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REPORT DATE:          September 13, 1979            REPORTABLE OCCURRENCE 79-35 ISSUE O OCCURRENCE DATE:      Auguse 31, 1979                Page 1 of 3
      -                  FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO P. O. BOX 361 PLATTEVILLE, COLORADO 80651 REPORT NO. 50-267/79-35/01-T-0 Preliminary IDENTIFICATION OF OCCURRENCE:
An engineering field audit and preliminary analysis of a random sample of safety related system piping and associated hangers has found inconsistencies that may Jeopardize the operability of systems In the event of a design basis earthquake.
Due to these inconsistencies, Public Service Company has elected to suspend operation of the Fort St. Vrain Unit No. 1, as of 1800 hours on Septe=ber 1, 1979.
9 An investigation of these inconsistencies is continuing.
This appears to be reportable per Fort St. Vrain Technical Specification AC 7.5.2(a)9.
EVENT DESCRIPTION:
Public Service Co=pany of Colorado has completed the field audit and a prelim-inary engineering analysis of a random sample of as-built safety related piping isometric and associated hanger drawings as committed to in Public Service Con-pany letter P-79161.
The audit included a field verification of the as-built installation of the piping shown on 26 Class I piping isometric drawings and the 94 associated hanger drawings. The general validity of the seismic design inputs documenta-tion on 18 of the isometric drawings and 64 of the hanger drawings was confirmed.
On the remaining eight isometric drawings and 30 hanger drawings, inconsisten-cies judged to be potentially significant were identified between the field installation and the reference documentation.
An analytical evaluation of the noted isometric drawing inconst. "cies indi-cates that they would not result in invalidation of the seismic qu .ification of the piping depicted on the subject iso =e.tric drawing.
Q'3 i 96!
7 909190 3NGt)
 
REPORTABLE OCCURRENCE 79-35 ISSUE O Page 2 of 3 EVENT DESCRIPTION (continued):
An analytical analysis of the inconsistencies identified in the hangers indi-cates that 18 of the hangers of concern fulfill Class I design requirements.
The retaining 12 hangers have inconsistencies that may jeopardize the opera-bility of the associated systems in the event of a design basis earthquake.
Because the sacpling of isometric drawings and associated hangers was made on a rando= basis, no conclusions can be drawn as to the continued operability of those systems or portions of systems required to re=ain operable during and after a design basis earthquake.
On the basis of the results of the audit, Public Service Co=pany of Colorado has determined that the piping systen seistic hanger / support systen for the Class I piping uay not be installed per the design requirements defined in the Final Safety Analysis Report and cay require corrective modifications to bring the "as-built" systems into agreement with the design intent.
Because of the inconsistencies noted, the Public Service Company of Colorado has temporarily suspended operation of the Fort St. Vrain unit as of approxi-cately 1800 hours on September 1,1979.
After further analysis, using more sophisticated analytical methods, it has been deter =ined that none of the systems examined to date are impaired per the Final Safety Analysis Report since the individual hangers are acceptable or, the asso-ciated piping and its remaining hangers would re=ain operable during the de-sign basis earthquake.
CAUSE DESCRIPTION:
The inconsistencies between the design and installation of the various hangers required re-analysis of the piping / hanger systems. The time involved did not allow a final resolution of the problem before a report was submitted. There-fore the plant was shutdown pending outcome of the investigation.
CORRECTIVE ACTION:
The re=aining hangers are being analyzed and the outcone of these analyses along with the corrective actions necessary, will be submitted in a future supplemental repo r t.
                                                                        ,,t  ,    0' to
 
REPORTABLE OCCURRENCE 79-35 ISSLT 0 Page 3 of 3 Prepared by:      /jZ.
Asa B. Reed Technical Services Technician Reviewed by:
g.W.Miali=
(/ Technical Services Supervisor Reviewed by:                b Frank 11. Mathie Operations !!anager Approved by:          %  YM Don Warenbourg          9
                                !!anager, Nuclear Production
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        -              .                                                            LICENSEE EVENT REPORT CONTROL BLOCK: l                    l    l      l    l    l h                  (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) o li            iCI0IFlSl vill @l0l0l-l010                                                        01010 - (010 25l@l4                  26 IlLICENSE1 (2TYPL  l 0Jol@l57 CAT  i
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7            8 9            LICENSEE CODE                14    15                          LICENSE NUM8ER CON'T REPORT
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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h Io        2        y field audit and preliminary engineering analysis of a random sample of as-built                                                                                                1 o    a        i safety related piping drawings showed that several hangers have inconsistencies that                                                                                            I l cay jeopardize the operability of the associated systems in the event of a design                                                                                              j o    4 c    5        I basis earthquake.                          Because of these inconsistencies the Fort St. Vrain unit was shut- l o    e        ! down on September 1,1979. This appears to be reportable per Fort St. Vrain Techni-ol7 Ical Specification AC 7.5.2(a)9. There was no affect on public health or safety.                                                                                                            [
l ota l                                                                                                                                                                                          80 7            8 9 SYSTEY              CAUSE            CAUSE                                                          COYP.            VALVE CCCE                COOE          SUSCCOE                    COMPONENT CODE                      SUBCODE            SUSCOCE o19                                  lZlZlh                          h l A lh {lU lP lO lR lT lh                                                A@                Zjh 7              8                        9        to            11                12              13 -                          18            19                20 S EQUE NTI A L                      QCCU A RENCE            REPORT                        A EVISION gga a0        EVENT YE AR                                  REPORT NO.                              CODE                  WPE                              NO.
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41                42 N l@            l Xlh lX l9 l9 l9 lh 43              44                47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1    0      lThe cause of this nroblem is dasim /f,R *C l otion fernnRis*encies which could ieonar-                                                                                            l 4,    ,, a o, 1      i      Idize the svstems involved.                                    The exact extent of the nrokler is not ver cer*                                                                    I i      ; l investigation is continuinc. When the exact cause is detedned the corrective action t-        3      l will be decided and a revised Licensee Event Recort s ubmi t t ed .                                                                                                              I 4                                                                                                                                                                                          I 1            I 80 7            8 9 ST      S            % POWER                        OTHER STATUS                    h1500 RY                                D'SCOVERY DESCRIPTION t    s l E l@            0 l 3 l 5 l@lo N/A                                              l    l C l@l Hanger Audit 7            8                  '                  1                                            a      45        4a                                                                          80 A8TiviTv CONTENT AMOUNT OF ACTivtTY                                                            LOCATION CF RELE ASE 1    6 RELE ASE@D Z
OF RELE ASEl"                            Zl@l lN/A  "
N/A l
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NUVSER                DESCRIPTICN                                                                            $
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l 0 l 0 l 0 l@l N/A                                                                                        , . (l l      (3l    _    1 m[          _3 80 7            8 9                  11        12
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LOSS OF CA OAVAGE TO FACILITY Q TYDE        DESCRI' TION                    U                                                                                                  f i l~) /
                                                                                                                                                                      ,              (T () ()U U
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w                                        J. W. Gahm              PwCNE:
(30 3) 785-2253                            e NAYE OF PAEPARER                                                                                                                                                        "o p              y}}

Latest revision as of 06:01, 2 February 2020

LER 79-035/01T-0:on 790831,field Audit Analysis Indicated Inconsistencies in Hangers of as-built safety-related Piping.Caused by Design & Installation Inconsistencies. Remaining Hangers Being Analyzed
ML19208B216
Person / Time
Site: Fort Saint Vrain Xcel Energy icon.png
Issue date: 09/13/1979
From: Gahm J
PUBLIC SERVICE CO. OF COLORADO
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
Shared Package
ML19208B217 List:
References
LER-79-035-01T, LER-79-35-1T, NUDOCS 7909190360
Download: ML19208B216 (4)


Text

. .

REPORT DATE: September 13, 1979 REPORTABLE OCCURRENCE 79-35 ISSUE O OCCURRENCE DATE: Auguse 31, 1979 Page 1 of 3

- FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO P. O. BOX 361 PLATTEVILLE, COLORADO 80651 REPORT NO. 50-267/79-35/01-T-0 Preliminary IDENTIFICATION OF OCCURRENCE:

An engineering field audit and preliminary analysis of a random sample of safety related system piping and associated hangers has found inconsistencies that may Jeopardize the operability of systems In the event of a design basis earthquake.

Due to these inconsistencies, Public Service Company has elected to suspend operation of the Fort St. Vrain Unit No. 1, as of 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> on Septe=ber 1, 1979.

9 An investigation of these inconsistencies is continuing.

This appears to be reportable per Fort St. Vrain Technical Specification AC 7.5.2(a)9.

EVENT DESCRIPTION:

Public Service Co=pany of Colorado has completed the field audit and a prelim-inary engineering analysis of a random sample of as-built safety related piping isometric and associated hanger drawings as committed to in Public Service Con-pany letter P-79161.

The audit included a field verification of the as-built installation of the piping shown on 26 Class I piping isometric drawings and the 94 associated hanger drawings. The general validity of the seismic design inputs documenta-tion on 18 of the isometric drawings and 64 of the hanger drawings was confirmed.

On the remaining eight isometric drawings and 30 hanger drawings, inconsisten-cies judged to be potentially significant were identified between the field installation and the reference documentation.

An analytical evaluation of the noted isometric drawing inconst. "cies indi-cates that they would not result in invalidation of the seismic qu .ification of the piping depicted on the subject iso =e.tric drawing.

Q'3 i 96!

7 909190 3NGt)

REPORTABLE OCCURRENCE 79-35 ISSUE O Page 2 of 3 EVENT DESCRIPTION (continued):

An analytical analysis of the inconsistencies identified in the hangers indi-cates that 18 of the hangers of concern fulfill Class I design requirements.

The retaining 12 hangers have inconsistencies that may jeopardize the opera-bility of the associated systems in the event of a design basis earthquake.

Because the sacpling of isometric drawings and associated hangers was made on a rando= basis, no conclusions can be drawn as to the continued operability of those systems or portions of systems required to re=ain operable during and after a design basis earthquake.

On the basis of the results of the audit, Public Service Co=pany of Colorado has determined that the piping systen seistic hanger / support systen for the Class I piping uay not be installed per the design requirements defined in the Final Safety Analysis Report and cay require corrective modifications to bring the "as-built" systems into agreement with the design intent.

Because of the inconsistencies noted, the Public Service Company of Colorado has temporarily suspended operation of the Fort St. Vrain unit as of approxi-cately 1800 hours0.0208 days <br />0.5 hours <br />0.00298 weeks <br />6.849e-4 months <br /> on September 1,1979.

After further analysis, using more sophisticated analytical methods, it has been deter =ined that none of the systems examined to date are impaired per the Final Safety Analysis Report since the individual hangers are acceptable or, the asso-ciated piping and its remaining hangers would re=ain operable during the de-sign basis earthquake.

CAUSE DESCRIPTION:

The inconsistencies between the design and installation of the various hangers required re-analysis of the piping / hanger systems. The time involved did not allow a final resolution of the problem before a report was submitted. There-fore the plant was shutdown pending outcome of the investigation.

CORRECTIVE ACTION:

The re=aining hangers are being analyzed and the outcone of these analyses along with the corrective actions necessary, will be submitted in a future supplemental repo r t.

,,t , 0' to

REPORTABLE OCCURRENCE 79-35 ISSLT 0 Page 3 of 3 Prepared by: /jZ.

Asa B. Reed Technical Services Technician Reviewed by:

g.W.Miali=

(/ Technical Services Supervisor Reviewed by: b Frank 11. Mathie Operations !!anager Approved by:  % YM Don Warenbourg 9

!!anager, Nuclear Production

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(7 77)

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7 8 9 LICENSEE CODE 14 15 LICENSE NUM8ER CON'T REPORT

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EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h Io 2 y field audit and preliminary engineering analysis of a random sample of as-built 1 o a i safety related piping drawings showed that several hangers have inconsistencies that I l cay jeopardize the operability of the associated systems in the event of a design j o 4 c 5 I basis earthquake. Because of these inconsistencies the Fort St. Vrain unit was shut- l o e  ! down on September 1,1979. This appears to be reportable per Fort St. Vrain Techni-ol7 Ical Specification AC 7.5.2(a)9. There was no affect on public health or safety. [

l ota l 80 7 8 9 SYSTEY CAUSE CAUSE COYP. VALVE CCCE COOE SUSCCOE COMPONENT CODE SUBCODE SUSCOCE o19 lZlZlh h l A lh {lU lP lO lR lT lh A@ Zjh 7 8 9 to 11 12 13 - 18 19 20 S EQUE NTI A L QCCU A RENCE REPORT A EVISION gga a0 EVENT YE AR REPORT NO. CODE WPE NO.

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41 42 N l@ l Xlh lX l9 l9 l9 lh 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h 1 0 lThe cause of this nroblem is dasim /f,R *C l otion fernnRis*encies which could ieonar- l 4, ,, a o, 1 i Idize the svstems involved. The exact extent of the nrokler is not ver cer* I i  ; l investigation is continuinc. When the exact cause is detedned the corrective action t- 3 l will be decided and a revised Licensee Event Recort s ubmi t t ed . I 4 I 1 I 80 7 8 9 ST S  % POWER OTHER STATUS h1500 RY D'SCOVERY DESCRIPTION t s l E l@ 0 l 3 l 5 l@lo N/A l l C l@l Hanger Audit 7 8 ' 1 a 45 4a 80 A8TiviTv CONTENT AMOUNT OF ACTivtTY LOCATION CF RELE ASE 1 6 RELE ASE@D Z

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