ML18113A320: Difference between revisions
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| issue date = 08/06/1976 | | issue date = 08/06/1976 | ||
| title = LER 1976-034-00 for St. Lucie Unit 1, in Order to Compensate for Errors Found in NSSS Vendor'S Strikin II Computer Code, Several Instrumentation and Control Setpoints Were Adjusted | | title = LER 1976-034-00 for St. Lucie Unit 1, in Order to Compensate for Errors Found in NSSS Vendor'S Strikin II Computer Code, Several Instrumentation and Control Setpoints Were Adjusted | ||
| author name = Schmidt A | | author name = Schmidt A | ||
| author affiliation = Florida Power & Light Co | | author affiliation = Florida Power & Light Co | ||
| addressee name = Moseley N | | addressee name = Moseley N | ||
| addressee affiliation = NRC/IE, NRC/RGN-II | | addressee affiliation = NRC/IE, NRC/RGN-II | ||
| docket = 05000335, 05000389 | | docket = 05000335, 05000389 | ||
Line 17: | Line 17: | ||
=Text= | =Text= | ||
{{#Wiki_filter:NRC Pv>1M 106 | {{#Wiki_filter:NRC Pv>1M 106 U.S. NUCLEAR REGULATORY C SION DOCKET NUMBER g.voI 50-335 FILE NUMBER NRC DISTRIBUTION FoR PART 60 DOCKET MATERIAL INCIDIWT RI"PORT TO: FROM: DATE OF DOCUMENT Florida'Power & Light Company 8/6/76 Mr. Norman C. Moseley Miami, Florida DATE RECEIVED A. D S'chmidt 9/l/76 LFTTER QNOTORIZED PROP INPUT FORM NUMBER OF COPIES RECEIVED jgoRIDINAL C3coPY g UN C LASS IF I E D I | ||
&Light Company Miami, Florida A.D S'chmidt | ~ 8 ~g ~ j ~ | ||
One signed | |||
('-').DONOV H,ZMOVZ NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J.COLLINS BRANCH CHIEF: W Cr8 1OR ACTION LIC..ASST.: | ~ I l~myv DESCRIPTION ENCLOSURE Ltr. trans the following: Licensee Event Report (RO 50-335-76-34) on 7/6/76 concerning corrective measures taken to compensate for errors found in the NSSS vendor's STRIKIN II computer code. | ||
W CYS ACRS CYS HOLDING S | ACKNOWLEDGED (l-P) ('-') .DONOV H,ZMOVZ PLANT NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J .COLLINS mIE't. | ||
Lucie Nl FOR ACTION/INFORMATION 9 2 76 RJL BRANCH CHIEF: Ziemann W Cr8 1OR ACTION LIC..ASST.: Di s W CYS ACRS CYS HOLDING S TO LA INTERNAL D IST R I BUTION NRC PDR IREE 2 MIPC SCHROEDER IPPOLITO HOUSTON NOVAK CHECK GRIMES CASE ~ ~ | |||
TEDESCO MACCARY EISENHUT SHAO VOLIZER BUNCH GER J. COLLINS EXTERNAL DISTRIBUTION CONTROL NUMBER LPDR: Ft. Pierce Fla. ~ | |||
g pig %>11 TIC: Irrwa | |||
0 I | |||
~ | F | ||
~ 4 5 ffpJp li i) v g/( llig pl | |||
~ E W1 | |||
P.O. SOX 0I3I00, MIAMI, FLORIDA 33IO'I cas ~gagulaelIX@~'" | |||
LK4ENSEE NAME[OD1]8 L S L S 1 0 | ~ ~gilllg | ||
[pp~]In order to compensate for errors found in the NSSS Vendor's STRIKIN II 7 8 9 80[QQ3]computer code (see LER 335-7 6-3 1), several instrumentation and control 7 8 9~80 top~]setpoints were adjusted.The adjustment factor for the core local 7 8 9 80[0D~]ower densit alarm was 1.24 however on Jul 6 a nonconservative 7 8 9 80 gg value of 1.1 was set into the instrumentation. | =-"O'a FLORIDA POWER 5 LIGHT COMPANY August 6, 1976 PRN-LI-76-199 tt | ||
The error was found | ~If,"P Mr. Norman C. Moseley, Director, Region XI Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 818 Atlanta, Georgia 30303 g,S, ~+~~INI08 C~I ~IIaII | ||
~I~AANNUNCNF120 | |||
~0 8 A nonconservative adjustment factor was set into | ==Dear Mr. Moseley:== | ||
~z~00 8 7 8 9 11 12 13 PERSONNEL INJURIES EH.LoL~ | REPORTABLE OCCURRENCE 335-76-34 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: JULY 6, 1976 LOCAL POWER DENSITY ALARM SETPOINT The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject. occurrence. | ||
Very truly yours, D. Schmidt Vice President Power Resources MAS/bfp Attachment cc: Jack R. Newman, Esquire Director, Office of Inspection and Enforcement (30) | |||
approximately 8 hours later during a review of the setpoints, ,and the setpoint for the core local power density alarm was corrected. | Director, Office of Management Information and Program Control (3) | ||
Review of the Digital Data Processor printout for this 8 hour period showed that there was no time during which operation was in noncompliance with the requirements of Technical Specification 3.2.1 for a revised linear heat rate limit of 12.7 kw/ft.This was the first occurrence of this type at St.Lucie Unit, l.(335-76-34) | HELPING BUILD FLORIDA | ||
Cause Description (Continued): | |||
LICENSEE EVENT REPORT CONTROL BLOCK: (PLEASE PRINT ALL RECIUIRED INFORMATION) | |||
LK4ENSEE UCENSE EVENT NAME LICENSE NUMBER TYPE TYPE | |||
[OD1] 8 L S L S 1 0 0 0 0 0 0 0 0 0 4 1 1 1 1 ~03 89 | |||
~ | |||
7 14 15 25 26 30 31 32 REPORT REPORT | |||
, CATEGORY TYPE SOURCE ~ | |||
DOCKET NUMBER EVENT OATE REPORT OATE QpgooN7 ~L ~L p 5 p p 3 3 5 0 7 0 6 7 6 0 8 0 6 7 6 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTION | |||
[pp~] In order to compensate for errors found in the NSSS Vendor's STRIKIN II 7 8 9 80 | |||
[QQ3] | |||
computer code ( see LER 335-7 6-3 1 ), several instrumentation and control 7 8 9 ~ | |||
80 top~] setpoints were adjusted. The adjustment factor for the core local 7 8 9 80 | |||
[0D~] ower densit alarm was 1.24 however on Jul 6 a nonconservative 7 8 9 80 gg value of 1.1 was set into the instrumentation. The error was found 7 8 9 PRME 80 7 | |||
~I~AANNUNCNF120 8 9 10 SYSTEM COBE CAUSE COBE 11 12 COMPONENT COOE 17 COMPONENT SUPPUER 43 44 COMPONENT MANUFACTURER 47 N | |||
48 CAUSE DESCRIPTION | |||
~0 8 A nonconservative adjustment factor was set into the Incore Detector 7 8 9 80 | |||
[oO~] S stem because of ersonnel error. A memorandum which lists the ro er 7 8 9 80 | |||
,Q~O set oin a d r ss 'm 7 89 80 FACRJTY METHOO OF STATUS 5 POWER OTHER STATUS OISCOVERY DISCOVERY OESCRIPTION | |||
~B ~08 0 N/A C N/A 7 8 9 10 12 13 44 45 46 80 FORM OF ACTIViTY COATENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE Q~g z z N/A N/A 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE OESCRIPTION | |||
~z ~00 8 N/A 7 8 9 11 12 13 80 PERSONNEL INJURIES EH. | |||
7 89 LoL~ 11 12 N A 80 PROBABLE CONSEQUENCES | |||
[<is] N/A 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE OESCRIPTION 7 | |||
HE89LzJ 10 80 PUBLICITY 7 89 ~ 80 ADDITIONAL FACTORS'ee 7 | |||
a e two for continuation of Event Descri tion and Cause 8 9 | |||
~99 Description. | |||
7 89 NAME: | |||
M.A.Schoppman PHONE'0 305/552-3779 GPO Spl GOT | |||
REPORTABLE OCCURRENCE 335-76-34 LICENSEE EVENT REPORT Pa e Two Event Descri tion (Continued): | |||
approximately 8 hours later during a review of the setpoints, | |||
,and the setpoint for the core local power density alarm was corrected. Review of the Digital Data Processor printout for this 8 hour period showed that there was no time during which operation was in noncompliance with the requirements of Technical Specification 3.2.1 for a revised linear heat rate limit of 12.7 kw/ft. This was the first occurrence of this type at St. Lucie Unit, l. (335-76-34) | |||
Cause Description (Continued): | |||
distributed for review by appropriate personnel.}} | distributed for review by appropriate personnel.}} |
Latest revision as of 03:26, 3 February 2020
ML18113A320 | |
Person / Time | |
---|---|
Site: | Saint Lucie |
Issue date: | 08/06/1976 |
From: | Schmidt A Florida Power & Light Co |
To: | Moseley N NRC/IE, NRC/RGN-II |
References | |
PRN-LI-76-199 LER 1976-034-00 | |
Download: ML18113A320 (7) | |
Text
NRC Pv>1M 106 U.S. NUCLEAR REGULATORY C SION DOCKET NUMBER g.voI 50-335 FILE NUMBER NRC DISTRIBUTION FoR PART 60 DOCKET MATERIAL INCIDIWT RI"PORT TO: FROM: DATE OF DOCUMENT Florida'Power & Light Company 8/6/76 Mr. Norman C. Moseley Miami, Florida DATE RECEIVED A. D S'chmidt 9/l/76 LFTTER QNOTORIZED PROP INPUT FORM NUMBER OF COPIES RECEIVED jgoRIDINAL C3coPY g UN C LASS IF I E D I
~ 8 ~g ~ j ~
One signed
~ I l~myv DESCRIPTION ENCLOSURE Ltr. trans the following: Licensee Event Report (RO 50-335-76-34) on 7/6/76 concerning corrective measures taken to compensate for errors found in the NSSS vendor's STRIKIN II computer code.
ACKNOWLEDGED (l-P) ('-') .DONOV H,ZMOVZ PLANT NOTE: IF PERSONNEL EXPOSURE IS INVOLVED SEND DIRECTLY TO KREGER/J .COLLINS mIE't.
Lucie Nl FOR ACTION/INFORMATION 9 2 76 RJL BRANCH CHIEF: Ziemann W Cr8 1OR ACTION LIC..ASST.: Di s W CYS ACRS CYS HOLDING S TO LA INTERNAL D IST R I BUTION NRC PDR IREE 2 MIPC SCHROEDER IPPOLITO HOUSTON NOVAK CHECK GRIMES CASE ~ ~
TEDESCO MACCARY EISENHUT SHAO VOLIZER BUNCH GER J. COLLINS EXTERNAL DISTRIBUTION CONTROL NUMBER LPDR: Ft. Pierce Fla. ~
g pig %>11 TIC: Irrwa
0 I
F
~ 4 5 ffpJp li i) v g/( llig pl
~ E W1
P.O. SOX 0I3I00, MIAMI, FLORIDA 33IO'I cas ~gagulaelIX@~'"
~ ~gilllg
=-"O'a FLORIDA POWER 5 LIGHT COMPANY August 6, 1976 PRN-LI-76-199 tt
~If,"P Mr. Norman C. Moseley, Director, Region XI Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 818 Atlanta, Georgia 30303 g,S, ~+~~INI08 C~I ~IIaII
Dear Mr. Moseley:
REPORTABLE OCCURRENCE 335-76-34 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: JULY 6, 1976 LOCAL POWER DENSITY ALARM SETPOINT The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30-day notification of the subject. occurrence.
Very truly yours, D. Schmidt Vice President Power Resources MAS/bfp Attachment cc: Jack R. Newman, Esquire Director, Office of Inspection and Enforcement (30)
Director, Office of Management Information and Program Control (3)
HELPING BUILD FLORIDA
LICENSEE EVENT REPORT CONTROL BLOCK: (PLEASE PRINT ALL RECIUIRED INFORMATION)
LK4ENSEE UCENSE EVENT NAME LICENSE NUMBER TYPE TYPE
[OD1] 8 L S L S 1 0 0 0 0 0 0 0 0 0 4 1 1 1 1 ~03 89
~
7 14 15 25 26 30 31 32 REPORT REPORT
, CATEGORY TYPE SOURCE ~
DOCKET NUMBER EVENT OATE REPORT OATE QpgooN7 ~L ~L p 5 p p 3 3 5 0 7 0 6 7 6 0 8 0 6 7 6 7 8 57 58 59 60 61 68 69 74 75 80 EVENT DESCRIPTION
[pp~] In order to compensate for errors found in the NSSS Vendor's STRIKIN II 7 8 9 80
[QQ3]
computer code ( see LER 335-7 6-3 1 ), several instrumentation and control 7 8 9 ~
80 top~] setpoints were adjusted. The adjustment factor for the core local 7 8 9 80
[0D~] ower densit alarm was 1.24 however on Jul 6 a nonconservative 7 8 9 80 gg value of 1.1 was set into the instrumentation. The error was found 7 8 9 PRME 80 7
~I~AANNUNCNF120 8 9 10 SYSTEM COBE CAUSE COBE 11 12 COMPONENT COOE 17 COMPONENT SUPPUER 43 44 COMPONENT MANUFACTURER 47 N
48 CAUSE DESCRIPTION
~0 8 A nonconservative adjustment factor was set into the Incore Detector 7 8 9 80
[oO~] S stem because of ersonnel error. A memorandum which lists the ro er 7 8 9 80
,Q~O set oin a d r ss 'm 7 89 80 FACRJTY METHOO OF STATUS 5 POWER OTHER STATUS OISCOVERY DISCOVERY OESCRIPTION
~B ~08 0 N/A C N/A 7 8 9 10 12 13 44 45 46 80 FORM OF ACTIViTY COATENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE Q~g z z N/A N/A 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE OESCRIPTION
~z ~00 8 N/A 7 8 9 11 12 13 80 PERSONNEL INJURIES EH.
7 89 LoL~ 11 12 N A 80 PROBABLE CONSEQUENCES
[<is] N/A 7 8 9 80 LOSS OR DAMAGE TO FACILITY TYPE OESCRIPTION 7
HE89LzJ 10 80 PUBLICITY 7 89 ~ 80 ADDITIONAL FACTORS'ee 7
a e two for continuation of Event Descri tion and Cause 8 9
~99 Description.
7 89 NAME:
M.A.Schoppman PHONE'0 305/552-3779 GPO Spl GOT
REPORTABLE OCCURRENCE 335-76-34 LICENSEE EVENT REPORT Pa e Two Event Descri tion (Continued):
approximately 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> later during a review of the setpoints,
,and the setpoint for the core local power density alarm was corrected. Review of the Digital Data Processor printout for this 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> period showed that there was no time during which operation was in noncompliance with the requirements of Technical Specification 3.2.1 for a revised linear heat rate limit of 12.7 kw/ft. This was the first occurrence of this type at St. Lucie Unit, l. (335-76-34)
Cause Description (Continued):
distributed for review by appropriate personnel.