 <XlNDITIONS PRIOR 'ID OCXl.JRRENCE unit 1: unit 2: Defueled, 000 % Reactor Power M:Jde 5, 000 % Reactor Power '!here -were no structures, caiponents, or systems that were inoperable at the start of the event that caitrib.rt:.ed to the event. DESOUPr!ON OF OCCURRENCE On Oct:cber 26, 1995 it was determined that doses durinJ a Loss Of Coolant Aa::ident (I.OCA) oculd potentially exceed the lOCFRlOO site bourrlacy dose limit am GOC 19 control roan dose limit. Previa.is analyses assrmv;,d that the positive displacement pmp (PDP) in the Olemical am Volume Control (OTC) system tripped after a safety injection (SI) signal. However, it was determined that the PDP only trips concurrent with a loss of offsite J;XJWer after a safety injection signal. DlrIDJ the cold leg recirculation i;ilase of a I.OCA, q;>eration of the PDP results in leakage of contaminated water past the PDP seals. '!he PDP seal leakage increases the total contaminated leakage to the Auxiliary BuildinJ.
'!he UFSAR accident analyses were perfonned assurniig the PDP trips after an safety injection signal am do not consider contaminated leakage from the PDP seals. DlrIDJ a I.OCA, the charcoal.
filter for the Auxiliary Buildin;J Ventilation (ABV) system is not autana.tically aligned but nust be aligned by an operator fram the control roan. In the UFSAR accident analysis, it is assumed that the exhaust from the ABV system passes through the charcoal filter durinJ the recirculation
- Eilase of the I.OCA. Without the dlarcoal.
filtration, calculated doses durinJ a I.OCA are significantly greater with PDP seal leakage am may exceed the lOCFRlOO site bourrlacy dose limits am the G1X! 19 control roam limit. NRC FORM 366A (4-'I:>
' I *
- U.S. llJClEAR IE&Jl..ATmt1' aJllJISSllll LICENSEE EVENT REPORT (LER) 'l'E}CI' CDN.l'INUATION FACILITY' NAME (1) DOCKET LER IUIBER (6) YEAR I SEQUENTIAL I REVIS! NllMBER ON SAUM GENERATING STATION UNIT* 1 05000272 i 95 .. 027 .. 00 TEXT (If more space is required, use additional copies of NRC Form 366A> (17> ANALYSIS OF OCXl.JRRENCE PAGE (3) 3 OF 4 '!he IDP is part of the eve system am is used for nonnal makeup, boratian am dilution c:perations.
'1he PDP is located in the Auxiliai:y Build.irg.
In addition to the PDP, there are two dlargmysafety injection (SI) p.mp; in the eve system. rurin} oonnal operation, these pmps provide additional makeup capacity when the system demani exceeds the capacity of the PDP. On receipt of a safety injection signal, both SI :puIIpS start autanatically.
PDP c:peration is not required for a safety injection.
Followi.n;J the April 7, 1994 Reactor Trip am Safety Injection event, review of the event identified that the PDP was operatin}
prior to the SI am that the PDP did not trip after receipt of the SI signal. Review of the instrumentation am control drawin.;Js oonfinned that the PDP control system was arrarged such that the PDP will not trip on receipt of a SI signal. An evaluation to detennine the effect of the PDP operation durin} a SI was oarpleted by Westin:;Jhouse in August 1994. '!he PDP seal leakage durin} punp operation can significantly increase the site bamdary am control roan dose. '!he Westin;Jhouse evaluation concluded that the increased dose due to PDP seal leakage durin} a IOCA would still meet GDC 19 am 10 CFR 100 requirements as lcn;J as the IDP seal leakage does not exceed 2 gpn. '1he Procedures (EDPs) TNere revised in August 1994 to manually trip the IDP prior to enterin} cold leg recirculation.
On Oct:d:>er 26, 1995, durirg evaluation of an autanatic trip function for the PDP, the issue of the PDP conti.nuirg to operate after a SI signal am its consequerx::es were reviewed for reportability.
rurin} this review, the Westi.Djlouse dose evaluation was detennined to be in error in that it assumed the A'fN system charcoal filter was aligned to provide filtration duri.rg the cold leg recirculation piase of a I.DCA. '!he A'fN system dlarooal filter is not autanatically aligned. Without charcoal filtration, calculated doses increase significantly. when the filter is aligned, the doses may exceed the 10 CFR 100 am the GDC 19 limits. APPARENI' CAUSE OF OCCIJRRENCE
'!he design basis for the operation am control of the PDP is not clearly dcx:::l.llnente in the UFSAR. '1he UFASR does not di saJSS the need to trip the PDP prior to cold leg recirculation durin} a IOCA. '1he incatplete doCl.nnentation of the eve system resulted in plant c:peration in a configuration which was not considered in the UFSAR accident analyses.
'!he desicjn basis documentation for the MN system is not canplete.
'1he :requirement to align the c:harooal filter prior'to cold leg recirculation duri.rg a I.DCA is not specified .iJi the UFSAR. . mIOR SIMIIAR CXXIJRRENCES lll.ere were two previous IERs where the IDP operation was a factor. I.ER 272/94-007-00 addressed the April 7, 1994 Reactor Trip arrl Safety Injection, am 272/94-017-01 addressed Pressurizer overpressure Protection bein;J outside of design basis. NRC FORM 366A (4*95))
-U.S. llJCLEAR REGUl.ATCllY CXMUSSIOll L:ICENSEE EVENT REPORT (LER) TfilIT CXNI'INUATION FACILITY """" (1) DOCKET LER IUllER (6) YEAR I SEQUENTIAL I REVIS[ __ NUMBER ON 95 *-027 .. 00 05000272 SAUM. GENERA'l:U:.G STATION UNIT 1 TEXT (If more space is required, use additional copies of NRC Form 366A> (17) RUOR SIMIIAR OCCIJRRENC&S (cont'd) PAGE (3) 4 OF 4 IER 272/95-017 identified that the operation of the Eme1:'gency Air ccn:li.tionin:;J System (EACS) as it was configured
'WOUld have :resulted in GOC 19 criteria for control roan habitability bei.rg exceeded.
Awareness of this I.ER aided in the identification of the PDP operation possibly exceeding the lOCFRlOO am GOC dose limits. '!\<<> IERs in 1995 identified incidents
'Where the UFSAR am the ac:x::ident analysis were in conflict.
I.ER 272/95-011-00 identified that a discrepancy existed between the UFSAR am the steam line break analysis for the oontairnnent penetration area. I.ER 272/95-016-00 identified a discrepancy
- involvi.rg the oontairnnent structure duri.rg a steam Line Break Analysis ani a Design Basis I.DCA. Both IERs are similar to this I.ER in that a discrepancy existed between the ac:x::ident analysis am the UFSAR. SAFEIY SIGNIFICANCE
'1he operation of the PDP after a lOCA has a direct i.npact on the potential for off-site release of radioactivity.
'lhe deficiency in the design basis could have resulted in site bcumary ani control roan doses exceeding licen.si.rg basis limits duri.rg a lOCA at either Salem Unit. A review of the Westin:]house evaluation revealed that an offsite dose in excess of the lOCFRlOO am GOC 19 limits ooold have ocx:urred a.ssumin;J a IDCA am an mifiltered release (dlarcoal filter not on-line).
'!he design basis sairce tenn values are considered to be conservatively high. Based on the sam:e tenn definition aooepted for the Mvanoed Light water Reactor design, the NRC ani the in:iustry are evaluatin_J the use of ioore :realistic source tenn predictions.
Use of the m:>re :realistic source tenn values in analyzi.rg the operation of the PDP during an SI inlicate that the 10 CFRlOO ani GOC 19 criteria would not likely have been exceeded if an event had occurred.
- 1. '1he EDPs were revised to include steps for manually triwi.rg the PDP prior to ocmnerx::i.ng cold leg recirculation.
- 2. Perfonn a ccmprehensive review of the UFSAR ClJapter 15 ac:x::ident analysis to better ensure the consistency between the design assumptions, am plant configuration am operation.
- 3. Identify am d<x:ument all sources of contaminated leakage, incluclir¥]
a secured PDP, into the .Auxiliary Building.duri.ng a IDCA am incorporate*
in dose calculations.
- 4. Review open items identified in the MN system CBDs to ensure that all issues that could inpa.ct the plant licensing basis have been addressed to ensure no safety concems exist post :restart.
Also, identify inprovements to the MN system aOO,lor revisions to the EDPs necessary to ensure corrplianc:e with lOCFRlOO limit am GOC 19 limit. Incorporate changes into the i.npacted docurmmtation, inch.r:li.rg the UFSAR. Items 2-4 will be ccmpleted prior to restart. NRC FORM 366A (4*95) -. ---;* :-..