ML13280A907: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
 
(9 intermediate revisions by the same user not shown)
Line 2: Line 2:
| number = ML13280A907
| number = ML13280A907
| issue date = 10/29/2013
| issue date = 10/29/2013
| title = Davis-Besse Nuclear Power Station, Unit No. 1 Review of the Spring 2012 Steam Generator Tube Inspections (TAC No. MF0316)(L-12-274)
| title = Review of the Spring 2012 Steam Generator Tube Inspections (TAC No. MF0316)(L-12-274)
| author name = Brown E A
| author name = Brown E
| author affiliation = NRC/NRR/DORL/LPLIII-2
| author affiliation = NRC/NRR/DORL/LPLIII-2
| addressee name = Lieb R A
| addressee name = Lieb R
| addressee affiliation = FirstEnergy Nuclear Operating Co
| addressee affiliation = FirstEnergy Nuclear Operating Co
| docket = 05000346
| docket = 05000346
Line 14: Line 14:
| page count = 4
| page count = 4
| project = TAC:MF0316
| project = TAC:MF0316
| stage =  
| stage = Approval
}}
}}


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:October 29, 2013 Mr. Raymond A. Lieb Site Vice President FirstEnergy Nuclear Operating Company Mail Stop A-DB-3080 5501 North State, Route 2 Oak Harbor, OH 43449-9760
October 29, 2013
 
Mr. Raymond A. Lieb Site Vice President FirstEnergy Nuclear Operating Company Mail Stop A-DB-3080 5501 North State, Route 2 Oak Harbor, OH 43449-9760  


==SUBJECT:==
==SUBJECT:==
DAVIS-BESSE NUCLEAR POWER STATION, UNIT NO. 1 - REVIEW   OF THE SPRING 2012 STEAM GENERATOR TUBE INSPECTIONS   (TAC NO. MF0316)(L-12-274)  
DAVIS-BESSE NUCLEAR POWER STATION, UNIT NO. 1 - REVIEW OF THE SPRING 2012 STEAM GENERATOR TUBE INSPECTIONS (TAC NO. MF0316)(L-12-274)


==Dear Mr. Lieb:==
==Dear Mr. Lieb:==


By letters dated August 20, 2012 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML12234A484), and November 30, 2012 (ADAMS Accession No. ML12339A071), FirstEnergy Nuclear Operating Company (the licensee) submitted information summarizing the results of the 2012 steam generator (SG) tube inspections at Davis-Besse Nuclear Power Station (DBNPS), Unit 1 during refueling outage 17. In addition to this report, the U.S. Nuclear Regulatory Commission staff summarized a conference call about the 2012 SG tube inspections at DBNPS in a letter dated July 16, 2012 (ADAMS Accession No. ML12167A026).  
By letters dated August 20, 2012 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML12234A484), and November 30, 2012 (ADAMS Accession No. ML12339A071), FirstEnergy Nuclear Operating Company (the licensee) submitted information summarizing the results of the 2012 steam generator (SG) tube inspections at Davis-Besse Nuclear Power Station (DBNPS), Unit 1 during refueling outage 17. In addition to this report, the U.S. Nuclear Regulatory Commission staff summarized a conference call about the 2012 SG tube inspections at DBNPS in a letter dated July 16, 2012 (ADAMS Accession No. ML12167A026).
 
The NRC staff has completed its review of the submittals pertaining to the DBNPS, Unit No. 1, SG inspections, and the associated review summary is enclosed. The NRC staff finds that the licensee has provided the information required by the technical specifications. In addition, the staff did not identify any technical issues that warrant follow-up action at this time. Based on these considerations, the subject TAC is being closed.
The NRC staff has completed its review of the submittals pertaining to the DBNPS, Unit No. 1, SG inspections, and the associated review summary is enclosed. The NRC staff finds that the licensee has provided the information required by the technical specifications. In addition, the staff did not identify any technical issues that warrant follow-up action at this time. Based on these considerations, the subject TAC is being closed.
Sincerely,
Sincerely,         / RA / Eva A. Brown, Senior Project Manager Plant Licensing Branch III-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-346  
                                              / RA /
Eva A. Brown, Senior Project Manager Plant Licensing Branch III-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-346


==Enclosure:==
==Enclosure:==
Steam Generator Review Summary cc w/encl:  Distribution via Listserv Mr. Raymond A. Lieb Site Vice President FirstEnergy Nuclear Operating Company Mail Stop A-DB-3080 5501 North State, Route 2 Oak Harbor, OH  43449-9760
==SUBJECT:==
DAVIS-BESSE NUCLEAR POWER STATION, UNIT NO. 1 - REVIEW OF THE SPRING 2012 STEAM GENERATOR TUBE INSPECTIONS  (TAC NO. MF0316)(L-12-274) 


==Dear Mr. Lieb:==
Steam Generator Review Summary cc w/encl: Distribution via Listserv


By letters dated August 20, 2012 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML12234A484), and November 30, 2012 (ADAMS Accession No. ML12339A071), FirstEnergy Nuclear Operating Company (the licensee) submitted information summarizing the results of the 2012 steam generator (SG) tube inspections at Davis-Besse Nuclear Power Station (DBNPS), Unit 1 during refueling outage 17. In addition to this report, the U.S. Nuclear Regulatory Commission staff summarized a conference call about the 2012 SG tube inspections at DBNPS in a letter dated July 16, 2012 (ADAMS Accession No. ML12167A026).  
ML12339A071), FirstEnergy Nuclear Operating Company (the licensee) submitted information summarizing the results of the 2012 steam generator (SG) tube inspections at Davis-Besse Nuclear Power Station (DBNPS), Unit 1 during refueling outage 17. In addition to this report, the U.S. Nuclear Regulatory Commission staff summarized a conference call about the 2012 SG tube inspections at DBNPS in a letter dated July 16, 2012 (ADAMS Accession No. ML12167A026).
The NRC staff has completed its review of the submittals pertaining to the DBNPS, Unit No. 1, SG inspections, and the associated review summary is enclosed. The NRC staff finds that the licensee has provided the information required by the technical specifications. In addition, the staff did not identify any technical issues that warrant follow-up action at this time. Based on these considerations, the subject TAC is being closed.
Sincerely,
                                                    / RA /
Eva A. Brown, Senior Project Manager Plant Licensing Branch III-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-346


The NRC staff has completed its review of the submittals pertaining to the DBNPS, Unit No. 1,  SG inspections, and the associated review summary is enclosed. The NRC staff finds that the licensee has provided the information required by the technical specifications. In addition, the staff did not identify any technical issues that warrant follow-up action at this time. Based on these considerations, the subject TAC is being closed.
==Enclosure:==
Sincerely,      / RA / Eva A. Brown, Senior Project Manager  Plant Licensing Branch III-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-346 Enclosure: Steam Generator Review Summary


cc w/encl: Distribution via Listserv DISTRIBUTION: PUBLIC   LPLIII-2 R/F RidsNrrDorlLplIII-2 RidsNrrPMDavis-Besse AJohnson, NRR   RidsNrrLASRohrer   RidsRgn3MailCenter Resource RidsOgcRp   RidsNrrDeEsgb RidsAcrsAcnw_MailCTR   KKarwoski, NRR ADAMS Accession No. ML13280A907
Steam Generator Review Summary cc w/encl: Distribution via Listserv DISTRIBUTION:
* via memo OFFICE NRR/DORL/LPLIII-2/PM NRR/DORL/LPLIII-2/LA NRR/DE/ESGB* NRR/DORL/LPLIII-2/BC NAME EBrown SRohrer GKulesa TTate DATE 10/ 21 /13 10/ 8 /13 8/27/2013 10/ 29 /13                   OFFICIAL RECORD COPY
PUBLIC                           LPLIII-2 R/F               RidsNrrDorlLplIII-2 RidsNrrPMDavis-Besse             AJohnson, NRR             RidsNrrLASRohrer RidsRgn3MailCenter Resource       RidsOgcRp                 RidsNrrDeEsgb RidsAcrsAcnw_MailCTR             KKarwoski, NRR ADAMS Accession No. ML13280A907
 
* via memo OFFICE     NRR/DORL/LPLIII-2/PM       NRR/DORL/LPLIII-2/LA     NRR/DE/ESGB*           NRR/DORL/LPLIII-2/BC EBrown                     SRohrer                   GKulesa                 TTate NAME 10/ 21 /13                 10/ 8 /13                 8/27/2013               10/ 29 /13 DATE STAFF EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO THE STEAM GENERATOR TUBE INSPECTIONS PERFORMED DURING THE 2012 REFUELING OUTAGE NO. 17 DAVIS-BESSE NUCLEAR POWER STATION FIRSTENERGY NUCLEAR OPERATING COMPANY UNIT NO. 1 DOCKET NO. 50-346 By letters dated August 20, 2012 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML12234A484), and November 30, 2012 (ADAMS Accession No. ML12339A071), FirstEnergy Nuclear Operating Company (the licensee) submitted information summarizing the results of the 2012 steam generator (SG) tube inspections at Davis-Besse Nuclear Power Station (DBNPS), Unit 1 during refueling outage 17. In addition to this report, the U.S. Nuclear Regulatory Commission (NRC) staff summarized a conference call about the 2012 SG tube inspections at DBNPS in a letter dated July 16, 2012 (ADAMS Accession No. ML12167A026).
STAFF EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION   RELATED TO THE STEAM GENERATOR TUBE INSPECTIONS PERFORMED DURING THE 2012 REFUELING OUTAGE NO. 17 DAVIS-BESSE NUCLEAR POWER STATION FIRSTENERGY NUCLEAR OPERATING COMPANY UNIT NO. 1 DOCKET NO. 50-346   By letters dated August 20, 2012 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML12234A484), and November 30, 2012 (ADAMS Accession No. ML12339A071), FirstEnergy Nuclear Operating Company (the licensee) submitted information summarizing the results of the 2012 steam generator (SG) tube inspections at Davis-Besse Nuclear Power Station (DBNPS), Unit 1 during refueling outage 17. In addition to this report, the U.S. Nuclear Regulatory Commission (NRC) staff summarized a conference call about the 2012 SG tube inspections at DBNPS in a letter dated July 16, 2012 (ADAMS Accession No. ML12167A026).  
There are two Babcock and Wilcox once-through steam generators (OTSG), designated 1-B and 2-A, at DBNPS. Each SG has approximately 15,500 Alloy 600 tubes in the mill-annealed condition. The tubes have a nominal outside diameter of 0.625 inches and a nominal wall thickness of 0.037 inches. Both OTSG 1-B and 2-A contain tubes with sleeves and tubes with shop re-rolls.
 
The licensee provided the scope, extent, methods, and results of their SG tube inspections in the documents referenced above. In addition, the licensee described corrective actions, e.g.,
There are two Babcock and Wilcox once-through steam generators (OTSG), designated 1-B and 2-A, at DBNPS. Each SG has approximately 15,500 Alloy 600 tubes in the mill-annealed condition. The tubes have a nominal outside diameter of 0.625 inches and a nominal wall thickness of 0.037 inches. Both OTSG 1-B and 2-A contain tubes with sleeves and tubes with shop re-rolls.  
tube plugging, taken in response to the inspection findings.
 
The licensee provided the scope, extent, methods, and results of their SG tube inspections in the documents referenced above. In addition, the licensee described corrective actions, e.g., tube plugging, taken in response to the inspection findings.
As a result of the review of the information provided by the licensee, the NRC staff has the following comments/observations:
As a result of the review of the information provided by the licensee, the NRC staff has the following comments/observations:
* In a conference call with the NRC on May 9, 2013, the licensee confirmed that the equivalent plugging percentage in SG-2A is 937 tubes, and that all tubes in the 2012 inspections with detected indications attributed to corrosion were plugged during the 2012 outage.
* In a conference call with the NRC on May 9, 2013, the licensee confirmed that the equivalent plugging percentage in SG-2A is 937 tubes, and that all tubes in the 2012 inspections with detected indications attributed to corrosion were plugged during the 2012 outage.
* The 2012 inspections were the last scheduled inspections for these SGs, which are scheduled to be replaced in the spring of 2014.
* The 2012 inspections were the last scheduled inspections for these SGs, which are scheduled to be replaced in the spring of 2014.
ENCLOSURE


ENCLOSURE
Based on a review of the information provided, the staff concludes that the licensee provided the information required by their technical specifications. In general, the SG tube inspections at DBNPS appear to be consistent with the objective of detecting potential tube degradation and the inspection results appear to be consistent with industry operating experience at similarly-designed and operated units.
          -2-Based on a review of the information provided, the staff concludes that the licensee provided the information required by their technical specifications. In general, the SG tube inspections at DBNPS appear to be consistent with the objective of detecting potential tube degradation and the inspection results appear to be consistent with industry operating experience at similarly-designed and operated units.  
The NRC staffs review did not reveal any issues warranting follow-up action.}}
 
The NRC staff's review did not reveal any issues warranting follow-up action.
}}

Latest revision as of 02:19, 6 February 2020

Review of the Spring 2012 Steam Generator Tube Inspections (TAC No. MF0316)(L-12-274)
ML13280A907
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 10/29/2013
From: Ellen Brown
Plant Licensing Branch III
To: Lieb R
FirstEnergy Nuclear Operating Co
Eva Brown, NRR/DORL 415-2315
References
L-12-274, TAC MF0316
Download: ML13280A907 (4)


Text

October 29, 2013 Mr. Raymond A. Lieb Site Vice President FirstEnergy Nuclear Operating Company Mail Stop A-DB-3080 5501 North State, Route 2 Oak Harbor, OH 43449-9760

SUBJECT:

DAVIS-BESSE NUCLEAR POWER STATION, UNIT NO. 1 - REVIEW OF THE SPRING 2012 STEAM GENERATOR TUBE INSPECTIONS (TAC NO. MF0316)(L-12-274)

Dear Mr. Lieb:

By letters dated August 20, 2012 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML12234A484), and November 30, 2012 (ADAMS Accession No. ML12339A071), FirstEnergy Nuclear Operating Company (the licensee) submitted information summarizing the results of the 2012 steam generator (SG) tube inspections at Davis-Besse Nuclear Power Station (DBNPS), Unit 1 during refueling outage 17. In addition to this report, the U.S. Nuclear Regulatory Commission staff summarized a conference call about the 2012 SG tube inspections at DBNPS in a letter dated July 16, 2012 (ADAMS Accession No. ML12167A026).

The NRC staff has completed its review of the submittals pertaining to the DBNPS, Unit No. 1, SG inspections, and the associated review summary is enclosed. The NRC staff finds that the licensee has provided the information required by the technical specifications. In addition, the staff did not identify any technical issues that warrant follow-up action at this time. Based on these considerations, the subject TAC is being closed.

Sincerely,

/ RA /

Eva A. Brown, Senior Project Manager Plant Licensing Branch III-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-346

Enclosure:

Steam Generator Review Summary cc w/encl: Distribution via Listserv

ML12339A071), FirstEnergy Nuclear Operating Company (the licensee) submitted information summarizing the results of the 2012 steam generator (SG) tube inspections at Davis-Besse Nuclear Power Station (DBNPS), Unit 1 during refueling outage 17. In addition to this report, the U.S. Nuclear Regulatory Commission staff summarized a conference call about the 2012 SG tube inspections at DBNPS in a letter dated July 16, 2012 (ADAMS Accession No. ML12167A026).

The NRC staff has completed its review of the submittals pertaining to the DBNPS, Unit No. 1, SG inspections, and the associated review summary is enclosed. The NRC staff finds that the licensee has provided the information required by the technical specifications. In addition, the staff did not identify any technical issues that warrant follow-up action at this time. Based on these considerations, the subject TAC is being closed.

Sincerely,

/ RA /

Eva A. Brown, Senior Project Manager Plant Licensing Branch III-2 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket No. 50-346

Enclosure:

Steam Generator Review Summary cc w/encl: Distribution via Listserv DISTRIBUTION:

PUBLIC LPLIII-2 R/F RidsNrrDorlLplIII-2 RidsNrrPMDavis-Besse AJohnson, NRR RidsNrrLASRohrer RidsRgn3MailCenter Resource RidsOgcRp RidsNrrDeEsgb RidsAcrsAcnw_MailCTR KKarwoski, NRR ADAMS Accession No. ML13280A907

  • via memo OFFICE NRR/DORL/LPLIII-2/PM NRR/DORL/LPLIII-2/LA NRR/DE/ESGB* NRR/DORL/LPLIII-2/BC EBrown SRohrer GKulesa TTate NAME 10/ 21 /13 10/ 8 /13 8/27/2013 10/ 29 /13 DATE STAFF EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO THE STEAM GENERATOR TUBE INSPECTIONS PERFORMED DURING THE 2012 REFUELING OUTAGE NO. 17 DAVIS-BESSE NUCLEAR POWER STATION FIRSTENERGY NUCLEAR OPERATING COMPANY UNIT NO. 1 DOCKET NO. 50-346 By letters dated August 20, 2012 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML12234A484), and November 30, 2012 (ADAMS Accession No. ML12339A071), FirstEnergy Nuclear Operating Company (the licensee) submitted information summarizing the results of the 2012 steam generator (SG) tube inspections at Davis-Besse Nuclear Power Station (DBNPS), Unit 1 during refueling outage 17. In addition to this report, the U.S. Nuclear Regulatory Commission (NRC) staff summarized a conference call about the 2012 SG tube inspections at DBNPS in a letter dated July 16, 2012 (ADAMS Accession No. ML12167A026).

There are two Babcock and Wilcox once-through steam generators (OTSG), designated 1-B and 2-A, at DBNPS. Each SG has approximately 15,500 Alloy 600 tubes in the mill-annealed condition. The tubes have a nominal outside diameter of 0.625 inches and a nominal wall thickness of 0.037 inches. Both OTSG 1-B and 2-A contain tubes with sleeves and tubes with shop re-rolls.

The licensee provided the scope, extent, methods, and results of their SG tube inspections in the documents referenced above. In addition, the licensee described corrective actions, e.g.,

tube plugging, taken in response to the inspection findings.

As a result of the review of the information provided by the licensee, the NRC staff has the following comments/observations:

  • In a conference call with the NRC on May 9, 2013, the licensee confirmed that the equivalent plugging percentage in SG-2A is 937 tubes, and that all tubes in the 2012 inspections with detected indications attributed to corrosion were plugged during the 2012 outage.
  • The 2012 inspections were the last scheduled inspections for these SGs, which are scheduled to be replaced in the spring of 2014.

ENCLOSURE

Based on a review of the information provided, the staff concludes that the licensee provided the information required by their technical specifications. In general, the SG tube inspections at DBNPS appear to be consistent with the objective of detecting potential tube degradation and the inspection results appear to be consistent with industry operating experience at similarly-designed and operated units.

The NRC staffs review did not reveal any issues warranting follow-up action.