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{{#Wiki_filter:NllCFormlll (SJ.&) LICENSEE EVENT REPORT CLEAi U.1. NUCLEAll lll!OULATOllV COllM*ION  
{{#Wiki_filter:NllCFormlll                                                                                                                                                     U.1. NUCLEAll lll!OULATOllV COllM*ION (SJ.&)
"""'OVED OMe NO. 311111-0ICM EXPlllEI:
                                                                                                                                                                        """'OVED OMe NO. 311111-0ICM EXPlllEI: 1/31111 LICENSEE EVENT REPORT CLEAi DOCICIT _ _ . .. 121                I      ** 0    fa I
1/31111 l'ACILITV NAME (1) Salem Generatinq Station -Unit 2 I DOCICIT __. .. 121 I **0* fa o I 5 I o 1 o I o 13 11 11 I 1 I oFI o 1 4 TITLI I .. T. S. Fune. Surv. 4.3.3.9.1.b.performed late due to inad. admin. controls IVINT DATI UH OTHlll FACILITIU INVOLVED Ill MONTH QAY YEAR YEAR fACI L.ITY NAMU DOCKET NUMBER(S)
l'ACILITV NAME (1)
Salem Unit 1 1 12 2 I 3 a 7 a I 7 Ol'lllATINO THll llEl'OllT II 1U911TTID l'UlllUANT TO THE llEOUllllMINTS OF 10 Cl'll §: (Checlt -or,,,.,,..
* Salem Generatinq Station - Unit 2                                                                                                                 o I 5 I o 1o I o 13 11 11 I 1 IoFI                  o14 TITLI I..
of 1M fol-,,.J 1111 MOOllll 20.4021111 20.40llal I0.71f8112111wl 7J.7111tl l'OWlll I 20.40ll*ll1 llll ---I0.*1*1111 LIVEL .._
T. S. Fune. Surv. 4.3.3.9.1.b.performed late due to inad. admin. controls IVINT DATI UH                                                                                                                       OTHlll FACILITIU INVOLVED Ill MONTH       QAY         YEAR     YEAR                                                                                         fACI L.ITY NAMU                       DOCKET NUMBER(S)
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Salem Unit 1 1 12 2 I 3               a     7   aI 7 THll llEl'OllT II 1U911TTID l'UlllUANT TO THE llEOUllllMINTS OF 10 Cl'll             §:                 or,,,.,,.. of 1M fol-,,.J 1111 lj"T;;;;;;:;-----------.~r::-:::~:.:.:.:.=:::..:.:.:.::...:.:..:::.:;~;:=:::.=::.;:;:::.::.::.:::::.:::::~;.."T"----------------1 Ol'lllATINO                                                                                                        (Checlt -
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--ll0.731oll211HO LICENll!E CONTACT FOii THll LEll 1121 NAME M. J. Pollack -LER Coordinator
                                                                              --      20.40llal
*.7Slol1211*1 iii.'i'iflil(jJlwiil
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*.n1o11211w1111111 I0.7Sloll211*1 AREA COD! 7J.711*1 OTHEll (Sp<<lfy ,_,_end 111 Tea:t, NllC Fann 3tlflAJ TELEl'HONE NUMIER 6 10 19 3 13 19 1-I 4 1 01 21 2 .
                                                                                      =>.=t*IC:I                               iii.'i'iflil(jJlwiil                            OTHEll (Sp<<lfy  In~
Ol\I;; LIN!< FOR lilACH COilrONli!in' l'AILUlll!
                                                                                                                                                                                ,_,_end 111 Tea:t, NllC Fann
DllClllHD IN THll lllPOllT 11,. CAUSE SYSTEM COMPONENT I I I I I I I I MANUFAC TUR ER I I I I I I
-==:~:::
* IUl'PLEMll!NTAL llEl'OllT l!!Xl'ICTID 1141 n VES (If....,, t:atnp/IN EXl'ECTED SVIJMISSION DATE/ rx, NO SYSTEM COMl'ONENT I I I I I I I I MANUFAC TUR ER I I I I I I EXPECTED MONTH DAV YiiOAR SUIMl .. ION DATE 1111i I I I On December 23, 1987 at 0825 hours, it was discovered that the required functional test for both Unit 1 and Unit 2 Waste Gas Oxygen Monitors were not performed within their required time frame. Technical Specification Surveillance 4.3.3.9.1.b.
ll0.73Cllll21111                        *.7"911211wlllllAI                              3tlflAJ K..
requires the performance of this functional test every 31 days. The root cause of this event has been attributed to inadequate adminstrative controls associated with the implementation of the new computer based work activity system, MMIS. Technical Specification surveillance 4.3.3.9.1.b was not scheduled and performed as required due to a misinterpretation of the scheduling responsibilities.-
NAME
The required functional surveillances were succesfully completed on 12/23/87.
                                                                              -       ll0.73Cllll211MI ll0.731oll211HO LICENll!E CONTACT FOii THll LEll 1121
A review of Chemistry Department Technical Specification required surveillances, during the period in question, was conducted.
                                                                                                                      -       *.n1o11211w1111111 I0.7Sloll211*1 TELEl'HONE NUMIER AREA COD!
No additional missed surveillances were discovered.
M. J. Pollack - LER Coordinator                                                                                                                        6 10 19 3 13 19 1- I 4 1 01 21 2
This event wili be reviewed with all Chemistry Department supervision by Chemistry Department management.
                                                  . CC:.;:>L~li! Ol\I;; LIN!< FOR lilACH COilrONli!in' l'AILUlll! DllClllHD IN THll lllPOllT 11,.
Administrative concerns associated with the implementation of the new MMIS system are being reviewed and addressed.
CAUSE SYSTEM             COMPONENT           MANUFAC                                                                                                    MANUFAC TUR ER                                                          SYSTEM        COMl'ONENT TUR ER I           I   I   I         I     I   I                                                         I           I      I      I          I  I    I I            I I      I          I    I    I                                                        I            I     I     I         I   I   I
The corrective actions associated with these administrative concerns will prevent of this type event. NllCFennlll 111-631 8802020195 880122 PDR ADOCK 05000311 S PDR LICENSEE EVENT REPORT (LER)
                                                      *IUl'PLEMll!NTAL llEl'OllT l!!Xl'ICTID 1141                                                                                   MONTH    DAV        YiiOAR rx, EXPECTED n       VES (If....,, t:atnp/IN EXl'ECTED SVIJMISSION DATE/                                         NO SUIMl. .ION DATE 1111i I       I           I On December 23, 1987 at 0825 hours, it was discovered that the required functional test for both Unit 1 and Unit 2 Waste Gas Oxygen Monitors were not performed within their required time frame.
CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 PLANT AND SYSTEM IDENTIFICATION:
Technical Specification Surveillance 4.3.3.9.1.b. requires the performance of this functional test every 31 days. The root cause of this event has been attributed to inadequate adminstrative controls associated with the implementation of the new computer based work activity system, MMIS. Technical Specification surveillance 4.3.3.9.1.b was not scheduled and performed as required due to a misinterpretation of the scheduling responsibilities.- The required functional surveillances were succesfully completed on 12/23/87. A review of Chemistry Department Technical Specification required surveillances, during the period in question, was conducted. No additional missed surveillances were discovered. This event wili be reviewed with all Chemistry Department supervision by Chemistry Department management. Administrative concerns associated with the implementation of the new MMIS system are being reviewed and addressed. The corrective actions associated with these administrative concerns will prevent ~ecurrence of this type event.
Westinghouse  
8802020195 880122 PDR ADOCK 05000311 NllCFennlll S                                         PDR 111-631
-Pressurized Water Reactor LER NUMBER 87-018-00 PAGE 2 of 4 Energy Industry Identification System (EIIS) codes are identified in the text as f xxl IDENTIFICATION OF OCCURRENCE:
 
Technical Specification Functional Surveillance 4.3.3.9.1.b Performed Late Due to Inadequate Administrative Controls Discovery Date: 12/23/87 Report Date: 1/22/88 This report was initiated by Incident Report No. 87-504. CONDITIONS PRIOR TO OCCURRENCE:
LICENSEE EVENT REPORT (LER) T~XT CONTINUATION Salem Generating Station       DOCKET NUMBER    LER NUMBER      PAGE Unit 2                           5000311         87-018-00      2 of 4 PLANT AND SYSTEM IDENTIFICATION:
Unit 1: Unit 2: Mode 5 Mode 1 Reactor Power 0% -Unit Load 0 MWe Reactor Power 100% -Unit Load 1150 MWe DESCRIPTION OF OCCURRENCE:
Westinghouse   - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as f xxl IDENTIFICATION OF OCCURRENCE:
On December 23, 1987 at 0825 hours, it was discovered that the required functional test for both Unit 1 and Unit 2 Waste Gas Oxygen Monitors were not performed within their required time frame. Technical Specification Surveillance 4.3.3.9.1.b.
Technical Specification Functional Surveillance 4.3.3.9.1.b Performed Late Due to Inadequate Administrative Controls Discovery Date:   12/23/87 Report Date:   1/22/88 This report was initiated by Incident Report No. 87-504.
requires the performance of this functional test every 31 days. The Unit 1 and Unit 2 monitors' functional surveillances were required to be done as of November 8, 1987 and December 6, 1987, respectively.
CONDITIONS PRIOR TO OCCURRENCE:
The Unit 1 and Unit 2 monitors' functional surveillances were completed on December 23, 1987. The Unit 1 November surveillance functional was not performed since the monitor required maintenance worke The Unit 1 and Unit 2 waste gas monitoring systems are cross connected such that either Unit's monitor will satisfy the Technical Specification monitoring requirements.
Unit 1: Mode 5   Reactor Power 0% - Unit Load 0 MWe Unit 2:  Mode 1    Reactor Power 100% - Unit Load 1150 MWe DESCRIPTION OF OCCURRENCE:
Therefore, the Unit 2 monitor satisfied the November monitoring requirements for Unit 1. APPARENT CAUSE OF OCCURRENCE:
On December 23, 1987 at 0825 hours, it was discovered that the required functional test for both Unit 1 and Unit 2 Waste Gas Oxygen Monitors were not performed within their required time frame.
The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work activity system, Managed Maintenance Information System (MMIS). Technical Specification surveillance 4.3.3.9.1.b was not scheduled and performed as required due to a misinterpretation of the scheduling responsibilities.
Technical Specification Surveillance 4.3.3.9.1.b. requires the performance of this functional test every 31 days.
Prior to the September 22, 1987 issuance of revision 8 to station Administrative Procedure AP-12, "Technical Specification Surveillance Program", Chemistry surveillances were scheduled by an internal Chemistry Department system. When the transition was made to fully LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 APPARENT CAUSE OF OCCURRENCE: (cont'd) LER NUMBER 87-018-00 PAGE 3 of 4 implement the MMIS, as per AP-12 Rev. 8, the transfer of Chemistry Department surveillance scheduling responsibilities was not clearly defined. In March 1987, the Station Planning Department began issuing "Daily Scheduling Reports" which identified those work activities (including surveillances) which were due within the following three days. This report was issued as an interdepartmental aid for scheduling work * . Chemistry supervision used this report for scheduling this surveillance, subsequently dispencing with their internal tracking system.* At the on-set of the Unit 1 refueling outage, Station Planning replaced this report with a report which only addressed the Unit 1 refueling outage related activities.
The Unit 1 and Unit 2 monitors' functional surveillances were required to be done as of November 8, 1987 and December 6, 1987, respectively. The Unit 1 and Unit 2 monitors' functional surveillances were completed on December 23, 1987. The Unit 1 November surveillance functional was not performed since the monitor required maintenance worke The Unit 1 and Unit 2 waste gas monitoring systems are cross connected such that either Unit's monitor will satisfy the Technical Specification monitoring requirements. Therefore, the Unit 2 monitor satisfied the November monitoring requirements for Unit 1.
Chemistry supervision subsequently missed the oxygen monitor functional surveillance.
APPARENT CAUSE OF OCCURRENCE:
The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work activity system, Managed Maintenance Information System (MMIS).
Technical Specification surveillance 4.3.3.9.1.b was not scheduled and performed as required due to a misinterpretation of the scheduling responsibilities.
Prior to the September 22, 1987 issuance of revision 8 to station Administrative Procedure AP-12, "Technical Specification Surveillance Program", Chemistry surveillances were scheduled by an internal Chemistry Department system. When the transition was made to fully
 
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station         DOCKET NUMBER    LER NUMBER        PAGE Unit 2                             5000311         87-018-00        3 of 4 APPARENT CAUSE OF OCCURRENCE:     (cont'd) implement the MMIS, as per AP-12 Rev. 8, the transfer of Chemistry Department surveillance scheduling responsibilities was not clearly defined.
In March 1987, the Station Planning Department began issuing "Daily Scheduling Reports" which identified those work activities (including surveillances) which were due within the following three days. This report was issued as an interdepartmental aid for scheduling work *
    . Chemistry supervision used this report for scheduling this surveillance, subsequently dispencing with their internal tracking system.* At the on-set of the Unit 1 refueling outage, Station Planning replaced this report with a report which only addressed the Unit 1 refueling outage related activities. Chemistry supervision subsequently missed the oxygen monitor functional surveillance.
ANALYSIS OF OCCURRENCE:
ANALYSIS OF OCCURRENCE:
The Waste Gas Holdup System oxygen monitors are used to identify increased ievels of oxygen before a potentially explosive mixture develops.
The Waste Gas Holdup System oxygen monitors are used to identify increased ievels of oxygen before a potentially explosive mixture develops. Contained within the Waste Gas Holdup System is hydrogen.
Contained within the Waste Gas Holdup System is hydrogen.
Hydrogen enters the system as a result of normal plant operations.
Hydrogen enters the system as a result of normal plant operations.
The mixture of hydrogen with sufficient levels of oxygen is explosive.
The mixture of hydrogen with sufficient levels of oxygen is explosive.
The periodic functional test of the oxygen monitors ensures their continued acceptable operation.
The periodic functional test of the oxygen monitors ensures their continued acceptable operation. The late functional surveillance was successful. No corrective maintenance was required based upon the results of the functional test. No problems with the Unit 2 Waste Gas Oxygen Monitor were indicated by a review of the Incident Reports for the period between December 6, 1987 and December 23, 1987.
The late functional surveillance was successful.
However, this event is reportable to the Nuclear Regulatory Commission in accordance with 10CFR 50.73(a) (2) (i) (B) since the monitors were not surveilled within the required time frame of Technical Specification 4.3.3.9.1.b.
No corrective maintenance was required based upon the results of the functional test. No problems with the Unit 2 Waste Gas Oxygen Monitor were indicated by a review of the Incident Reports for the period between December 6, 1987 and December 23, 1987. However, this event is reportable to the Nuclear Regulatory Commission in accordance with lOCFR 50.73(a) (2) (i) (B) since the monitors were not surveilled within the required time frame of Technical Specification 4.3.3.9.1.b.
CORRECTIVE ACTION:
CORRECTIVE ACTION: The required functional surveillances for both Units' monitors was successfully completed on December 23, 1987. A review of all Chemistry Department Technical Specification required surveillances, during the period when Station Planning was not providing the "Daily Scheduling Report", was conducted.
The required functional surveillances for both Units' monitors was successfully completed on December 23, 1987.
No other missed surveiilances were discovered.
A review of all Chemistry Department Technical Specification required surveillances, during the period when Station Planning was not providing the "Daily Scheduling Report", was conducted. No other missed surveiilances were discovered. Therefore, this event is considered an isolated occurrence.
Therefore, this event is considered an isolated occurrence.
This event will be reviewed with all Chemistry Department supervision by Chemistry Department management.
This event will be reviewed with all Chemistry Department supervision by Chemistry Department management.
Administrative concerns associated with the implementation of the new I . .. LICENSEE EVENT REPORT CLER) TEXT CONTINUATION Salem Generating Station Unit 2 CORRECTIVE ACTION: (cont'd) DOCKET NUMBER 5000311 LER NUMBER 87-018-00 PAGE 4 of 4 MMIS system are being reviewed and addressed.
Administrative concerns associated with the implementation of the new
The corrective actions associated with these administrative concerns will prevent recurrence of this type event. G9.::i:a:!:9  
 
' Salem Operations MJP:pc SORC Mtg. 88-008 Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555  
LICENSEE EVENT REPORT CLER) TEXT CONTINUATION I
Salem Generating Station     DOCKET NUMBER     LER NUMBER       PAGE Unit 2                          5000311        87-018-00       4 of 4 CORRECTIVE ACTION:  (cont'd)
MMIS system are being reviewed and addressed. The corrective actions associated with these administrative concerns will prevent recurrence of this type event.
G9.::i:a:!:9 '
Salem Operations MJP:pc SORC Mtg. 88-008
 
Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station January 22, 1988 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC               20555


==Dear Sir:==
==Dear Sir:==
SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 87-018-00 January 22, 1988 This Licensee Event Report is being submitted pursuant to the requirements of lOCFR 50.73(a) (2) (i) (B). This report is required within thirty (30) days of discovery.
 
MJP:pc Distribution Sincerely yours, General Salem Operations}}
SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 87-018-00 This Licensee Event Report is being submitted pursuant to the requirements of 10CFR 50.73(a) (2) (i) (B). This report is required within thirty (30) days of discovery.
Sincerely yours, General Manager-Salem Operations MJP:pc Distribution}}

Latest revision as of 07:47, 3 February 2020

LER 87-018-00:on 871223,discovered That Required Functional Test for Waste Gas Oxygen Monitors Performed Late.Caused by Inadequate Administrative Controls.Required Functional Surveillances Sucessfully Completed on 871223.W/880122 Ltr
ML18093A602
Person / Time
Site: Salem PSEG icon.png
Issue date: 01/22/1988
From: Pollack M, Zupko J
Public Service Enterprise Group
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
LER-87-018-02, LER-87-18-2, NUDOCS 8802020195
Download: ML18093A602 (5)


Text

NllCFormlll U.1. NUCLEAll lll!OULATOllV COllM*ION (SJ.&)

"""'OVED OMe NO. 311111-0ICM EXPlllEI: 1/31111 LICENSEE EVENT REPORT CLEAi DOCICIT _ _ . .. 121 I ** 0 fa I

l'ACILITV NAME (1)

  • Salem Generatinq Station - Unit 2 o I 5 I o 1o I o 13 11 11 I 1 IoFI o14 TITLI I..

T. S. Fune. Surv. 4.3.3.9.1.b.performed late due to inad. admin. controls IVINT DATI UH OTHlll FACILITIU INVOLVED Ill MONTH QAY YEAR YEAR fACI L.ITY NAMU DOCKET NUMBER(S)

Salem Unit 1 1 12 2 I 3 a 7 aI 7 THll llEl'OllT II 1U911TTID l'UlllUANT TO THE llEOUllllMINTS OF 10 Cl'll §: or,,,.,,.. of 1M fol-,,.J 1111 lj"T;;;;;;:;-----------.~r::-:::~:.:.:.:.=:::..:.:.:.::...:.:..:::.:;~;:=:::.=::.;:;:::.::.::.:::::.:::::~;.."T"----------------1 Ol'lllATINO (Checlt -

MOOllll I

1-----.....,.----.&..:::~-l 20.4021111

-- 20.40llal

-- I0.71f8112111wl 7J.7111tl l'OWlll 20.40ll*ll1 llll I0.*1*1111 *.7Slol1211*1 7J.711*1 LIVEL .._

~~111!~1~~1.,.il!o,!01;....,..10.4--l :!l!.@!!!!oll1llSI

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,_,_end 111 Tea:t, NllC Fann

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NAME

- ll0.73Cllll211MI ll0.731oll211HO LICENll!E CONTACT FOii THll LEll 1121

- *.n1o11211w1111111 I0.7Sloll211*1 TELEl'HONE NUMIER AREA COD!

M. J. Pollack - LER Coordinator 6 10 19 3 13 19 1- I 4 1 01 21 2

. CC:.;:>L~li! Ol\I;; LIN!< FOR lilACH COilrONli!in' l'AILUlll! DllClllHD IN THll lllPOllT 11,.

CAUSE SYSTEM COMPONENT MANUFAC MANUFAC TUR ER SYSTEM COMl'ONENT TUR ER I I I I I I I I I I I I I I I I I I I I I I I I I I I I

  • IUl'PLEMll!NTAL llEl'OllT l!!Xl'ICTID 1141 MONTH DAV YiiOAR rx, EXPECTED n VES (If....,, t:atnp/IN EXl'ECTED SVIJMISSION DATE/ NO SUIMl. .ION DATE 1111i I I I On December 23, 1987 at 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br />, it was discovered that the required functional test for both Unit 1 and Unit 2 Waste Gas Oxygen Monitors were not performed within their required time frame.

Technical Specification Surveillance 4.3.3.9.1.b. requires the performance of this functional test every 31 days. The root cause of this event has been attributed to inadequate adminstrative controls associated with the implementation of the new computer based work activity system, MMIS. Technical Specification surveillance 4.3.3.9.1.b was not scheduled and performed as required due to a misinterpretation of the scheduling responsibilities.- The required functional surveillances were succesfully completed on 12/23/87. A review of Chemistry Department Technical Specification required surveillances, during the period in question, was conducted. No additional missed surveillances were discovered. This event wili be reviewed with all Chemistry Department supervision by Chemistry Department management. Administrative concerns associated with the implementation of the new MMIS system are being reviewed and addressed. The corrective actions associated with these administrative concerns will prevent ~ecurrence of this type event.

8802020195 880122 PDR ADOCK 05000311 NllCFennlll S PDR 111-631

LICENSEE EVENT REPORT (LER) T~XT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 87-018-00 2 of 4 PLANT AND SYSTEM IDENTIFICATION:

Westinghouse - Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as f xxl IDENTIFICATION OF OCCURRENCE:

Technical Specification Functional Surveillance 4.3.3.9.1.b Performed Late Due to Inadequate Administrative Controls Discovery Date: 12/23/87 Report Date: 1/22/88 This report was initiated by Incident Report No.87-504.

CONDITIONS PRIOR TO OCCURRENCE:

Unit 1: Mode 5 Reactor Power 0% - Unit Load 0 MWe Unit 2: Mode 1 Reactor Power 100% - Unit Load 1150 MWe DESCRIPTION OF OCCURRENCE:

On December 23, 1987 at 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br />, it was discovered that the required functional test for both Unit 1 and Unit 2 Waste Gas Oxygen Monitors were not performed within their required time frame.

Technical Specification Surveillance 4.3.3.9.1.b. requires the performance of this functional test every 31 days.

The Unit 1 and Unit 2 monitors' functional surveillances were required to be done as of November 8, 1987 and December 6, 1987, respectively. The Unit 1 and Unit 2 monitors' functional surveillances were completed on December 23, 1987. The Unit 1 November surveillance functional was not performed since the monitor required maintenance worke The Unit 1 and Unit 2 waste gas monitoring systems are cross connected such that either Unit's monitor will satisfy the Technical Specification monitoring requirements. Therefore, the Unit 2 monitor satisfied the November monitoring requirements for Unit 1.

APPARENT CAUSE OF OCCURRENCE:

The root cause of this event has been attributed to inadequate administrative controls associated with the new computer based work activity system, Managed Maintenance Information System (MMIS).

Technical Specification surveillance 4.3.3.9.1.b was not scheduled and performed as required due to a misinterpretation of the scheduling responsibilities.

Prior to the September 22, 1987 issuance of revision 8 to station Administrative Procedure AP-12, "Technical Specification Surveillance Program", Chemistry surveillances were scheduled by an internal Chemistry Department system. When the transition was made to fully

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 87-018-00 3 of 4 APPARENT CAUSE OF OCCURRENCE: (cont'd) implement the MMIS, as per AP-12 Rev. 8, the transfer of Chemistry Department surveillance scheduling responsibilities was not clearly defined.

In March 1987, the Station Planning Department began issuing "Daily Scheduling Reports" which identified those work activities (including surveillances) which were due within the following three days. This report was issued as an interdepartmental aid for scheduling work *

. Chemistry supervision used this report for scheduling this surveillance, subsequently dispencing with their internal tracking system.* At the on-set of the Unit 1 refueling outage, Station Planning replaced this report with a report which only addressed the Unit 1 refueling outage related activities. Chemistry supervision subsequently missed the oxygen monitor functional surveillance.

ANALYSIS OF OCCURRENCE:

The Waste Gas Holdup System oxygen monitors are used to identify increased ievels of oxygen before a potentially explosive mixture develops. Contained within the Waste Gas Holdup System is hydrogen.

Hydrogen enters the system as a result of normal plant operations.

The mixture of hydrogen with sufficient levels of oxygen is explosive.

The periodic functional test of the oxygen monitors ensures their continued acceptable operation. The late functional surveillance was successful. No corrective maintenance was required based upon the results of the functional test. No problems with the Unit 2 Waste Gas Oxygen Monitor were indicated by a review of the Incident Reports for the period between December 6, 1987 and December 23, 1987.

However, this event is reportable to the Nuclear Regulatory Commission in accordance with 10CFR 50.73(a) (2) (i) (B) since the monitors were not surveilled within the required time frame of Technical Specification 4.3.3.9.1.b.

CORRECTIVE ACTION:

The required functional surveillances for both Units' monitors was successfully completed on December 23, 1987.

A review of all Chemistry Department Technical Specification required surveillances, during the period when Station Planning was not providing the "Daily Scheduling Report", was conducted. No other missed surveiilances were discovered. Therefore, this event is considered an isolated occurrence.

This event will be reviewed with all Chemistry Department supervision by Chemistry Department management.

Administrative concerns associated with the implementation of the new

LICENSEE EVENT REPORT CLER) TEXT CONTINUATION I

Salem Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 2 5000311 87-018-00 4 of 4 CORRECTIVE ACTION: (cont'd)

MMIS system are being reviewed and addressed. The corrective actions associated with these administrative concerns will prevent recurrence of this type event.

G9.::i:a:!:9 '

Salem Operations MJP:pc SORC Mtg.88-008

Public Service Electric and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station January 22, 1988 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Dear Sir:

SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT 87-018-00 This Licensee Event Report is being submitted pursuant to the requirements of 10CFR 50.73(a) (2) (i) (B). This report is required within thirty (30) days of discovery.

Sincerely yours, General Manager-Salem Operations MJP:pc Distribution