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{{#Wiki_filter:(7 77)LICENSEE EVENT REPORT CONTROL BLOCK: l llllllh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 M lN l C 1Bk' P l 1 l@15l 0l 0l -l 0l O! 0l O! O ~l0l0l@l4l1 1l 1l 1l@l ll@7 8 9*lTCENSJE ODE 14 LICENSE NUMBER 25 26 LICEs SE TYPE JO
{{#Wiki_filter:(7 77)
$7 CAT $8 CON'T EnN l L l@l 0 l 5 l0 l- 10 l 3 l 2 l5 @l Ol 91 il 7l 7 9hl1l0 l0 l3 [7 l9 lg O 1 7 8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 FtEPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l O 121 lWhile performing PT 19.6.0.2, Visual Inspection of Accessible Snubbers on Safety l@ l Related Systems, the following were found inoperable:
LICENSEE EVENT REPORT CONTROL BLOCK: l 1
: 1) ISW-173SS175, service water l lTITl to discharge canal; 2) 1E11-18SS47, line from RHR heat exchanger to vessel; 3) 1C41-ll0lsl 9SS27, line from SLC pumps to vessel; 4) 1G41-1SS22, fuel pool cooling line to RHR; l0 sl5) IG41-20SS76, fuel pool cooling recirculation line.
l    l    l      l    l 6
I I O I 7 I lTechnical Specifications 3.7.5, 6.9.1.9b l0 all7 8 9 80 DE CODE SU8C E COMPONENT CODE SU8 CODE SU ElS lH l@ Q@
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M lN 7        8 9 l C *lTCENSJE 1Bk' ODEP l 1 l@15l 0l 0l -lLICENSE 14                                0l O!       0l O! O ~l0l0l@l4l1LICEs1l NUMBER                  25      26 1l 1l@l$7 CAT SE TYPE JO l    l@
B O 9 7 8 9 10 11 12 13 18 19 20., SEQUENTI AL OCCURRENCE REPORT REVISION LER/RO EVENT YEAR R EPOR7 NO.
                                                                                                                                                                        $8 CON'T O  1            EnN l L l@l 0 l 5 l0 l- 10 l 3 l 682 l5 @l Ol 91 il 7l 7 9hl1l0 l0 l3 [7 l980 lg                           74      75 7       8                     60           61           DOCKET NUMBER                           69     EVENT DATE                             FtEPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l O 121 lWhile performing PT 19.6.0.2, Visual Inspection of Accessible Snubbers on Safety                                                                                             l
CODE TYPE N O.@ REPOyl217l 9ll_ll 0l 6l 1l y 0l3llL g W 22 23 24 26 27 28 29 30 31 32 KN A O O PLANT M HOURS 22 58 i FOR 8.SUP Lt R MANUFACTURER lB l@34Zl@
@ l Related Systems, the following were found inoperable:                                                                 1) ISW-173SS175, service water l lTITl           to discharge canal; 2) 1E11-18SS47, line from RHR heat exchanger to vessel; 3) 1C41-                                                                                 l l0lsl 9SS27, line from SLC pumps to vessel; 4) 1G41-1SS22, fuel pool cooling line to RHR;                                                                                             l 0  s      l5) IG41-20SS76, fuel pool cooling recirculation line.                                                                                                                 I I O I 7 I lTechnical Specifications 3.7.5, 6.9.1.9b                                                                                                                                   l 0  a      l                                                                                                                                                                      l 7        8 9                                                                                                                                                                     80 DE           CODE           SU8C E                   COMPONENT CODE                 SU8 CODE         SU         E 7
Zl@l Zl@l 0l 0; 0l lNlglY[g A lgl B 2l0l9lg 33 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AP..> CORRECTIVE ACTIONS h i Ol Snubbers ISW-173SS175, and IE11-18SS47 had a low fluid level. These snubbers were li li l l rebuilt with new seals and functionally tested. Snubbers IC41-9SS27. and IG41-ISS?C ITT q and 1G41-20SS76 had loose pipe clamps which allowed the snubbers to slip on their i g pipes. The snubbers were positioned per plant drawings and tightened. Testing of I g l snubbers will continue per Technical Specifications.
O  9 8                      9 lS lH l@ Q@
7 8 9 80 ST S% POWER OTHER STATUS DIS RY DISCOVERY DESCRIPTION y W@ l 0l 0l 0l@lNA ll B l@l Periodic Test lA TIVITY CO TENT RELEASS.D OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE R W @ lZ l@l NA llNAlPERSONNEL EXPOS ES NUMBER TYPF.DESCRIPTION ITTil l O l 0 l 0 l@l z l@l NA l'* '''" PERSONN E t iNauNiES
10        11 B    l@ l S l U l P l 0 l R l T l@ W@ y @
-~" , NUMBER DESCRIPTION ll0l0 0l@lNAlt s 7 8 9 11 12 80'#;5 ESC %^fy'J,''C'''"'@7910180' " ^E Zl@lNAl1 9 7 8 9 10* ' ' '80 iSSuEf@lDISCRiPr!ON O
12             13                           18         19               20
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                                .,                                           SEQUENTI AL                       OCCURRENCE           REPORT                         REVISION LER/RO       EVENT YEAR                               R EPOR7 NO.                           CODE               TYPE                           N O.
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l, N_NA 2 o'8 9 10 68 69 80 g o NAME OF PREPARER
27 0l3l              lL              g             W 28       29           30             31           32 KN A       O             O PLANT           M                           HOURS 22         58 i           FOR       8.     SUP Lt R             MANUFACTURER Zl@           l36 Zl@           l 0l 0; 0l               lNlg            lY[g               A lg l B 2l0l9lg lB 33   l@34Zl@                35                                   37                   40   41             42               43               44               47 CAUSE DESCRIPTION AP..> CORRECTIVE ACTIONS h i O      l Snubbers ISW-173SS175, and IE11-18SS47 had a low fluid level. These snubbers were li li l l rebuilt with new seals and functionally tested. Snubbers IC41-9SS27. and IG41-ISS?C ITT q           and 1G41-20SS76 had loose pipe clamps which allowed the snubbers to slip on their                                                                                   i g               pipes. The snubbers were positioned per plant drawings and tightened. Testing of                                                                                   I g l snubbers will continue per Technical Specifications.
**'*}}
7       8 9                                                                                                                                                                     80 ST       S         % POWER                       OTHER STATUS                 DIS       RY                       DISCOVERY DESCRIPTION y W@ l 0l 0l 0l@lNA                                                                     l      l B l@l Periodic Test                                                               l A TIVITY CO TENT RELEASS.D OF RELEASE                       AMOUNT OF ACTIVITY                                                       LOCATION OF RELEASE R W @ lZ l@l NA                                                                         l            lNA                                                                            l PERSONNEL EXPOS ES NUMBER             TYPF.       DESCRIPTION ITTil*l 'O l 0 l 0 l@l z l@l NA                                                                                                                                                   l PERSONN E t iNauNiES                                                                                                                 ,
                                                                                                                                                            -             ~
NUMBER             DESCRIPTION l
7 t s 8 9 l0l0 0l@l      11       12 NA                                                                                                                            l 80
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                                  %^fy'J,
                                          ''C'''"'
                                                      @                                                             7910180 1 9 7       8 9 Zl@l10                            NA l
                  * ' ' '                                                       ~
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NAME OF PREPARER                                             '       *}}

Latest revision as of 06:10, 2 February 2020

LER 79-061/03L-0:on 790917,various Snubbers on safety- Related Sys Found Inoperable.Caused by Low Fluid Level & Loose Pipe Clamps Leading to Snubber Clippage.Snubbers Positioned Per Plant Drawings & Tightened
ML19209C973
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 10/03/1979
From: Tollison A
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19209C970 List:
References
LER-79-061-03L-01, LER-79-61-3L-1, NUDOCS 7910180534
Download: ML19209C973 (1)


Text

(7 77)

LICENSEE EVENT REPORT CONTROL BLOCK: l 1

l l l l l 6

lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

M lN 7 8 9 l C *lTCENSJE 1Bk' ODEP l 1 l@15l 0l 0l -lLICENSE 14 0l O! 0l O! O ~l0l0l@l4l1LICEs1l NUMBER 25 26 1l 1l@l$7 CAT SE TYPE JO l l@

$8 CON'T O 1 EnN l L l@l 0 l 5 l0 l- 10 l 3 l 682 l5 @l Ol 91 il 7l 7 9hl1l0 l0 l3 [7 l980 lg 74 75 7 8 60 61 DOCKET NUMBER 69 EVENT DATE FtEPORT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h l O 121 lWhile performing PT 19.6.0.2, Visual Inspection of Accessible Snubbers on Safety l

@ l Related Systems, the following were found inoperable: 1) ISW-173SS175, service water l lTITl to discharge canal; 2) 1E11-18SS47, line from RHR heat exchanger to vessel; 3) 1C41- l l0lsl 9SS27, line from SLC pumps to vessel; 4) 1G41-1SS22, fuel pool cooling line to RHR; l 0 s l5) IG41-20SS76, fuel pool cooling recirculation line. I I O I 7 I lTechnical Specifications 3.7.5, 6.9.1.9b l 0 a l l 7 8 9 80 DE CODE SU8C E COMPONENT CODE SU8 CODE SU E 7

O 9 8 9 lS lH l@ Q@

10 11 B l@ l S l U l P l 0 l R l T l@ W@ y @

12 13 18 19 20

., SEQUENTI AL OCCURRENCE REPORT REVISION LER/RO EVENT YEAR R EPOR7 NO. CODE TYPE N O.

@ REPOy l217l229l l_l 23 l 0l 6l 1l 24 26 y

27 0l3l lL g W 28 29 30 31 32 KN A O O PLANT M HOURS 22 58 i FOR 8. SUP Lt R MANUFACTURER Zl@ l36 Zl@ l 0l 0; 0l lNlg lY[g A lg l B 2l0l9lg lB 33 l@34Zl@ 35 37 40 41 42 43 44 47 CAUSE DESCRIPTION AP..> CORRECTIVE ACTIONS h i O l Snubbers ISW-173SS175, and IE11-18SS47 had a low fluid level. These snubbers were li li l l rebuilt with new seals and functionally tested. Snubbers IC41-9SS27. and IG41-ISS?C ITT q and 1G41-20SS76 had loose pipe clamps which allowed the snubbers to slip on their i g pipes. The snubbers were positioned per plant drawings and tightened. Testing of I g l snubbers will continue per Technical Specifications.

7 8 9 80 ST S  % POWER OTHER STATUS DIS RY DISCOVERY DESCRIPTION y W@ l 0l 0l 0l@lNA l l B l@l Periodic Test l A TIVITY CO TENT RELEASS.D OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE R W @ lZ l@l NA l lNA l PERSONNEL EXPOS ES NUMBER TYPF. DESCRIPTION ITTil*l 'O l 0 l 0 l@l z l@l NA l PERSONN E t iNauNiES ,

- ~

NUMBER DESCRIPTION l

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NAME OF PREPARER ' *