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| issue date = 05/27/1977
| issue date = 05/27/1977
| title = LER 1976-027-03 for R.E. Ginna, Leak in Letdown Diversion Line on 12/16/1976, and LER 1976-030-03 a Mixed Bed Demineralizer Inlet Piping Leak
| title = LER 1976-027-03 for R.E. Ginna, Leak in Letdown Diversion Line on 12/16/1976, and LER 1976-030-03 a Mixed Bed Demineralizer Inlet Piping Leak
| author name = White L D
| author name = White L
| author affiliation = Rochester Gas & Electric Corp
| author affiliation = Rochester Gas & Electric Corp
| addressee name = O'Reilly J P
| addressee name = O'Reilly J
| addressee affiliation = NRC/IE, NRC/RGN-I
| addressee affiliation = NRC/IE, NRC/RGN-I
| docket = 05000244
| docket = 05000244
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=Text=
=Text=
{{#Wiki_filter:~U.S.NUCLEAR REGULATORY COMMISSION NRC DISTRI8UTION FDR PART 50 DOCKET MATERIAL DOCKET NUMBER FILE NUMBER INCIDENT REPORT J.P.O'REXLLY, FROM:ROCHESTER GAS&ELEC.CORP.ROCHESTER, N.Y.'L.D.WHITE, JR.~DATE OF DOCUMENT'ATE RECEIVED Q LETT E R QOAIGINAL K)CO>Y ONOTOAIZED EBUNCLASSIFIED PROP INPUT FOAM NUMBE R OF COPIES RECEIVED DESCAIPTION 1'TR'RANS THE FOLLOWXNG PLANT NAME'E GINNA 4/SAB I" I:.~(1P).ENCLOSURE UBDATE LICENSEE EVENT REPORT/f 76-27, 30 DAY ON 12/16/76 CONCERNING LIQUID COMING THROUGH INSULA ION ON 2" LE'ZDOWN DIVERSION LINE.......
{{#Wiki_filter:~   U.S. NUCLEAR REGULATORY COMMISSION   DOCKET NUMBER FILE NUMBER NRC DISTRI8UTION FDR PART 50 DOCKET MATERIAL                                       INCIDENT REPORT FROM:ROCHESTER GAS & ELEC. CORP.                 DATE OF J.P.O'REXLLY,                                                                                  DOCUMENT'ATE ROCHESTER, N.Y.
UPDATE LICENSEE EVQP REPORT 1/76-30, 30 DAY ON 12/17/76.CONCERNIg+LXQUPJ"%EARP, FROM THE"A" MIXED.BED SEMINERAL'IZQR I%K'ET~~QIg M k4I II';I)K: NOTE~IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/Jo COLLINS'RANCH CHIEF!W 3 CYS FOR ACTION LIC, ASST'!W/CYS ACRS/CYS 14Ch5%NG S NT FOR ACTION/INFO FIMAT I ON INTERNAL DISTRI BUTION'NRC PDR MIPC~SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES BUTLER IIANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS LPDR: TIC: EANAL DISTRIBUTION CON OL NUMBER NAC FORM 105 I2.ld)71540052 o~o o~~o g Io o~o~o~~, ll'gV o~~~o~o a~oo I~)II~
                                                    'L.D.       WHITE, JR.   ~                       RECEIVED Q LETTE R             ONOTOAIZED           PROP                       INPUT FOAM           NUMBER OF COPIES RECEIVED QOAIGINAL          EBUNCLASSIFIED K)CO> Y DESCAIPTION                                                       ENCLOSURE 1'TR'RANS         THE FOLLOWXNG                               UBDATE LICENSEE EVENT REPORT /f 76-27, 30 DAY ON 12/16/76 CONCERNING LIQUID COMING THROUGH INSULA ION ON 2"   LE'ZDOWN DIVERSION LINE.......
r Qg P i'iI'4'"7/"'"PW i't.i<IL'/74Ii W'"W ROCHESTER GAS AND ELECTRIC CORPORATlON PI~~0~rake 89 EAST AVENUE, ROCHESTER,, N.Y.14649 LEON D.WHITE.JR.VICC PACSIDCNT May 27, 1977 TCLCPNONC iPCi CONC TIO 54G 2700 Mr.James P~O'Reilly, Director U.S.Nuclear Regulatory Commis%%8 Office of inspection and Enforcement Region I 63 1 Park Avenue King of Prussia, Pennsylvania 19406 r 8>ge'Ctt g UN 2 3977~'EI g..S.IIIIC'C">RUU5h5kV re'~I>Ncll54rtbe
I:.    ~
UPDATE LICENSEE EVQP REPORT       1/ 76-30, 30 DAY ON (1P)    .        12/17/76. CONCERNIg+LXQUPJ"%EARP, FROM THE "A" MIXED. BED SEMINERAL'IZQR I%K'ET~~QIg M k4I II';I)K:
PLANT NAME'        E  GINNA  4/
I"  SAB NOTE ~   IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/Jo COLLINS FOR ACTION/INFOFIMATI ON
    'RANCH CHIEF!
W   3 CYS FOR ACTION LIC, ASST'!
W     /CYS ACRS     / CYS 14Ch5%NG S NT INTERNAL DISTRI BUTION
    'NRC PDR MIPC
~   SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES BUTLER IIANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS EANAL DISTRIBUTION                                             CON             OL NUMBER LPDR:
TIC:
71540052 NAC FORM 105 I2.ld)
 
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        'iI'4'"7/ "'"PW Pi i't.i<IL'/74Ii W'"W ROCHESTER GAS AND ELECTRIC CORPORATlON               89 EAST AVENUE, ROCHESTER,, N.Y. 14649 LEON D. WHITE. JR.                                                                 TCLCPNONC VICC PACSIDCNT                                                         iPCi CONC   TIO 54G   2700 May 27, 1977 r
Mr. James P O'Reilly, Director
                            ~
8 >        ge 'Ctt U. S. Nuclear Regulatory Commis%%8                                         g UN        2 3977~
Office of inspection and Enforcement Region I
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                                                                                            >Ncll54rtbe 63 1 Park Avenue King of Prussia, Pennsylvania          19406


==Subject:==
==Subject:==
Supplemental reports on Reportable Occurrences:
Supplemental reports on Reportable Occurrences:
76-27 (30-day report)Leak in letdown diversion line 76-30 (30-day report)"A" mixed bed demineralizer inlet piping leak R.E.Qinna Nuclear Power Plant, Unit No.1 Docket No.50-244  
76-27 (30-day report) Leak in letdown diversion line 76-30 (30-day report) "A" mixed bed demineralizer inlet piping leak R. E. Qinna Nuclear Power Plant, Unit No. 1 Docket No. 50-244
 
==Dear Mr. O'Reilly:==
 
The purpose of this letter is to provide you with corrected component manufacturer information in connection with the subject reports which were submitted January 4 and January 12, 1977 respectively. The attached update reports LER 76-27/30 and LER 76-30/30 provide this information.
Two additional copies of  this letter and the attachments are enclosed to conform to the original submittal of LER 76-27/3L and LER 76-30/3L.
Very truly yours, L. D. White Jr.
cc: Dr. Ernst Volgenau (30)
Mr. William G. McDonald (3)
                                                                                            .77g540052.
 
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LER    76-27/30 Update Report  Previous Report Date 1/4/77 CONTROL BLOCK:
Q.IOENSEE EVENT REPORT
                                                                                                              +
fPLEASE PAINT ALL REQVIREO IiNFORIViATION)
LICENSEE                                                                                UCENSE                EVENT NAME                                  UCENSE NUMBER                                      TYPE                TYPE
[op~j      N Y        R    B    G    1        0 0    0      0  0    0    0    0        0        O  1    1    1'        ~03
                    ~
7 89                                    14    15                                              25    26                    30  31    32 REPORT    REPORT CATEGORY        TYPE    SOURCE            DOCKET NUMBER                            EVENT DATE                    REPORT DATE 0
7
[oO~]corn 8            57      58 0
59 L
60    61 0    5  0              2  4    4 68    69 1  2    1  6    7    6 74  '50    5    2    7    7      7 80 EVENT DESCRIPTION gg            During normal rounds operator noticed liquid coming through insulation on 2" letdown 7 8    9                                                                                                                                                    80 tOQ3) diversion line          ~    Upon return to steady state letdown condition, line was isolated                                      ~
7    89                                                                                                                                                      80 (Reportable Occurrence 76-27, 30-day)                          .
7 8 9                                                                                                                                                        80 toom 7 8 9                                                                                                                                                        80 tm 7 8      9                                                              PA VIE                                                                              80
          . SYSTEM        CAUSE                                      COMPONENT              COMPONENT CODE        CODE            COMPONENT CODE            SUPPUER              MANUFACTURER            VGIATION
[ocvj  ~CG                B            P  I    P B  X X            ~N                B    1    3  0              N 7 8 9 10                    11        12                      17        43            44                  47          48 CAUSE DESCRIPTION A  pinhole leak was found fn socket weld between pipe and elbow. Weld was built up 7    8 9                                                                                                                                                      80
  ~09          in area of leak, and a visual inspection performed upon return of system to service ver 7    8 9                                                                                                                                                      80 Q~g          ified leak was stopped.                  This section of line was (cont'd. under Additional Factors) 7    89                                                                                                                                                      80 FACILITY                                                          METHOD OF STATUS            % POWER                OTHER STATUS            DISCOVERY                        DISCOVERY DESCRIPTION gg8 7              9 B            ~io 10 o
12 13 NA 44 b
45      46 0 erator makin rounds FORM OF
                          .                                                                                                                                  80 AMOUNT OF ACTIVITY                                              LOCATION OF RELEASE 7    8          9                10      11                                44        45                                                                    80 PERSONNEL EXPOSURES 7    89                  11      12      13                                                                                                                  80 PEFISONNEL INJURIES NUMBER            DESCRIPTION
~4 ~oo                o                              NA 7    8 9    .            11    12                                                                                                                            80 OFFSITE CONSEQUENCES NA 7    8 9                                                                                                                                                      80 LOSS OR DAMAGE TO FACILITY TYPE        DESCRIPTION
~16                                                  NA 7 89                10                                                                                                                                        80 PUBLICITY 7    89                                                                                                                                                      80 ADDITIONAL FACTORS
[J>QB          (cont'd. from Cause Description) replaced during refueling shutdown to remove weld 7    89                                                                                                                                                      80 Qg 7    89 which had been leaking.                    CAR  llllwas issued                to document this corrective action.
80 NAME:                ames    Witte/D. Hamelink                                    pgONE', 7 1  6/546-2 700, ext.            29  1 -2 1 5 GPO  661    6 61
 
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~ l    e LER    76-30/30 UDdate Report                    Previous Report Date 1/12/77 CONTROL BLOCK
                                                            ~    ICENSEE EVENT REPORT fPLEAGE PRINT ALL RECIUIRED INFORMATION) 1                        6 UCENSEE                                                                                            LICENSE              EVENT NAME                                  LICENSE NUMBEA                                            TYPE                'TYPE Qg09        N Y        R    E    G    1        0  0    0      0  0                                        4                          LBO~J
                        ~
7                                      14      15                                                  25        26                      30    31      32 REPORT    REPORT CATEGORY        TYPE    SOURCE              DOCKET NUMBER                                    EVENT DATE                      AEPOAT DATE
      ~cl cowl                            0          L        0    5  0  0          2    4    4        1        2    1  7      7          0    5    2    7  7  7 7    8          57      58      59        60    61                                      68    69                              74    75                        80 I
EVENT DESCRIPTION During normal rounds an operator discovered liquid leaking from the "A" mixed bed 7    8 9                                                                                                                                                            80 demineralizer inlet pipe                .    (Reportable Occurrence 76-30, 30-day)                                  .
7    09                                                                                                                                                            80 t00j4 7    8 9                                                                                                                                                            80 Jog 7 0 9                                                                                                                                                                80
[0DQ 7    09                                                                  PAVE                                                                                      80 SYSTEM        CAUSE                                        COMPONENT                COMPONENT MANUFACTUREA
                      ~IB CODE          CODE            COMPONENT CODE              SUPPUER                                            VIOIATKIN tocC>~ILcGCa                            P      I  P  E    x x              N                  B  1      3      0              N 7    8 9 10                11        12                          17        43              44                      47          48 CAUSE DESCRIPTION Q~g          Pinhole leak in weld between pipe and elbow. Hole was ground out and repaired using 7    0 9                                                                                                                                                            80
[pgg]        proper welding procedure. The piping was visually inspected for leakage after return 7 8 9                                                                                                                                                                80 Q~g          to service.            CAR 1114 was            issued for this event.
7      89                                                                          METHOD OF 80 FACILITY STATUS                POWER                  OTHER STATUS              DISCOVERY                          ~  DISCOVERY DESCRIPTION 7
Eg 0
LEJ 9
                                    ~io 10 o
12 13 NA 44      45 b
46 0 erator makin rounds FOAM OF 80 ACTIVITY        COATENT AELEASEO      OF RELEASE            AMOUNT OF ACTIVITY                                                      LOCATION OF RELEASE Qg              H              sj                    NA 7    8        9                10      11                                    44          45                                                                        00 PERSONNEL EXPOSURES NUMBER          TYPE      DESCRIPTION Pg~oo 7 8 9 o          B 12      13 NA 11                                                                                                                                        80 PERSONNEL INJURIES NUMBER            DESCRIPTION fig      ~00          0                                NA 7 09        ~
11  12                                                                                                                                    80 OFFSITE CONSEQUENCES Qg                                                      NA 7    09                                                                                                                                                            00 LOSS OR DAMAGE TO FACILITY TYPE        DESCRIPTION Q~g        s 7      09          10                                                                                                                                                80 PUBLICITY Q~~]                                                                          ~ e ~ i +II'lI    Ej
                                                                                                                  $ Pl, 7 89                                                                                                                                                                  80 ADDITIONAL FACTORS l,lJ ~
NA 7      89                                                                                                                                                            80 7      09                                                                                                                                                            80 NAME:                  , Dave Hamelink                                                      PHDNL.".
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==Dear Mr.O'Reilly:==
                          \ ~
The purpose of this letter is to provide you with corrected component manufacturer information in connection with the subject reports which were submitted January 4 and January 12, 1977 respectively.
                      ) f
The attached update reports LER 76-27/30 and LER 76-30/30 provide this information.
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Two additional copies of this letter and the attachments are enclosed to conform to the original submittal of LER 76-27/3L and LER 76-30/3L.Very truly yours, L.D.White Jr.cc: Dr.Ernst Volgenau (30)Mr.William G.McDonald (3).77g540052.
ee),
ao~4~\J I I"$'d LER 76-27/30 Update Report-Previous Report Date 1/4/77 Q.IOENSEE EVENT REPORT+CONTROL BLOCK: f PLEASE PAINT ALL REQVIREO IiNFORIViATION)
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LICENSEE NAME[op~j N Y R B G 1 0 7 89 14 15 UCENSE NUMBER 0-0 0 0 0 0-0 0 25 EVENT TYPE UCENSE TYPE O 1 1 1'~03 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE[oO~]corn~0 L 7 8 57 58 59 60 EVENT DESCRIPTION gg During normal rounds DOCKET NUMBER EVENT DATE REPORT DATE 0 5 0-0 2 4 4 1 2 1 6 7 6 0 5 2 7 7 7 61 68 69 74'5 80 operator noticed liquid coming through insulation on 2" letdown 7 8 9 80 tOQ3)diversion line~Upon return to steady state letdown condition, line was isolated~80 7 89 (Reportable Occurrence 76-27, 30-day).7 8 9 toom 7 8 9 tm COMPONENT MANUFACTURER N 47 7 8 9 PA VIE.SYSTEM CAUSE COMPONENT CODE CODE COMPONENT CODE SUPPUER VGIATION[ocvj~CG B P I P B X X~N B 1 3 0 7 8 9 10 11 12 17 43 44 48 CAUSE DESCRIPTION A pinhole leak was found fn socket weld between pipe and elbow.Weld was built up 80 80 80 7 8 9 80~09 in area of leak, and a visual inspection performed upon return of system to service ver 80 7 89 FACILITY STATUS%POWER gg B~io o 7 8 9.10 12 13 FORM OF 7 8 9 10 11 PERSONNEL EXPOSURES 7 89 11 12 13 PEFISONNEL IN JURIES NUMBER DESCRIPTION
(
~4~oo o NA 7 8 9.11 12 METHOD OF DISCOVERY DISCOVERY DESCRIPTION 0 erator makin rounds OTHER STATUS b NA 44 45 46 80 LOCATION OF RELEASE AMOUNT OF ACTIVITY 44 45 80 80 80 OFFSITE CONSEQUENCES NA 7 8 9 80 Q~g ified leak was stopped.This section of line was (cont'd.under Additional Factors)7 8 9 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION
~~~~~"~~0 0~3~~~~~
~16 7 89 10 PUBLICITY NA 80 80 7 89 ADDITIONAL FACTORS[J>QB (cont'd.from Cause Description) replaced during refueling shutdown to remove weld 7 89 Qg which had been leaking.CAR llll was issued to document this corrective action.80 80 7 89 NAME: ames Witte/D.Hamelink 80 pgONE', 7 1 6/546-2 700, ext.29 1-2 1 5 GPO 661 6 61
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~l e CONTROL BLOCK LER 76-30/30 UDdate Report-Previous Report Date 1/12/77~ICENSEE EVENT REPORT f PLEAGE PRINT ALL RECIUIRED INFORMATION) 1 6 UCENSEE NAME LICENSE NUMBEA LICENSE TYPE EVENT'TYPE Qg N Y R E G 1 0 0-0 0 0 7 09 14 15 4 25 26 LBO~J 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER~clcowl~7 8 57 58 0 L 0 5 0-0 2 4 59 60 61 EVENT DATE AEPOAT DATE 4 1 2 1 7 7 0 5 2 7 7 7 68 69 74 75 80 EVENT DESCRIPTION During normal rounds an operator discovered liquid leaking from the"A" mixed bed 7 8 9 I demineralizer inlet pipe.(Reportable Occurrence 76-30, 30-day).7 09 t00j4 7 8 9 Jog 7 0 9[0DQ 80 80 80 80 7 09 PAVE SYSTEM CAUSE COMPONENT CODE CODE COMPONENT CODE SUPPUER VIOIATKIN tocC>~ILcGCa~IB P I P E x x N B 1 3 0 N 7 8 9 10 11 12 17 43 47 CAUSE DESCRIPTION Q~g Pinhole leak in weld between pipe and elbow.Hole was ground out and repaired using 80 COMPONENT MAN UFACTUREA 44 48 7 0 9 80[pgg]proper welding procedure.
The piping was visually inspected for leakage after return 7 8 9 Q~g to service.CAR 1114 was issued for this event.80 OTHER STATUS NA AMOUNT OF ACTIVITY OFFSITE CONSEQUENCES 7 89 FACILITY STATUS POWER Eg LEJ~io o 7 0 9 10 12 13 FOAM OF ACTIVITY COATENT AELEASEO OF RELEASE Qg H sj NA 7 8 9 10 11 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Pg~oo o B NA 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTION fig~00 0 NA 7 09~11 12 METHOD OF DISCOVERY b 44 45 46 44 45~DISCOVERY DESCRIPTION 0 erator makin rounds LOCATION OF RELEASE 80 80 00 80 80 Qg 7 09 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION Q~g s 7 09 10 PUBLICITY Q~~]7 89 ADDITIONAL FACTORS 7 89 NA NA$Pl,~e~i+II'lI Ej l,lJ~00 80 80 80 7 09 NAME: , Dave Hamelink 80 PHDNL.".7 1 6/5 4 6-2 7 0 0, ex t~2 9 1-2 1 5 GPO 8
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Latest revision as of 00:34, 3 February 2020

LER 1976-027-03 for R.E. Ginna, Leak in Letdown Diversion Line on 12/16/1976, and LER 1976-030-03 a Mixed Bed Demineralizer Inlet Piping Leak
ML18142B229
Person / Time
Site: Ginna Constellation icon.png
Issue date: 05/27/1977
From: White L
Rochester Gas & Electric Corp
To: O'Reilly J
NRC/IE, NRC Region 1
References
LER 1976-027-03
Download: ML18142B229 (8)


Text

~ U.S. NUCLEAR REGULATORY COMMISSION DOCKET NUMBER FILE NUMBER NRC DISTRI8UTION FDR PART 50 DOCKET MATERIAL INCIDENT REPORT FROM:ROCHESTER GAS & ELEC. CORP. DATE OF J.P.O'REXLLY, DOCUMENT'ATE ROCHESTER, N.Y.

'L.D. WHITE, JR. ~ RECEIVED Q LETTE R ONOTOAIZED PROP INPUT FOAM NUMBER OF COPIES RECEIVED QOAIGINAL EBUNCLASSIFIED K)CO> Y DESCAIPTION ENCLOSURE 1'TR'RANS THE FOLLOWXNG UBDATE LICENSEE EVENT REPORT /f 76-27, 30 DAY ON 12/16/76 CONCERNING LIQUID COMING THROUGH INSULA ION ON 2" LE'ZDOWN DIVERSION LINE.......

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UPDATE LICENSEE EVQP REPORT 1/ 76-30, 30 DAY ON (1P) . 12/17/76. CONCERNIg+LXQUPJ"%EARP, FROM THE "A" MIXED. BED SEMINERAL'IZQR I%K'ET~~QIg M k4I II';I)K:

PLANT NAME' E GINNA 4/

I" SAB NOTE ~ IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/Jo COLLINS FOR ACTION/INFOFIMATI ON

'RANCH CHIEF!

W 3 CYS FOR ACTION LIC, ASST'!

W /CYS ACRS / CYS 14Ch5%NG S NT INTERNAL DISTRI BUTION

'NRC PDR MIPC

~ SCHROEDER/IPPOLITO HOUSTON NOVAK/CHECK GRIMES BUTLER IIANAUER TEDESCO/MACCARY EISENHUT BAER SHAO VOLLMER/BUNCH KREGER/J COLLINS EANAL DISTRIBUTION CON OL NUMBER LPDR:

TIC:

71540052 NAC FORM 105 I2.ld)

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'iI'4'"7/ "'"PW Pi i't.i<IL'/74Ii W'"W ROCHESTER GAS AND ELECTRIC CORPORATlON 89 EAST AVENUE, ROCHESTER,, N.Y. 14649 LEON D. WHITE. JR. TCLCPNONC VICC PACSIDCNT iPCi CONC TIO 54G 2700 May 27, 1977 r

Mr. James P O'Reilly, Director

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8 > ge 'Ctt U. S. Nuclear Regulatory Commis%%8 g UN 2 3977~

Office of inspection and Enforcement Region I

'EI re' ~I g..S. IIIIC'C">RUU5h5kV

>Ncll54rtbe 63 1 Park Avenue King of Prussia, Pennsylvania 19406

Subject:

Supplemental reports on Reportable Occurrences:

76-27 (30-day report) Leak in letdown diversion line 76-30 (30-day report) "A" mixed bed demineralizer inlet piping leak R. E. Qinna Nuclear Power Plant, Unit No. 1 Docket No. 50-244

Dear Mr. O'Reilly:

The purpose of this letter is to provide you with corrected component manufacturer information in connection with the subject reports which were submitted January 4 and January 12, 1977 respectively. The attached update reports LER 76-27/30 and LER 76-30/30 provide this information.

Two additional copies of this letter and the attachments are enclosed to conform to the original submittal of LER 76-27/3L and LER 76-30/3L.

Very truly yours, L. D. White Jr.

cc: Dr. Ernst Volgenau (30)

Mr. William G. McDonald (3)

.77g540052.

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LER 76-27/30 Update Report Previous Report Date 1/4/77 CONTROL BLOCK:

Q.IOENSEE EVENT REPORT

+

fPLEASE PAINT ALL REQVIREO IiNFORIViATION)

LICENSEE UCENSE EVENT NAME UCENSE NUMBER TYPE TYPE

[op~j N Y R B G 1 0 0 0 0 0 0 0 0 0 O 1 1 1' ~03

~

7 89 14 15 25 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE REPORT DATE 0

7

[oO~]corn 8 57 58 0

59 L

60 61 0 5 0 2 4 4 68 69 1 2 1 6 7 6 74 '50 5 2 7 7 7 80 EVENT DESCRIPTION gg During normal rounds operator noticed liquid coming through insulation on 2" letdown 7 8 9 80 tOQ3) diversion line ~ Upon return to steady state letdown condition, line was isolated ~

7 89 80 (Reportable Occurrence 76-27, 30-day) .

7 8 9 80 toom 7 8 9 80 tm 7 8 9 PA VIE 80

. SYSTEM CAUSE COMPONENT COMPONENT CODE CODE COMPONENT CODE SUPPUER MANUFACTURER VGIATION

[ocvj ~CG B P I P B X X ~N B 1 3 0 N 7 8 9 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION A pinhole leak was found fn socket weld between pipe and elbow. Weld was built up 7 8 9 80

~09 in area of leak, and a visual inspection performed upon return of system to service ver 7 8 9 80 Q~g ified leak was stopped. This section of line was (cont'd. under Additional Factors) 7 89 80 FACILITY METHOD OF STATUS  % POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION gg8 7 9 B ~io 10 o

12 13 NA 44 b

45 46 0 erator makin rounds FORM OF

. 80 AMOUNT OF ACTIVITY LOCATION OF RELEASE 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES 7 89 11 12 13 80 PEFISONNEL INJURIES NUMBER DESCRIPTION

~4 ~oo o NA 7 8 9 . 11 12 80 OFFSITE CONSEQUENCES NA 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION

~16 NA 7 89 10 80 PUBLICITY 7 89 80 ADDITIONAL FACTORS

[J>QB (cont'd. from Cause Description) replaced during refueling shutdown to remove weld 7 89 80 Qg 7 89 which had been leaking. CAR llllwas issued to document this corrective action.

80 NAME: ames Witte/D. Hamelink pgONE', 7 1 6/546-2 700, ext. 29 1 -2 1 5 GPO 661 6 61

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~ l e LER 76-30/30 UDdate Report Previous Report Date 1/12/77 CONTROL BLOCK

~ ICENSEE EVENT REPORT fPLEAGE PRINT ALL RECIUIRED INFORMATION) 1 6 UCENSEE LICENSE EVENT NAME LICENSE NUMBEA TYPE 'TYPE Qg09 N Y R E G 1 0 0 0 0 0 4 LBO~J

~

7 14 15 25 26 30 31 32 REPORT REPORT CATEGORY TYPE SOURCE DOCKET NUMBER EVENT DATE AEPOAT DATE

~cl cowl 0 L 0 5 0 0 2 4 4 1 2 1 7 7 0 5 2 7 7 7 7 8 57 58 59 60 61 68 69 74 75 80 I

EVENT DESCRIPTION During normal rounds an operator discovered liquid leaking from the "A" mixed bed 7 8 9 80 demineralizer inlet pipe . (Reportable Occurrence 76-30, 30-day) .

7 09 80 t00j4 7 8 9 80 Jog 7 0 9 80

[0DQ 7 09 PAVE 80 SYSTEM CAUSE COMPONENT COMPONENT MANUFACTUREA

~IB CODE CODE COMPONENT CODE SUPPUER VIOIATKIN tocC>~ILcGCa P I P E x x N B 1 3 0 N 7 8 9 10 11 12 17 43 44 47 48 CAUSE DESCRIPTION Q~g Pinhole leak in weld between pipe and elbow. Hole was ground out and repaired using 7 0 9 80

[pgg] proper welding procedure. The piping was visually inspected for leakage after return 7 8 9 80 Q~g to service. CAR 1114 was issued for this event.

7 89 METHOD OF 80 FACILITY STATUS POWER OTHER STATUS DISCOVERY ~ DISCOVERY DESCRIPTION 7

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LEJ 9

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12 13 NA 44 45 b

46 0 erator makin rounds FOAM OF 80 ACTIVITY COATENT AELEASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE Qg H sj NA 7 8 9 10 11 44 45 00 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Pg~oo 7 8 9 o B 12 13 NA 11 80 PERSONNEL INJURIES NUMBER DESCRIPTION fig ~00 0 NA 7 09 ~

11 12 80 OFFSITE CONSEQUENCES Qg NA 7 09 00 LOSS OR DAMAGE TO FACILITY TYPE DESCRIPTION Q~g s 7 09 10 80 PUBLICITY Q~~] ~ e ~ i +II'lI Ej

$ Pl, 7 89 80 ADDITIONAL FACTORS l,lJ ~

NA 7 89 80 7 09 80 NAME: , Dave Hamelink PHDNL.".

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