ML20059D212: Difference between revisions

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| number = ML20059D212
| number = ML20059D212
| issue date = 08/23/1993
| issue date = 08/23/1993
| title = Intervenor Exhibit I-MFP-210,consisting of Rept, SI-1-8805A, Failed to Cycle on Actuation Signal, Dtd 900827
| title = Intervenor Exhibit I-MFP-210,consisting of Rept, SI-1-8805A, Failed to Cycle on Actuation Signal,
| author name =  
| author name =  
| author affiliation = AFFILIATION NOT ASSIGNED
| author affiliation = AFFILIATION NOT ASSIGNED
Line 11: Line 11:
| contact person =  
| contact person =  
| document report number = OLA-2-I-MFP-210, NUDOCS 9401070071
| document report number = OLA-2-I-MFP-210, NUDOCS 9401070071
| title reference date = 08-27-1990
| document type = EXHIBITS (DOCKETING AND SERVICES BRANCH INFORMATION, LEGAL TRANSCRIPTS & ORDERS & PLEADINGS
| document type = EXHIBITS (DOCKETING AND SERVICES BRANCH INFORMATION, LEGAL TRANSCRIPTS & ORDERS & PLEADINGS
| page count = 8
| page count = 8

Latest revision as of 12:13, 2 June 2023

Intervenor Exhibit I-MFP-210,consisting of Rept, SI-1-8805A, Failed to Cycle on Actuation Signal,
ML20059D212
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 08/23/1993
From:
AFFILIATION NOT ASSIGNED
To:
References
OLA-2-I-MFP-210, NUDOCS 9401070071
Download: ML20059D212 (8)


Text

'

() L i - @ 'Od'i '/Vy4" {'~ Eof 8 30- 2 75 u3 - OLA SI-1-8805A FATLED TO CYCLE ON ACTUATION SIGNAL T-w=h 2/O 8,bslg3 I. Plant Conditions gpggg/g M FC ht A.,

The unit was in Mode 1 (Power Operation)'at 100 percent powe j DCT 28 P6 25 II. Description of Problem s

A. Problem:  % ;n-p ' -

In December, 1982, the motor operator for valve SI-1-8805A was l overhauled as part of the preventative maintenance program for

! Limitorque motor operators.

, On May 25, 1990, at 1416 PDT, Control room operators took the

! control switch for motor controlled valve SI-1-8805A to the open

, position. The valve stroked open. The control switch was then

! taken to the closed position, and the valve stroked close. The control switch was taken back to the open position, and nothing happened. The control room operator was under the impression that.

the breaker had failed to close, and proceeded to cycle the breaker ,

several times. Another attempt was made to stroke the valve .

successfully. One more attempt to stroke the valve failed.

Electrical Maintenance was contacted at 1435 PDT and asked to investigate the problem. ,

An electrician was dispatched to the site. At 1510 PDT the electrician found that the motor was running, and that the-declutch-lever was bouncing up and down. The control room was contacted, requesting the breaker for the motor be opened to shut off.the motor. The motor had been running approximately 50 minutes, and was too hot to touch. Trouble shootino was started on the motor.

At 1738 PDT, a visual inspection at the line starter and terminations found no abnormalities. At 1810 -a visual inspection at the valve was performed. A clearance had been hung _on the valve after the valve was declared inoperable. The control room operator responsible for hanging the clearance said that the valve was not in manual, and that he depressed the declutch lever and verified that the valve was fully closed using the handwheel.

At 1900 PDT the operator cover was removed and an inspection of the motor connections and the torque switch performed. The inspection did not identify any abnormalities. At 1905 PDT, the valve was stroked fully open with no problems. Upon reaching full closed, i i

however, the torque switch failed to open ,and the declutch lever started bouncing. The breaker was opened to shut off the motor. i The brake housing cover was then removed, and the current signature '

l equipment installed. Another attempt to stroke the valve.then failed with no sign of excessive torquing of the motor. The operator was overhauled and the declutch fork was found installed upside down.

On May 27, 1990, at 1827 PDT, troubleshooting, repair, and testing of the motor operator for valve SI-1-8805A was completed, and the valve was declared operable. '

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Page 3 of 8 '

SI-1-8805A FAILED TO CYCLE ON ACTUATION SIGNAL- '

It took eight years for the operator to fail because of aging and '

t stressing of components. With the declutch mechanism installed upside down, the declutch mechanism only partially engages. The partial engagement causes excessive stress on the load bearing surfaces and will eventually cause failure.

B. Inoperable structures, components, or systems that contributed to the problem:

None.

C. Dates and approximate times for major occurrences.  ;

1. December, 1982 Motor operator on SI-1-8805A overhauled and declutch fork

~ installed upside down.

2. May 25, 1990 at 1416 PDT: Event / Discovery date -

SI-1-8805A declared inoperable after motor operator fails to stroke valve. '

3. May 25, 1990 at 1435 PDT: Electrical Maintenance asked to investigate problem with motor operator.
4. May 25, 1990 at 1510 PDT: Electrician found motor I operator still running.

Breaker opened to shut off motor.

5. May 25, 1990 at 1910 PDT: After initial tecubleshocting, valve stroked open successfully, and then failed to shut off while clnsing.

Troubleshooting continued.

6. May 27, 1990 at 1827 PDT: Valve SI-1-8805A declared-operable and returned.to service.

D Other systems or secondary functions affected:

None E. Method of discovery:

The event was immediately apparent to the control' room operators due indications in the control room.

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SI-1-8805A FAILED TO CYCLE ON' ACTUATION SIGNAL Operator. actions:

  1. F. ,

l Operators declared valve SI-1-8805A inoperable and contacted j Electrical Maintenance to investigate the problem.

l G. Safety system responses:

None.

III. Cause of the Problem The following is a systematic analysis of root cause.as required by NPAP C-23, " Technical Review Groups." ,

A. Determination of Cause:

I. Human Factors:

a. Communications Communicatioris occurred in a timely manner between Operations and Electrical Maintenance and within Electrical Maintenance. Communications is not a factor in this.

problem,

b. Procedures Procedureswerefollowed.in-the-handlingoffthe_responseto the motor operator problem. ;A procedural problem existed with the procedures governing work on Limitorque motor operators, as the declutch mechanism was installed upside; down. The procedures used at the time'of the valve overhaul in 1982 did not incluce specific instructions.regarding.the installation of the-declutch' fork.
c. Training Training was a factor in this' problem regarding the training of the technician. responsible for the installation of the declutch mechanism. The technician responsible for.the overhaul had not been specifically trained on rebuilding of Limitorque motor operators because the training did-not exist at the time.
d. Human Error Personnel error was a factor in this problem in that the-declutch mechanism was installed incorrectly by the technician.
e. Management System Management systems.were not involved.in this problem. This is not considered a factor in this problem.

II. Equipment / Material

a. Material Degradation-
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'Page:5_of:8L  ?

' i' SI-1-8805A FAILED T0-CYCLE ON ACTUATION.SIGNALL As a results of the declutch fork =being' installed upside.' .

down-and causing incorrect' operator.. function, the worm gear  !

lugs were found to be worn.

b. Installation The declutch mechanism was installed incorrectly. I Installation is a. factor in this problem.

i C. Immediate Cause:

The technician performing the motor operator overhaul installed.the I declutch mechanism upside down.. 1 D. Root Cause:

l 1. A procedure containing~ appropriate cautions regarding the-  ;

l installation of the declutch fork did not exist in 1982. 1 I

2. Training of the technician in~1982 was not adequate in that a training-program'for the overhauling of Limitorque motor.

operators did not exist. '

IV. Analysis of the Problem A. Safety Analysis: i l

SI-1-8805A is one of two parallel valves which open on a SI signal.

These valves align the Refueling Water Storage-Tank (RWST)'with the-i suction header for the centrifugal charging pumps to-allow' injection-of borated water into'the RCS. .The-operability of either 8805A.or 88058 will allow for sufficient _ flow from the RWST to the'RCS.

Additionally, valve 8805A fully ' opened on an' actuation 3ignal, as required. In the event of an SI signal, SI-1-8805A would have l

perfdtmed its required safety function. Therefore..no. adverse {

consequences resulted from this problem and;the health and safety of the public were not affected by this problem.

B. Reportability:

1. Reviewed under QAP-15.B and determined to be non-conforming in_..

accordance with Section 2.1.2. '

i

2. Reviewed under NUREG 1022 and determined not.to bel reportable in accordance with 10 CFR 50.73(a)(2)(1)(B)'and (C).
3. This problem does not constitute a-10 CFR 21 reporting. problem..
4. This problem does not require reporting via a Network entry because the entry would'not provide any new information.to other facilities.

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Page 6 of 8 SI-1-8805A FAILED T0 CYCLE ON ACTUATION SlGNAL.

t f= 5. Reviewed under 10 CFR 50.9 and determined to be not reportable -

since this event does not have a significant implication for .l public health and safety or common defense and security..

V. Corrective Actions A. Immediate Corrective Actions:

The motor operator was overhauled and all worn parts were j 1.

replaced, and the declutch fork installed correctly. .The motor  !

was also replaced as a prudent measure. .

B. Corrective Actions to Prevent Recurrence: .i

1. Electrical Maintenance Procedure MP E-53.10I, "Limitorque' SMB-000 Valve Operator Maintenance", and MP E-53.10J, "Limitorque SMB-00 and SB-00 Valve Operator Maintenance", have been revised to include caution statements concerning properfinstallation of the declutch fork.
2. Technicians performing work on Limitorque motor:c?erators are now trained on the proper method for overbauling-Limitorque operators, including the correct installation of the declutch fork.
3. Limitorque motor operators are overhauled every 4.5. years as part of the preventative maintenance program. Approximately 60 percent of the Limitorque motor operators ~have been overhauled to date, and the improper installation of the declutch fork has been found in only this operator. This problem is considered an ,

isolated incident, and an immediate inspection-is not considered necessary.

VI. Additiona1 Information A. Failed Components:

None.

B. Previous NCRs on similar problems:

None.

C. Operating Experience Review:

1; NPRDS.

Two entries regarding declutch fork problems were found, H however, the problems with the declutch forks were different.

2. NRC IE Information Notices, Bulletins, generic letters.-  !

None.

l i

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SI-1-8805A FAILED TO CYCLE ON ACTUATION SIGNAL

3. INP0 50ERs and SERs. I i

l None.

l D. Trend Code EM - C - 3 : Electrical Maintenance, Material / Equipment Deficiency, t

Installation EM - B - 1 : Electrical Maintenance, Procedure Deficiency, No Procedure l EM - A - 2 : Electrical Maintene ~ e, Personnel Error, Training Deficiency E. Corrective Action Tracking:

1. All corrective actions are complete. No tracking AR is necessary.

l 1

F. Footnotes and special comments:

INP0 instructions and diagrams regarding overhauling of Limitorque motor operators provide more detail than Limitorque drawings, and clarify the necessary steps to be taken when performing maintenance.

F.

References:

1. Initiating Action Request A0193445.

G. TRG Meeting Minutes:

6/27/90

1. The TRG discussed the problem description ard the chronology.

The overhaul date for the operator will be included in both. (To be provided by M. Fraunheim)

2. The worm gear was removed as an inoperable component that contributed to the problem because the damage to the worm gear lugs was a result of the problem, and not a cause.
3. The causal factor analysis was discussed. Procedures, training and human error are considered factors in this event.
4. The immediate cause was determined to be improper installation '

of the declutch fork. The root causes were determined to be an inadequate overhaul procedure in 1982, and inadequate training in 1982.

5. CAPR were discussed and will include procedure revisions since 1982, training programs initiated since 1982, dnd the recurring overhauls on Limitorque operators. Since 2/3 of the Limitorque operators have been overhauled to date, and this is the only
instance of a declutch fork being installed upside down, this 90ncr\90emn042.ptn 7

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,' Page 8 of 8 SI-1-8805A F4ILED TO CYCLE ON ACTUATION SIGNAL incident is considered isolated. It is not necessary to check every operator in the plant immediMely.

6. The question was posed as to why it took eight years for the operator to fail. The reason for the extended time to failure is due to aging and stressing of components. With the declutch mechanism installed upside down, the declutch mechanism only partially engages. The partial engagement causes excessive stress on the load bearing surfaces and will eventually cause failure.
7. M. Fraunheim to provide verification of date of last overhaul of operator and verification that the caution regarding fork installation was not included in the 1982 procedure. If it was, the TRG will have to reconvene to discuss root cause.

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