|
|
(6 intermediate revisions by the same user not shown) |
Line 3: |
Line 3: |
| | issue date = 01/05/1993 | | | issue date = 01/05/1993 |
| | title = LER 92-025-00:on 921206,identified That Analog Rod Position Indications for CR in Violation of TS 3.0.3.Caused by Equipment Failure.Work Order Has Been Initiated to Replace 2DI & 1D4 Signal Conditioning modules.W/930105 Ltr | | | title = LER 92-025-00:on 921206,identified That Analog Rod Position Indications for CR in Violation of TS 3.0.3.Caused by Equipment Failure.Work Order Has Been Initiated to Replace 2DI & 1D4 Signal Conditioning modules.W/930105 Ltr |
| | author name = POLLACK M J, VONDRA C A | | | author name = Pollack M, Vondra C |
| | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY | | | author affiliation = PUBLIC SERVICE ELECTRIC & GAS CO. OF NEW JERSEY |
| | addressee name = | | | addressee name = |
Line 16: |
Line 16: |
|
| |
|
| =Text= | | =Text= |
| {{#Wiki_filter:. --- | | {{#Wiki_filter:. |
| Pui'..1ic Service Electric *and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station u. s. Nuclear Regulatory Commission Document control Desk Washington, DC 20555 | | PS~G Pui'..1ic Service Electric *and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station January 5, 1993 |
| | : u. s. Nuclear Regulatory Commission Document control Desk Washington, DC 20555 |
|
| |
|
| ==Dear Sir:== | | ==Dear Sir:== |
| SALEM GENERATING STATION . LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 92-025-00 January 5, 1993 Licensee Event requirements of 50.73(a) (2).(i) (B). thirty ( 3 O) days of Report is being submitted pursuant*
| |
| to the Code of Federal Regulations lOCFR This report is required to be issued within event discovery.
| |
| -MJP:pc Distribution 9.301070182 930105 . PDR ADOCK 05000272 PDR s Sincerely yours, . ;/ f i //) . /
| |
| c .. A Vondra -General.Manager
| |
| -Salem Operations
| |
| / If I 1-fe!" -.(i l\lRC FOR!l;! 366 .U.S. NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO. 3150-0104 (6-891 , EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE .TO COMPLY WTH THIS LICENSEE EVENT-REPORT (LER) INFORMATION COlLECTION REQUEST: 50.0 HRS; FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS . AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR .. REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO .I THE PAPERWORK R'EDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDG.ET, WASHINGTON, DC 20503. ** FACILITY NAME (1) I DOCK.ET NUMBER (2) I PAGE 131 Salem Generating Sta ti op -Unit 1 01s1010101 21 712 , OF 0 I 4 TITLE (4) -Tee:h Snee 3.0.3 entry; more than one analog rod position indicator per bank .. tl.npperable.
| |
| EVENT DATE 15.l* LER NUMBER (6) REPORT DATE (71 OTHER FACILITIES INVOLVED (81 MONTH DAY YEAR YEAR *:*:*:*:*:*
| |
| SEQUENTIAL
| |
| ::::::::::
| |
| REVISION MONTH DAY YEAR FACILITY NAMES DOCKET NUMBERISI
| |
| *.*.*.*.*.*
| |
| NUMBER :::::;::::
| |
| NUMBER i> 1 s Io Io* I o I I I -11 ol6 91 2 -ol 2 Is -o lo 0!1 ol s 91 2 9 *2 2 0 I 5 I 0 I 0 I 0 I I I OPERATING THIS REPORT IS SUBMITTED*PURSUANT TO THE OF 10 CFR §: (Chock one or more of the following)
| |
| (111 MODE (9) 1 20.402(b) 20.405(cl 50.73(1)(2)(iv) 73.71(b) l 1; ,....__ ,_ ,....__ -POWER 20.406(11(1 llil 60.38(c)(1) 50.73(1)(2)(v) 73.71 (cl *LEVEL ----,....__ (10) 010 20.406(1)(1 l(ii) 50.38(c)(2) 50.73(1)(2)(vii)
| |
| OTHER (Spacify in Abstract ---.....,.....
| |
| below tJnd in Toxr, NRC Form 20.406(1)(1 l(iii) x 50.73(1112Hil 60.73111(2)(viii)(AI 366A) ----20.405(1)(1 l(lv) 60.73(1)(2l(ii) 50.73(11(2)(viii)(BI
| |
| :;:::::::::::::::::::::::::::::::::::::::::;:;:;::::::::::::::::::::::
| |
| ,....,_ ,....__ -
| |
| 20.405(1)(1
| |
| )(y) 50.73(1)(2)(iii) 50.73(1)(211*1 . LICENSEE CONTACT FOR THIS LER (12) NAME TELEPHONE NUMBER AREA CODE M.J. Pollack -LER Coordinator
| |
| -610 19 313191-12 IO 12 12 COMPLETE ONE LINE FOR EACH COMPONENT .FAILURE OESCRIBED IN THIS REPORT (13) , ................
| |
| ........ .........
| |
| .... , ... >::::::::
| |
| .. ...... ....... MANUFAC* REPORTABLE 1:-:*:-:-.**
| |
| ... , .. ,. , ... ,, ... ..... , .. MANUFAC* REPORTABLE CAUSE SYSTEM COMPONENT CAUSE SYSTEM COMPONENT , ..... , . ... , ... ...........
| |
| * TUR ER TO NPRDS "'""* .. , ..... , .... , ... , .. TUR ER TO .NPRDS -[::::::: *.*. . ,., .. , . .... , ....... ..........
| |
| .. , ..... ..... , . ...........
| |
| ;.;.;.;. :-::-: ,., .... , ,., .. ,. 1:-:*:-:*
| |
| .... ........ .. , . ...........
| |
| * [*:"""'"*
| |
| -:* , ... B AIA I IM 10 ID H I Oi 115 y ..... ,.* . ;.: ... , .. , . I I I I I I .. ... ,. "" *.-.*:*. ... , ... , I ..... *:-: :-::*: .-:*:*:*.'
| |
| *.'::*:* "" *:-: -:*. *:*: ){} {{ ..... , .. . , ..........
| |
| !: .. :,:: :-:-:-:--:*::*:--:-:
| |
| -:* ,., .. , ... , I I I I I i I !:::::::::::::
| |
| ........ ....... , ...........
| |
| I I I I I .I I :::::::: ., .........
| |
| *.*. .. ..........
| |
| ..........
| |
| ,. ' SUPPLEMENTAL REPORT EXPECTED 1141 MONTH DAY YEAR rxi 'EXPECTED
| |
| .. SUBMISSION "J YES (If V"'* complete EXPECTED SUBMISSION DATE) DATE 1151 NO I I I . ABSTRACT (Limir to 1400 spsces. i.e .. approximately fiftef!n single.space typewritten
| |
| /in.es} (161 On 12/6/92, at 1743 hours, during full power operation, the Control Room Operator identified that Analog Rod Position Indications (ARPis) for Control Rods 104 and 2Dl. were indicating greater than a+/- 12 step deviation from their group demand counter. Technical Specification 3.1.3.2.1 addresses.the operability requirement of *the "Reactivity Control System's" position indicating systems. Actions required when more than one ARP! per bank is inoperable exceed the Tech. Spec.
| |
| Limiting Condition For Operation; therefore,.
| |
| actions associated*
| |
| with Tech. Spec. 3.0.3 apply (and was entered *on 12 / 6 / 9 2 ) .
| |
| On 12/6/92, at 1816 hours, the *2n1 control rod position indication was corrected by adjustment of the signal conditioning module. Tech. Spec .. 3.0.3 was. subsequently exited. Technical Specification Action 3.1.3.2.la.a
| |
| *remained in affect until the 1D4 control rod position indication was. corrected, at 1827 hours. The cause of the ARPis having greater than.+/- 12 step deviation from their group demand counter, for the two (2) control rods, is equipment failure. Signal conditioning modul*e drift was responsible for the two (2) control rods to be indicating greater than +/- ,12 steps from their group demand counter. The ARP! system electronics associated with the Westinghouse Signal Condition Module, will ha.ve some drift. aowever, it*is expected that this drift will not exceed the acceptable limit of + 12 steps from group demand within the 18 month calibration period. The signal conditioning module for the 2Dl and 1D4 control rod indicators are being rTplaced.
| |
| .. NRC .Form.366 16-891
| |
| * LICENSEE EVENT REPORT (LER) TEXT CONTINUATION S al em Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-025-00 2 of 4 PLANT AND SYSTEM IDENTIFICATION:
| |
| Westinghouse
| |
| -.Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx} IDENTIFICATION OF OCCURRENCE:
| |
| ' *Technical Specification 3.0'.3 entry; more than one analog rod position indicator per bank inoperable Event Dates:* 12/06/92 Report Date:
| |
| * 1/05/93 This report was initiated by Incident Report No. 92-803. CONDITIONS PRIOR TO OCCURRENCE:
| |
| Mode 1 Reactor Power 100%--Unit Load 1150 MWe On,12/6/92 at 0315 hours, a power increase from 81% to 100% was initiated.
| |
| As of 0715 hours, reactor power was ioo% with the control rods in manual. DESCRIPTION OF OCCURRENCE:
| |
| On December 6, 1992, at 1743 hours, during full-power operation, the Control Room Operator identified that Analog Rod Position Indications (ARPis) for Control Rods 1D4 and 2Dl were indicating greater than a +/- 12 step deviation from their group demand counter. Technical Specification
| |
| -3.1.3.2.1 addresses the operability requirement of the "Reactivity Control System's" {AA} position indicating systems. The indicators are determined operable by verifying that the* rod position indication system agrees within twelve (12) steps of the* group demand counters.
| |
| Actions required when more than one ARPI per is inoperable exceed the Technical Specification 3.L3.2.l Limiting Condition .For Operation; therefore, actions associated with Technical Specification
| |
|
| |
|
| ====3.0.3 apply====
| | SALEM GENERATING STATION |
| (and was entered on December 6, 1992). Technical
| | . LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 92-025-00 Thi~ Licensee Event Report is being submitted pursuant* to the requirements of th~ Code of Federal Regulations 10CFR 50.73(a) (2).(i) (B). This report is required to be issued within thirty ( 3 O) days of event discovery. - |
| | Sincerely yours, |
| | .. ;/ ~-If i //) / |
| | *1/Ju~lf{Mr c .. A Vondra - |
| | General.Manager - |
| | Salem Operations MJP:pc Distribution |
| | / If I 1-fe!" |
| | - .(i 9.301070182 930105 . |
| | PDR ADOCK 05000272 s PDR |
|
| |
|
| ====3.0.3 states==== | | l\lRC FOR!l;! 366 .U.S. NUCLEAR REGULATORY COMMISSION |
| "When a Limiting Condition for Operation is not met except provided in the associated ACTION requirements, within one hour action shall be initiated to place the unit in a MODE in which does n9t apply by placing it, as applicable, .in: .. 1. At least HOT STANDBY within the next 6 hours, 2. At least HOT SHUTDOWN within the following 6 hours, and | | , (6-891 APPROVEO OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE .TO COMPLY WTH THIS INFORMATION COlLECTION REQUEST: 50.0 HRS; FORWARD LICENSEE EVENT- REPORT (LER) |
| ' . .. --LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station DOCKET.NUMBER LER NUMBER PAGE unit 1 5000212 92-025-00 3 of 4 DESCRIPTION OF OCCURRENCE: | | . COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO |
| -(cont'd) 3. At least COLD SHUTDOWN within the subsequent 24 hours. Where corrective measures are completed that permit operation under the ACTION-requirements, the ACTION may be taken in -accordance with the specified time limits as measured from the -time of failure to meet the Limiting Condition of Operation. | | ** .I THE PAPERWORK R'EDUCTION PROJECT (3150-0104), OFFICE I |
| Exceptions to these requirements are stated -in the individual | | OF MANAGEMENT AND BUDG.ET, WASHINGTON, DC 20503. |
| * | | FACILITY NAME (1) |
| | Salem Generating Sta ti op |
| | - Unit 1 DOCK.ET NUMBER (2) 01s1010101 21 712 I |
| | , PAGE 131 OF 0 I 4 TITLE (4) |
| | Tee:h Snee 3.0.3 entry; more than one analog rod position indicator per bank .. tl.npperable. |
| | EVENT DATE 15.l* LER NUMBER (6) REPORT DATE (71 OTHER FACILITIES INVOLVED (81 MONTH DAY YEAR YEAR *:*:*:*:*:* SEQUENTIAL :::::::::: REVISION DAY YEAR FACILITY NAMES DOCKET NUMBERISI |
| | *.*.*.*.*.* NUMBER :::::;:::: NUMBER MONTH i> 1s Io Io* I o I I I |
| | -11 2 ol6 9 *2 91 2 |
| | - ol 2 Is - o lo 0!1 ol s 91 2 0 I5 I0 I0 I 0 I I I OPERATING THIS REPORT IS SUBMITTED*PURSUANT TO THE R~QUIREMENTS OF 10 CFR §: (Chock one or more of the following) (111 MODE (9) 1 20.402(b) |
| | ,....__ 20.405(cl ,_ 50.73(1)(2)(iv) |
| | ,....__ -73.71(b) |
| | POWER |
| | *LEVEL (10) l 1; 010 - 20.406(11(1 llil 20.406(1)(1 l(ii) ---- 60.38(c)(1) 50.38(c)(2) 50.73(1)(2)(v) 50.73(1)(2)(vii) |
| | ,....__ 73.71 (cl OTHER (Spacify in Abstract |
| | :;': : : ':~*: : *: : : : :*: .:-.:=: : : : : :*: ': : : : : : : : : - |
| | ~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:i:~:~:~:~:~:~:~:~: |
| | 20.406(1)(1 l(iii) 20.405(1)(1 l(lv) 20.405(1)(1 )(y) |
| | -- x 50.73(1112Hil 60.73(1)(2l(ii) 50.73(1)(2)(iii) 60.73111(2)(viii)(AI 50.73(11(2)(viii)(BI 50.73(1)(211*1 . |
| | below tJnd in Toxr, NRC Form 366A) |
| | LICENSEE CONTACT FOR THIS LER (12) |
| | NAME TELEPHONE NUMBER AREA CODE M.J. Pollack - LER Coordinator - 610 19 313191-12 IO 12 12 COMPLETE ONE LINE FOR EACH COMPONENT .FAILURE OESCRIBED IN THIS REPORT (13) |
| | REPORTABLE 1:-:*:-:-.** ...,,... .....,. ....... |
| | CAUSE SYSTEM COMPONENT MANUFAC* |
| | TUR ER TO NPRDS "'""* .,.,,...... ,.,........,,....... |
| | , CAUSE SYSTEM COMPONENT MANUFAC* |
| | TUR ER REPORTABLE TO .NPRDS .......... . ,..... .....,. |
| | - [::::::: *.*. ........... |
| | ,.,....,,.,..,. 1:-:*:-:* .... |
| | [*:"""'"* |
| | y .....,.* .;.: ...,. ,. |
| | B AIA I IM 10 ID H I Oi 115 *.-.*:*. ..., ..., I I I I I I I ..... *:-: :-::*: |
| | ){} (( :-:-:-:- -:*::*:--:-: -:* "" |
| | I I I I I i I !::::::::::::: ....... ,........... |
| | ........ I I I I I .I I !:. :,:: ::::::::........... |
| | ' MONTH DAY YEAR SUPPLEMENTAL REPORT EXPECTED 1141 |
| | 'EXPECTED rxi SUBMISSION "J YES (If V"'* complete EXPECTED SUBMISSION DATE) NO DATE 1151 I I I |
| | . ABSTRACT (Limir to 1400 spsces. i.e .. approximately fiftef!n single.space typewritten /in.es} (161 On 12/6/92, at 1743 hours, during full power operation, the Control Room Operator identified that Analog Rod Position Indications (ARPis) for Control Rods 104 and 2Dl. were indicating greater than a+/- 12 step deviation from their group demand counter. Technical Specification 3.1.3.2.1 addresses.the operability requirement of *the "Reactivity Control System's" position indicating systems. Actions required when more than one ARP! per bank is inoperable exceed the Tech. Spec. |
| | 3.1~3.2.l Limiting Condition For Operation; therefore,. actions associated* |
| | with Tech. Spec. 3.0.3 apply (and was entered *on 12 / 6 / 9 2 ) . On 12/6/92, at 1816 hours, the *2n1 control rod position indication was corrected by adjustment of the signal conditioning module. Tech. Spec .. 3.0.3 was. |
| | subsequently exited. Technical Specification Action 3.1.3.2.la.a |
| | *remained in affect until the 1D4 control rod position indication was. |
| | corrected, at 1827 hours. The cause of the ARPis having greater than.+/- |
| | 12 step deviation from their group demand counter, for the two (2) control rods, is equipment failure. Signal conditioning modul*e drift was responsible for the two (2) control rods to be indicating greater than +/- |
| | ,12 steps from their group demand counter. The ARP! system electronics s~ttings, associated with the Westinghouse Signal Condition Module, will ha.ve some drift. aowever, it*is expected that this drift will not exceed the acceptable limit of + 12 steps from group demand within the 18 month calibration period. The signal conditioning module for the 2Dl and 1D4 control rod indicators are being rTplaced. |
| | NRC .Form.366 16-891 |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION |
| | * ~~~7~~~~~~~~~~~~~~~~~~~~~~--"'-~~...,,.;...._,..~~~~~~~~- |
| | S al em Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-025-00 2 of 4 PLANT AND SYSTEM IDENTIFICATION: |
| | Westinghouse -.Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx} |
| | IDENTIFICATION OF OCCURRENCE: |
| | *Technical Specification 3.0'.3 entry; more than one analog rod position indicator per bank inoperable Event Dates:* 12/06/92 Report Date: |
| | * 1/05/93 This report was initiated by Incident Report No. 92-803. |
| | CONDITIONS PRIOR TO OCCURRENCE: |
| | Mode 1 Reactor Power 100%-- Unit Load 1150 MWe On,12/6/92 at 0315 hours, a power increase from 81% to 100% was initiated. As of 0715 hours, reactor power was ioo% with the control rods in manual. |
| | DESCRIPTION OF OCCURRENCE: |
| | On December 6, 1992, at 1743 hours, during full-power operation, the Control Room Operator identified that Analog Rod Position Indications (ARPis) for Control Rods 1D4 and 2Dl were indicating greater than a +/- |
| | 12 step deviation from their group demand counter. |
| | Technical Specification -3.1.3.2.1 addresses the operability requirement of the "Reactivity Control System's" {AA} position indicating systems. The indicators are determined operable by verifying that the* rod position indication system agrees within twelve (12) steps of the* group demand counters. Actions required when more than one ARPI per b~nk is inoperable exceed the Technical Specification 3.L3.2.l Limiting Condition .For Operation; therefore, actions associated with Technical Specification 3.0.3 apply (and was entered on December 6, 1992). |
| | Technical S~ecification 3.0.3 states: |
| | "When a Limiting Condition for Operation is not met except as-provided in the associated ACTION requirements, within one hour action shall be initiated to place the unit in a MODE in which th~ s~ecification does n9t apply by placing it, as applicable, |
| | .in: |
| | . 1. At least HOT STANDBY within the next 6 hours, |
| | : 2. At least HOT SHUTDOWN within the following 6 hours, and |
| | |
| | ' ~ |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION |
| | ----~~'-----------------_;:_--------------------------------------..-------------~ |
| | Salem Generating Station DOCKET.NUMBER LER NUMBER PAGE unit 1 5000212 92-025-00 3 of 4 DESCRIPTION OF OCCURRENCE: - (cont'd) |
| | : 3. At least COLD SHUTDOWN within the subsequent 24 hours. |
| | Where corrective measures are completed that permit operation under the ACTION-requirements, the ACTION may be taken in - |
| | accordance with the specified time limits as measured from the |
| | -time of failure to meet the Limiting Condition of Operation. |
| | Exceptions to these requirements are stated -in the individual specifications~" * |
| * On December 6, 1992., at 1816 hours, the 2Dl control rod position indication was corrected by adjustment of the signal -conditioning | | * On December 6, 1992., at 1816 hours, the 2Dl control rod position indication was corrected by adjustment of the signal -conditioning |
| _module. Technical Specification | | _module. Technical Specification 3. o. 3 was subsequently exited. |
| : 3. o. 3 was subsequently exited. Technical Specification Action 3.1.3.2.la.a remained in affect until the control rod position indication was corrected, at 1827 hours. APPARENT CAUSE OF OCCURRENCE:
| | Technical Specification Action 3.1.3.2.la.a remained in affect until the lD~ control rod position indication was corrected, at 1827 hours. |
| The cause of the ARPis having greater than +/- 12 step deviation from their group demand counter, for the two '(2) control -rods, is equipment failure. Maintenance-I&C investigation identified that signal conditioning module drift was responsible for the two (2) control rods to be indicating greater than+/- | | APPARENT CAUSE OF OCCURRENCE: |
| from their group demand counter. The ARPI system electronics settings, associated with the Westinghouse Signal Condition Module, will have some drift .. However, it is expected that this drift wiil not exceed the acceptable limit of +/- 12 steps from group demand within the 18 month calibration period .. ANALYSIS-OF OCCURRENCE: | | The cause of the ARPis having greater than +/- 12 step deviation from their group demand counter, for the two '(2) control -rods, is equipment failure. Maintenance-I&C investigation identified that signal conditioning module drift was responsible for the two (2) control rods to be indicating greater than+/- 12*st~ps from their group demand counter. |
| Operability of the ARPis is required to determine control rod position. | | The ARPI system electronics settings, associated with the Westinghouse Signal Condition Module, will have some drift . . However, it is expected that this drift wiil not exceed the acceptable limit of +/- 12 steps from group demand within the 18 month calibration period .. |
| This ensures with control rod alignment and insertion limits assumed in the accident analyses. | | ANALYSIS-OF OCCURRENCE: |
| Investigation of this event showed that actual rod positions (per group demand) were correct, with ortiy.the indication being wrong. However, -had a control rod actually been misaligned, the appropriate Technical Specification Action Statement requirements would have been met. The false rod positioning indication did not affect the health or safety of the public; however, since Technical Specification 3.0.3 was entered, this-event is-reportable to the Nuclear Regulatory Commission in accordance with Code of Federal Regulations lOCFR 50. 73 (a) (2) (i) (B). -CORRECTIVE ACTION: As stated in the* Description of Occurrence section, the 2Dl and 1D4 control rod position indications were corrected by adjustment of their conditioning modules. | | Operability of the ARPis is required to determine control rod position. This ensures co~pliance with control rod alignment and insertion limits assumed in the accident analyses. Investigation of this event showed that actual rod positions (per group demand) were correct, with ortiy.the indication being wrong. However, -had a control rod actually been misaligned, the appropriate Technical Specification Action Statement requirements would have been met. |
| LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating station Unit 1 CORRECTIVE ACTION: (cont'd) DOCKET *NUMBER 5000272 LER NUMBER 92-025.;..00 | | The false rod positioning indication did not affect the health or safety of the public; however, since Technical Specification 3.0.3 was entered, this-event is-reportable to the Nuclear Regulatory Commission in accordance with Code of Federal Regulations 10CFR |
| .. PAGE 4 of. *4 A work order has be.en initiated to :r*eplace the. 201 and 104 signal conditioning modules. system is continuing its review of this event and similar prior events. Additional corrective action will be implemented based this MJP:pc SORC Mtg. 93-001 enera1* anager -, Salem Operations}}
| | : 50. 73 (a) (2) (i) (B). - |
| | CORRECTIVE ACTION: |
| | As stated in the* Description of Occurrence section, the 2Dl and 1D4 control rod position indications were corrected by adjustment of their sign~l conditioning modules. |
| | |
| | LICENSEE EVENT REPORT (LER) TEXT CONTINUATION |
| | ~~~0;...._~~~~~~~~---'-~~~~~~~~~~~~~~~~~~~~~~~~~~ |
| | Salem Generating station DOCKET *NUMBER LER NUMBER PAGE Unit 1 5000272 92-025.;..00 4 of. *4 CORRECTIVE ACTION: (cont'd) |
| | A work order has be.en initiated to :r*eplace the. 201 and 104 signal conditioning modules. |
| | system ~ngineering is continuing its review of this event and similar prior events. Additional corrective action will be implemented based |
| | ~pon this review~ |
| | fld~ |
| | enera1* anager - |
| | , Salem Operations MJP:pc SORC Mtg. 93-001}} |
Similar Documents at Salem |
---|
Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
Text
.
PS~G Pui'..1ic Service Electric *and Gas Company P.O. Box E Hancocks Bridge, New Jersey 08038 Salem Generating Station January 5, 1993
- u. s. Nuclear Regulatory Commission Document control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION
. LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 92-025-00 Thi~ Licensee Event Report is being submitted pursuant* to the requirements of th~ Code of Federal Regulations 10CFR 50.73(a) (2).(i) (B). This report is required to be issued within thirty ( 3 O) days of event discovery. -
Sincerely yours,
.. ;/ ~-If i //) /
- 1/Ju~lf{Mr c .. A Vondra -
General.Manager -
Salem Operations MJP:pc Distribution
/ If I 1-fe!"
- .(i 9.301070182 930105 .
PDR ADOCK 05000272 s PDR
l\lRC FOR!l;! 366 .U.S. NUCLEAR REGULATORY COMMISSION
, (6-891 APPROVEO OMB NO. 3150-0104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE .TO COMPLY WTH THIS INFORMATION COlLECTION REQUEST: 50.0 HRS; FORWARD LICENSEE EVENT- REPORT (LER)
. COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P-530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO
- .I THE PAPERWORK R'EDUCTION PROJECT (3150-0104), OFFICE I
OF MANAGEMENT AND BUDG.ET, WASHINGTON, DC 20503.
FACILITY NAME (1)
Salem Generating Sta ti op
- Unit 1 DOCK.ET NUMBER (2) 01s1010101 21 712 I
, PAGE 131 OF 0 I 4 TITLE (4)
Tee:h Snee 3.0.3 entry; more than one analog rod position indicator per bank .. tl.npperable.
EVENT DATE 15.l* LER NUMBER (6) REPORT DATE (71 OTHER FACILITIES INVOLVED (81 MONTH DAY YEAR YEAR *:*:*:*:*:* SEQUENTIAL :::::::::: REVISION DAY YEAR FACILITY NAMES DOCKET NUMBERISI
- .*.*.*.*.* NUMBER :::::;:::: NUMBER MONTH i> 1s Io Io* I o I I I
-11 2 ol6 9 *2 91 2
- ol 2 Is - o lo 0!1 ol s 91 2 0 I5 I0 I0 I 0 I I I OPERATING THIS REPORT IS SUBMITTED*PURSUANT TO THE R~QUIREMENTS OF 10 CFR §: (Chock one or more of the following) (111 MODE (9) 1 20.402(b)
,....__ 20.405(cl ,_ 50.73(1)(2)(iv)
,....__ -73.71(b)
POWER
- LEVEL (10) l 1; 010 - 20.406(11(1 llil 20.406(1)(1 l(ii) ---- 60.38(c)(1) 50.38(c)(2) 50.73(1)(2)(v) 50.73(1)(2)(vii)
,....__ 73.71 (cl OTHER (Spacify in Abstract
- '
- : : ':~*: : *: : : : :*: .:-.:=: : : : : :*: ': : : : : : : : : -
~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:~:i:~:~:~:~:~:~:~:~:
20.406(1)(1 l(iii) 20.405(1)(1 l(lv) 20.405(1)(1 )(y)
-- x 50.73(1112Hil 60.73(1)(2l(ii) 50.73(1)(2)(iii) 60.73111(2)(viii)(AI 50.73(11(2)(viii)(BI 50.73(1)(211*1 .
below tJnd in Toxr, NRC Form 366A)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE M.J. Pollack - LER Coordinator - 610 19 313191-12 IO 12 12 COMPLETE ONE LINE FOR EACH COMPONENT .FAILURE OESCRIBED IN THIS REPORT (13)
REPORTABLE 1:-:*:-:-.** ...,,... .....,. .......
CAUSE SYSTEM COMPONENT MANUFAC*
TUR ER TO NPRDS "'""* .,.,,...... ,.,........,,.......
, CAUSE SYSTEM COMPONENT MANUFAC*
TUR ER REPORTABLE TO .NPRDS .......... . ,..... .....,.
- [::::::: *.*. ...........
,.,....,,.,..,. 1:-:*:-:* ....
[*:"""'"*
y .....,.* .;.: ...,. ,.
B AIA I IM 10 ID H I Oi 115 *.-.*:*. ..., ..., I I I I I I I ..... *:-: :-::*:
){} (( :-:-:-:- -:*::*:--:-: -:* ""
I I I I I i I !::::::::::::: ....... ,...........
........ I I I I I .I I !:. :,:: ::::::::...........
' MONTH DAY YEAR SUPPLEMENTAL REPORT EXPECTED 1141
'EXPECTED rxi SUBMISSION "J YES (If V"'* complete EXPECTED SUBMISSION DATE) NO DATE 1151 I I I
. ABSTRACT (Limir to 1400 spsces. i.e .. approximately fiftef!n single.space typewritten /in.es} (161 On 12/6/92, at 1743 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.632115e-4 months <br />, during full power operation, the Control Room Operator identified that Analog Rod Position Indications (ARPis) for Control Rods 104 and 2Dl. were indicating greater than a+/- 12 step deviation from their group demand counter. Technical Specification 3.1.3.2.1 addresses.the operability requirement of *the "Reactivity Control System's" position indicating systems. Actions required when more than one ARP! per bank is inoperable exceed the Tech. Spec.
3.1~3.2.l Limiting Condition For Operation; therefore,. actions associated*
with Tech. Spec. 3.0.3 apply (and was entered *on 12 / 6 / 9 2 ) . On 12/6/92, at 1816 hours0.021 days <br />0.504 hours <br />0.003 weeks <br />6.90988e-4 months <br />, the *2n1 control rod position indication was corrected by adjustment of the signal conditioning module. Tech. Spec .. 3.0.3 was.
subsequently exited. Technical Specification Action 3.1.3.2.la.a
- remained in affect until the 1D4 control rod position indication was.
corrected, at 1827 hours0.0211 days <br />0.508 hours <br />0.00302 weeks <br />6.951735e-4 months <br />. The cause of the ARPis having greater than.+/-
12 step deviation from their group demand counter, for the two (2) control rods, is equipment failure. Signal conditioning modul*e drift was responsible for the two (2) control rods to be indicating greater than +/-
,12 steps from their group demand counter. The ARP! system electronics s~ttings, associated with the Westinghouse Signal Condition Module, will ha.ve some drift. aowever, it*is expected that this drift will not exceed the acceptable limit of + 12 steps from group demand within the 18 month calibration period. The signal conditioning module for the 2Dl and 1D4 control rod indicators are being rTplaced.
NRC .Form.366 16-891
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
- ~~~7~~~~~~~~~~~~~~~~~~~~~~--"'-~~...,,.;...._,..~~~~~~~~-
S al em Generating Station DOCKET NUMBER LER NUMBER PAGE Unit 1 5000272 92-025-00 2 of 4 PLANT AND SYSTEM IDENTIFICATION:
Westinghouse -.Pressurized Water Reactor Energy Industry Identification System (EIIS) codes are identified in the text as {xx}
IDENTIFICATION OF OCCURRENCE:
- Technical Specification 3.0'.3 entry; more than one analog rod position indicator per bank inoperable Event Dates:* 12/06/92 Report Date:
- 1/05/93 This report was initiated by Incident Report No.92-803.
CONDITIONS PRIOR TO OCCURRENCE:
Mode 1 Reactor Power 100%-- Unit Load 1150 MWe On,12/6/92 at 0315 hours0.00365 days <br />0.0875 hours <br />5.208333e-4 weeks <br />1.198575e-4 months <br />, a power increase from 81% to 100% was initiated. As of 0715 hours0.00828 days <br />0.199 hours <br />0.00118 weeks <br />2.720575e-4 months <br />, reactor power was ioo% with the control rods in manual.
DESCRIPTION OF OCCURRENCE:
On December 6, 1992, at 1743 hours0.0202 days <br />0.484 hours <br />0.00288 weeks <br />6.632115e-4 months <br />, during full-power operation, the Control Room Operator identified that Analog Rod Position Indications (ARPis) for Control Rods 1D4 and 2Dl were indicating greater than a +/-
12 step deviation from their group demand counter.
Technical Specification -3.1.3.2.1 addresses the operability requirement of the "Reactivity Control System's" {AA} position indicating systems. The indicators are determined operable by verifying that the* rod position indication system agrees within twelve (12) steps of the* group demand counters. Actions required when more than one ARPI per b~nk is inoperable exceed the Technical Specification 3.L3.2.l Limiting Condition .For Operation; therefore, actions associated with Technical Specification 3.0.3 apply (and was entered on December 6, 1992).
Technical S~ecification 3.0.3 states:
"When a Limiting Condition for Operation is not met except as-provided in the associated ACTION requirements, within one hour action shall be initiated to place the unit in a MODE in which th~ s~ecification does n9t apply by placing it, as applicable,
.in:
. 1. At least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,
- 2. At least HOT SHUTDOWN within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, and
' ~
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
~~'-----------------_;:_--------------------------------------..-------------~
Salem Generating Station DOCKET.NUMBER LER NUMBER PAGE unit 1 5000212 92-025-00 3 of 4 DESCRIPTION OF OCCURRENCE: - (cont'd)
- 3. At least COLD SHUTDOWN within the subsequent 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
Where corrective measures are completed that permit operation under the ACTION-requirements, the ACTION may be taken in -
accordance with the specified time limits as measured from the
-time of failure to meet the Limiting Condition of Operation.
Exceptions to these requirements are stated -in the individual specifications~" *
- On December 6, 1992., at 1816 hours0.021 days <br />0.504 hours <br />0.003 weeks <br />6.90988e-4 months <br />, the 2Dl control rod position indication was corrected by adjustment of the signal -conditioning
_module. Technical Specification 3. o. 3 was subsequently exited.
Technical Specification Action 3.1.3.2.la.a remained in affect until the lD~ control rod position indication was corrected, at 1827 hours0.0211 days <br />0.508 hours <br />0.00302 weeks <br />6.951735e-4 months <br />.
APPARENT CAUSE OF OCCURRENCE:
The cause of the ARPis having greater than +/- 12 step deviation from their group demand counter, for the two '(2) control -rods, is equipment failure. Maintenance-I&C investigation identified that signal conditioning module drift was responsible for the two (2) control rods to be indicating greater than+/- 12*st~ps from their group demand counter.
The ARPI system electronics settings, associated with the Westinghouse Signal Condition Module, will have some drift . . However, it is expected that this drift wiil not exceed the acceptable limit of +/- 12 steps from group demand within the 18 month calibration period ..
ANALYSIS-OF OCCURRENCE:
Operability of the ARPis is required to determine control rod position. This ensures co~pliance with control rod alignment and insertion limits assumed in the accident analyses. Investigation of this event showed that actual rod positions (per group demand) were correct, with ortiy.the indication being wrong. However, -had a control rod actually been misaligned, the appropriate Technical Specification Action Statement requirements would have been met.
The false rod positioning indication did not affect the health or safety of the public; however, since Technical Specification 3.0.3 was entered, this-event is-reportable to the Nuclear Regulatory Commission in accordance with Code of Federal Regulations 10CFR
- 50. 73 (a) (2) (i) (B). -
CORRECTIVE ACTION:
As stated in the* Description of Occurrence section, the 2Dl and 1D4 control rod position indications were corrected by adjustment of their sign~l conditioning modules.
LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
~~~0;...._~~~~~~~~---'-~~~~~~~~~~~~~~~~~~~~~~~~~~
Salem Generating station DOCKET *NUMBER LER NUMBER PAGE Unit 1 5000272 92-025.;..00 4 of. *4 CORRECTIVE ACTION: (cont'd)
A work order has be.en initiated to :r*eplace the. 201 and 104 signal conditioning modules.
system ~ngineering is continuing its review of this event and similar prior events. Additional corrective action will be implemented based
~pon this review~
fld~
enera1* anager -
, Salem Operations MJP:pc SORC Mtg.93-001