05000416/LER-1983-169, Corrected LER 83-169/03X-1:on 831023,nitrogen Pressure Control Rod Scram Accumulators 40-53 & 24-29 Fell Below Tech Specs.Caused by Normal Leakage.Accumulators Recharged.W/ 840321 Ltr: Difference between revisions

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#REDIRECT [[05000416/LER-1983-169, Updated LER 83-169/03X-1:on 831023,nitrogen Pressure in Control Rod Scram Accumulators 40-53 & 24-29 Fell Below 1,520 Psig.Caused by Normal Leakage.Pressure Switch & Gauge tested.W/840321 Ltr]]
{{Adams
| number = ML20087P400
| issue date = 03/21/1984
| title = Corrected LER 83-169/03X-1:on 831023,nitrogen Pressure Control Rod Scram Accumulators 40-53 & 24-29 Fell Below Tech Specs.Caused by Normal Leakage.Accumulators Recharged.W/ 840321 Ltr
| author name = Byrd R, Dale L
| author affiliation = MISSISSIPPI POWER & LIGHT CO.
| addressee name = Oreilly J
| addressee affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| docket = 05000416
| license number =
| contact person =
| document report number = AECM-84-0170, AECM-84-170, LER-83-169-03X-01, LER-83-169-3X-1, NUDOCS 8404060386
| document type = LICENSEE EVENT REPORT (SEE ALSO AO RO), TEXT-SAFETY REPORT
| page count = 3
}}
{{LER
| Title = Corrected LER 83-169/03X-1:on 831023,nitrogen Pressure Control Rod Scram Accumulators 40-53 & 24-29 Fell Below Tech Specs.Caused by Normal Leakage.Accumulators Recharged.W/ 840321 Ltr
| Plant =
| Reporting criterion =
| Power level =
| Mode =
| Docket = 05000416
| LER year = 2083
| LER number = 169
| LER revision =
| Event date =
| Report date =
| ENS =
| abstract =
}}
 
=text=
{{#Wiki_filter:-
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            ",'yyf" Updzte Raport - Previous Rsport Date 11/22/83
                                ,                                                    LICENSEE-EVEMT REPORir                    Attachment to AECM-84/0170 Page 1 of 1 CONTROL BLOCK: l              l      l      l  l  l Q
er gagssgl;I nats a tisus m m tempomanaries b l ds Sl 7              e d ucansasccos Gl d 1lh]sO            i+ l C4 i      - 2 OI O    uselmaasumasa d O l Cl - l d Om Q .a4 l 1l          1 lTwo ucous          i h si cxl T ia@
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                                                                    "_{accagT O lsegusan C1 O l 4 S1l 6S h 1lOl            2l 3l E414 3 hl OlmePORT EveufDATE                75 3l2lDATs 1] B lse4lh EVENT D6SCRIPTtOft AfeEP peneimaan s CONSEQUENCEh h GT71 tion October 23, 1983, the nitrogen pressure in control rod scram                                                                                      l K
g l accumulators 40^53 and 24-29 fel1 below 1520 psig. An atcumulator j                .
            .ol4l l trouble alarm was received on accumulator 24-29 but not on accumulator                                                                              l
            ,t l5] l,40-53.                  The low pressuee in 40-53 was found by thrt weekly sur vei l l anc e_.                                                    l ITTe b 1,The required alarm setpoint is 1520 +30, -O psig on decreasing pressure.1
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            ,r T {y] [ A n LCO was entered pursuant to T.S.3.1.3.3.                                                    The accumulators were re-                      l o , geharged within 3 hours. This is reported pursuant to T.S.6.9.1.13.b.                                                                              l
              ?        eo                                                                                                                                              8' "co*E"            E          => =e"na's          courceavr come            = =ca==        sEs Q          g l Rl B l@ ]@ ]@ l Al C l Cl U l 1 U h Z@ Z@
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CAJEE DESCRiPTiM AND COmstECTM AC7 bens h
              - ] (The low pressure is attributed to normal leakage. The pressure switch go                                                                                                                                                          3
                        )g and        pressure gauge were tested fcr setpoint and function and were found l g
to operate correctly. This test was repeated in February and the set-                                                                      3 gp oint had not drifted. The failure to alarm is nct repeatable and is                                                                        g onsidered an isolated event. This is a final report.                                                                                    g a
s                            OTHER STATw                                          Os
                  , ,        sgglol'T'[Roig; m                                                      j g neu surniume.ecOwlety r                    OSS'J4sPnose                  1
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l LOS5 Of on DAMAGE TO FAc8LaTv Tyf      gR4FisOes
              ,        e e            io                                            8404060386 840321                                                                m rusucivv g                              PDR ADOCK 05000416                                              NRC UEE ONLY a o                                                                                                                      I      11Il111111IlI
                ,      , ,            ..                                                                                                = ..                        =s o                                                                          Ron Byrd                                                                          ..
o NAME OF PREPARER                                                                      PHONE-                                      i,
 
N MISSISSIPPI POWER & LIGHT COMPANY Helping Build Mississippi P. O. BOX 1840. J ACKSON. MISSISSIPPI 39205 March 21, 1984 CORRECTED COPY wuctuan enoouenon oseantment          4g3        A 3 *. 4 0 In the second sentence of U.S. Nuclear Regulatory Commission                                letter, 24-59 should have been 24-29, Region II 101 Marietta St.. N.W., Suite 2900 Atlanta, Georgia 30303 Attention:    Mr. J. P. O'Reilly, Regional Administrator
 
==Dear Mr. O'Reilly:==
 
==SUBJECT:==
Grand Gulf Nuclear Station Unit 1 Docket No. 50-416 Licerac No. NPF-13 File: 0260/L-835.0 Update Report - Low Nitrogen Pressure in Control Rod Scram Accumulators LER 83-169/03 X-1 AECM-84/0170 This letter submits an update to a previous report submitted on November 22, 1983. The event for which the report was submitted occurred on October 23, 1983, when the nitrogen pressure in control rod scram accumulatcrs 40-53 and 24-29 iell below 1520 psig. An accumulator trouble alarm was received on accumulator 24-29 but not on accumulator 40-53. The required alarm setpoint is 1520 + 30. -0 psig on decreasing pressure. A Limiting Condition for Operation was entered pursuant to Technical Specification 3.1.3.3. This was reported pursuant to Technical Specification 6.9.1.13.b.
Our investigation into the cause of the alarm failure for accumulator 40-53 is complete. Attached is LER 83-169/03 X-1 which is a final report.
Yours truly, L. F. Dale Manager of Nuclear Services EBS/SHH rg Attachment cc: See next page OFFICI AL COPi, .
74 E E DESIGNATED ORIGINAL Cortified By
                                    .....-....th-,.....t..                                    1p
~-
 
AECM-84/0170 "I*
MISSISSIPPI POWER & LIGHT COMPANY cc: Mr. J. B. Richard (w/a)
Mr. R. B. McGehee (w/o)
Mr. T. B. Conner (w/o)
Mr. G. B. Taylor (w/o)
Mr. Richard C. DeYoung Director (w/a)
Office of Inspection & Enforcement U. S. Nuclear Regulatory Comission Washington, D. C. 20555 Document Control Desk (w/a)
U. S. Nuclear Regulatory Comission Washington, D. C. 20555 s
}}
 
{{LER-Nav}}

Latest revision as of 23:04, 15 April 2020

Corrected LER 83-169/03X-1:on 831023,nitrogen Pressure Control Rod Scram Accumulators 40-53 & 24-29 Fell Below Tech Specs.Caused by Normal Leakage.Accumulators Recharged.W/ 840321 Ltr
ML20087P400
Person / Time
Site: Grand Gulf Entergy icon.png
Issue date: 03/21/1984
From: Byrd R, Dale L
MISSISSIPPI POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
References
AECM-84-0170, AECM-84-170, LER-83-169-03X-01, LER-83-169-3X-1, NUDOCS 8404060386
Download: ML20087P400 (3)


LER-2083-169, Corrected LER 83-169/03X-1:on 831023,nitrogen Pressure Control Rod Scram Accumulators 40-53 & 24-29 Fell Below Tech Specs.Caused by Normal Leakage.Accumulators Recharged.W/ 840321 Ltr
Event date:
Report date:
4162083169R00 - NRC Website

text

-

=

"*""*'**""*""YCC"**""

",'yyf" Updzte Raport - Previous Rsport Date 11/22/83

, LICENSEE-EVEMT REPORir Attachment to AECM-84/0170 Page 1 of 1 CONTROL BLOCK: l l l l l l Q

er gagssgl;I nats a tisus m m tempomanaries b l ds Sl 7 e d ucansasccos Gl d 1lh]sO i+ l C4 i - 2 OI O uselmaasumasa d O l Cl - l d Om Q .a4 l 1l 1 lTwo ucous i h si cxl T ia@

1) ai CON'T

?

o i ,

E g .0

{< O L 61

"_{accagT O lsegusan C1 O l 4 S1l 6S h 1lOl 2l 3l E414 3 hl OlmePORT EveufDATE 75 3l2lDATs 1] B lse4lh EVENT D6SCRIPTtOft AfeEP peneimaan s CONSEQUENCEh h GT71 tion October 23, 1983, the nitrogen pressure in control rod scram l K

g l accumulators 40^53 and 24-29 fel1 below 1520 psig. An atcumulator j .

.ol4l l trouble alarm was received on accumulator 24-29 but not on accumulator l

,t l5] l,40-53. The low pressuee in 40-53 was found by thrt weekly sur vei l l anc e_. l ITTe b 1,The required alarm setpoint is 1520 +30, -O psig on decreasing pressure.1

~

l

,r T {y] [ A n LCO was entered pursuant to T.S.3.1.3.3. The accumulators were re- l o , geharged within 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br />. This is reported pursuant to T.S.6.9.1.13.b. l

? eo 8' "co*E" E => =e"na's courceavr come = =ca== sEs Q g l Rl B l@ ]@ ]@ l Al C l Cl U l 1 U h Z@ Z@

9 10 11 12 13 IS

, m OccumstegeCE sWPORT RTVISION d R 40 tytNTvtAm stancerfescL cues Yvyt sec.

0 3.= 1 * ! 31

,, , h=1 L' l' i ') (<J (34 VJ 171 6J

, ~,=

9 aw p@ =pJ@ . = = ..

=QJ@( w$ @ w[ IOL J O _

}

t i 1 2 C.J@

l"I i#I l@

CAJEE DESCRiPTiM AND COmstECTM AC7 bens h

- ] (The low pressure is attributed to normal leakage. The pressure switch go 3

)g and pressure gauge were tested fcr setpoint and function and were found l g

to operate correctly. This test was repeated in February and the set- 3 gp oint had not drifted. The failure to alarm is nct repeatable and is g onsidered an isolated event. This is a final report. g a

s OTHER STATw Os

, , sgglol'T'[Roig; m j g neu surniume.ecOwlety r OSS'J4sPnose 1

,,,,,, ear,,,, n n ~ = = =

.p. o, y

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l 8, L._1 . L. J@l i ,, . . =

PtR30egestL ENPOSURES i 7 l '7l"8 j@LJ88 1

,,,,,,,,,,, , a, 8, l 071%n j@t"

. . u =

l LOS5 Of on DAMAGE TO FAc8LaTv Tyf gR4FisOes

, e e io 8404060386 840321 m rusucivv g PDR ADOCK 05000416 NRC UEE ONLY a o I 11Il111111IlI

, , , .. = .. =s o Ron Byrd ..

o NAME OF PREPARER PHONE- i,

N MISSISSIPPI POWER & LIGHT COMPANY Helping Build Mississippi P. O. BOX 1840. J ACKSON. MISSISSIPPI 39205 March 21, 1984 CORRECTED COPY wuctuan enoouenon oseantment 4g3 A 3 *. 4 0 In the second sentence of U.S. Nuclear Regulatory Commission letter, 24-59 should have been 24-29, Region II 101 Marietta St.. N.W., Suite 2900 Atlanta, Georgia 30303 Attention: Mr. J. P. O'Reilly, Regional Administrator

Dear Mr. O'Reilly:

SUBJECT:

Grand Gulf Nuclear Station Unit 1 Docket No. 50-416 Licerac No. NPF-13 File: 0260/L-835.0 Update Report - Low Nitrogen Pressure in Control Rod Scram Accumulators LER 83-169/03 X-1 AECM-84/0170 This letter submits an update to a previous report submitted on November 22, 1983. The event for which the report was submitted occurred on October 23, 1983, when the nitrogen pressure in control rod scram accumulatcrs 40-53 and 24-29 iell below 1520 psig. An accumulator trouble alarm was received on accumulator 24-29 but not on accumulator 40-53. The required alarm setpoint is 1520 + 30. -0 psig on decreasing pressure. A Limiting Condition for Operation was entered pursuant to Technical Specification 3.1.3.3. This was reported pursuant to Technical Specification 6.9.1.13.b.

Our investigation into the cause of the alarm failure for accumulator 40-53 is complete. Attached is LER 83-169/03 X-1 which is a final report.

Yours truly, L. F. Dale Manager of Nuclear Services EBS/SHH rg Attachment cc: See next page OFFICI AL COPi, .

74 E E DESIGNATED ORIGINAL Cortified By

.....-....th-,.....t.. 1p

~-

AECM-84/0170 "I*

MISSISSIPPI POWER & LIGHT COMPANY cc: Mr. J. B. Richard (w/a)

Mr. R. B. McGehee (w/o)

Mr. T. B. Conner (w/o)

Mr. G. B. Taylor (w/o)

Mr. Richard C. DeYoung Director (w/a)

Office of Inspection & Enforcement U. S. Nuclear Regulatory Comission Washington, D. C. 20555 Document Control Desk (w/a)

U. S. Nuclear Regulatory Comission Washington, D. C. 20555 s