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| issue date = 06/10/1976
| issue date = 06/10/1976
| title = LER 1976-09-00 for St. Lucie Unit 1, Mechanical Pipe Restraints Supplementary Report No. 1
| title = LER 1976-09-00 for St. Lucie Unit 1, Mechanical Pipe Restraints Supplementary Report No. 1
| author name = Schmidt A D
| author name = Schmidt A
| author affiliation = Florida Power & Light Co
| author affiliation = Florida Power & Light Co
| addressee name = Moseley N C
| addressee name = Moseley N
| addressee affiliation = NRC/IE, NRC/RGN-II
| addressee affiliation = NRC/IE, NRC/RGN-II
| docket = 05000335, 05000389
| docket = 05000335, 05000389
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:NIIC FOflM 195 U.S.NUCLGAA flGOULATOIIV COMMIS ION DOCKET NUMOEf1 I 2-701~t NBC DISTBIOUTION Fol I ART 50 DOCKET MATERIAL 50-336 FILE NUMOL'll INCIDI',NT REPORT N.C.Mgs'eley FRoM:Flordia Power.8'ight Co.Miami, Flordia A.D.Schmidt DATE OF DOCUMENT 6-10-76 DATE RECEIVED 6-17-.76 QLCTTEA QOAIGINAL EICOPV ONOTOAIZGD
{{#Wiki_filter:NIIC FOflM 195                                             U.S. NUCLGAA flGOULATOIIVCOMMIS ION DOCKET NUMOEf1 I 2-701                                                                                                 50-336
@UNCLASSIFIED PROP INPUT FOAM NUMOGA OF COPIES AGCEIVFD DESCRIPTION Ltr..trans the.following......,.'0 ENCLOSURE Licensee Event Report (R.O.76-9)on.,3-31-76
~t FILE NUMOL'll NBC DISTBIOUTION Fol       I   ART 50 DOCKET MATERIAL                           INCIDI',NT REPORT N.C. Mgs'eley FRoM:Flordia   Power. 8'ight   Co.       DATE OF DOCUMENT Miami, Flordia                             6-10-76 A.D. Schmidt                         DATE RECEIVED 6-17-.76 QLCTTEA                       ONOTOAIZGD             PROP                   INPUT FOAM         NUMOGA OF COPIES AGCEIVFD QOAIGINAL
~Concerning Mechanical Pipe Restraints Supplementary Report 81.......(30 Carbon Signed Cys.Received)(4 Page's)PLANT NAME: St.Lucie 8 1 ACKNOWLEDGED,.D>>OT aZMOVz NOTE: IF PERSONNEL EfiPOSURE XS'INVOLVED., SEND DIRECTLY TO KREGER/J.COLLINS SAFETY BRANCH C11IEF: N 3 CYS FOR ACTXON LIC;ASST': K'ee FOR ACTION/INFORMATION ENVIRO M/-CYS Acss16 css.KiBIBHRII ssz ic is.FXL NRC PDR I&E 2 (3 SCHROEDER/XPPOLITO 04 NOVAK C111'CK R MES INTERNAL DISTRIBUTION tier hHMHi TEDI'.SCO/I IACCA Y E.N I'AER SIIAO VOT.Lt I I'.R./II UNC I I KREQQQJ~OLQ~NS LPDR: Ft.Pierce F.TXC NSIC EXTEIINAL DISTRIBUTION CONTROL NUMBER 6135.'
                            .following......,.'0
0 I~" Mtl h'l hh, heal'~~\~4~their hh-)'hhl hW)g'hi"~+Pg, hhh*"h~e~~~~~~"~Itl'~>h I~"3h"'<>f'" O h a I<<g hg hhhh hf Ih hh I h h'll Re 8'ulg)0 P.O, BOX 013100,>MIAMI, FLORIDA"3101 I//cg//g~Co~R Rg0I 77 1$5gpN I0RL t".:.','a.'~>>'>~I l.>///yygx-H FLORIDA POVsER B LiGHT GOl:><<t!Y June 10, 1976 PRN-LI-76-143 Mr.Norman C;Moseley, Director, Region II Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission 230 Peachtree Street, N.N., Suite 818.Atlanta, Georgia ,30303
                              @UNCLASSIFIED EICOPV DESCRIPTION                                                        ENCLOSURE Ltr.. trans      the                                                Licensee Event Report (R.O. 76-9) on.,3-31-76
                                                                        ~
Concerning Mechanical Pipe Restraints Supplementary Report 81     .......
(30 Carbon Signed Cys. Received)
(4 Page's)
ACKNOWLEDGED,                    .
D>>OT aZMOVz PLANT NAME:           St. Lucie   8 1                               NOTE:     IF PERSONNEL EfiPOSURE XS 'INVOLVED.,
SEND DIRECTLY TO KREGER/J. COLLINS SAFETY                                   FOR ACTION/INFORMATION                ENVIRO BRANCH C11IEF:                       K N 3 CYS FOR ACTXON                     'ee LIC;   ASST':
M/ -CYS Acss16       css.     KiBIBHRII ssz ic is INTERNAL DISTRIBUTION
          . FXL NRC PDR I & E 2 (3
SCHROEDER/XPPOLITO 04 NOVAK C111'CK R MES tier hHMHi TEDI'.SCO/I IACCA Y E     .N I
    'AER SIIAO VOT.LtI I'.R./IIUNC I I KREQQQJ~OLQ~NS EXTEIINALDISTRIBUTION                                          CONTROL NUMBER LPDR:   Ft. Pierce       F .
TXC NSIC                                                                                                   6135.'


==Dear Mr.Moseley:==
0
.00CKOEO VS'>P 5oel'>>>>>gob~C4>I>, REPORTABLE OCCURRENCE 335-76-9 ST.LUCIE UNIT 1 DATE OF OCCURRENCE:
                                    ~    " Mtl  h'l  I hh, heal'                        hh
MARCH 31'976 MECHANICAL PIPE RESTRAINTS SUPPLEMENTARY REPORT NO.1 The attached Licensee Event Report is being submitted to supplement our initial report of April 12, 1976.Very truly yours, Vice President Power Resources MAS/cpc At tachment cc: Jack R.Newman, Esquire-Director, Office of.Inspection and Enforcement (40)Director,.-
                                        )
Office of Management Information and Program Control (3) r I h Ui IJ CONTROL BLOCK: 1.UCENSEE'/'AME~01 FLSLZ1 0 0 7 89 14 15 REPOAT, REPORT CATEOORY TYPE SOURCE[001j coN'r~T~L 0 7 8 57 58 59 60 61 EVENT OESCRIPTION Qg P o rational testin LICENSEE EVENT REPORT Sf PRINT ALL Rf QUIRE 0 INFORMATION) 6 UCENSE EVENT UCENSE NUMBER TYPE TYPE 00000-00 41 1 11L000~1I 25 26 30 31 32 OOCKET NUMBER~EVENT OATC AEPORT OATE 5 0-0 3 3 5 0 3 3 1 7 6 0 6 1 0 7 6 68 69 74 75 80 of i in restraints snubbers was bein er-7 8 9 80 Qg'ormed durin the heatu for Post Core Hot Functional testin.At the 7 89[GD4]260'F heatu lateau five INC mechanical snubbers were found to be 80 7 8 9 80 Qo 5 locked u.The immediate action was to replace the defective snubbers 7 8 9 80 toad with o erable snubbers.All of the INC snubbers have since been replace 60 7 8 9 SYSTEM CAUSE COOE COOE[oa~j~zz~z 7 8 9 10 11 12 CAUSE OESCFIIPTION Qg As reviousl PRME COMPOI4ENT SUPPUER COMPONENT MANUFACTURER COMPONENT COOE A N G E R~A'B 2 1 0 43 44 47'N 17 re orted it was determined that oxidation of internal 7 8 9 80 to09 corn onents was the cause of the occurrence.
                                                  'hhl e ~ ~ ~ ~ ~ ~
Subse uent factory labora-7 8 9 80 tor testin and anal sis showed the followin OTHER STATUS N A P>QQ~LE CONSEQUENCES 7 8 9 LOSS OR OAMAGE TO FACILITY TYPE OESCAIPTION EE L~l 7 89 10 PUBLICITY 7 8 9 7 89 FACVPf STATUS 9fi POWER Q~g 0 Loaoo J 7 8 9 10 12 13 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE'AMOUNT OF ACTIVITY t11g~Z Z N/A 7 8 9 10 11 PERSONNEL EXPOSURES 7 8 9 11 12 13 PERSONNEL INJURIES 0ESCRIPTION
                                                                          "~  Itl      '~>h I~"3h      "
~4 0'0 7 8 9 11 12 METHOO OF 06COVERY 44 45 46 44 45 LOCATION OF RELEASE N/A N A N A N A N/A OISCOVEAY OESCRIPTION Preo erational Test Procedure 80 80 80 80 80 80 80 80 AOOITIONAL FACTORS'18 See Pa es 2 and 3 for continuation of Event&Cause Descriptions.
                                                                                                          '< >f'" O their hW)  g 'hi"    ~
7 89 80 7 89 NAMEI M.A.Schop man PHONE 305/552-3779 80 GPO IIAI~6/7 REPORTABLE OCCURRENCE 335-7 6-9 SUPPLEMENTARY LER NO.l PAGE TWO Event Descri tion (Continued)
                                        +Pg,    hhh * "h ~
C by Pacific Scientific snubbers.Cause.Descri tion (Continued)
        ~ ~ \ ~ 4 ~
S/N 000377 The front.and rear caps of the snubber were removed.A thin layer of oxidation was found on the inside of both caps, and there was water inside the rear cap.The ball screw was opera-tional, and clearances between'internal components were normal.However, there was a large amount of rust sludge and water inside the center section which, caused rotational binding.The rotational binding resulted in resistance to thermal move-~ment.Also, the thrust bearing was installed incorrectly at.the factory, but this did not cause the snubber malfunction.
h a
S/N 000343 This snubber was found to have an improper end fitting (i.e., no ball bushing), and its indicator bar was slightly bent.With the correct-end fitting, the snubber was opeiational, therefore, it was not disassembled.
I
S/N 000525 The front and rear caps were removed and the snubber interior was found to be clean..The ball screw was operational, and the clearances between internal components were normal.However,'here was slight, rotational binding in the center section.When the adaptor assembly was rotated one revolution, the.snubber began to operate,.but with a higher.than normal resistance to movement.The adaptor assembly was removed and a small amount of oxidation was found on the thrust bearing.The amount of oxidation was considered large enough to have caused the snubber malfunction.
                                                                                    <<g hg hhhh hf Ih hh      I  h  h 'll
S/N 000695 Same description as for 000525.
 
'i~'REPORTABLE OCCURRENCE 335-76-9 SUPPLEMENTARY LER NO..1 PAGE THREE Cause'escri tion (Continued)
P.O, BOX 013100, >MIAMI, FLORIDA "3101 Re 8'ulg)0 t"
S/N 000632": The'ront and rear caps were'removed.and'he snubber-interior:was found to be clean.'The ball screw.was operational, and the clearances between internal components were normal;However,;there-was rotational binding in the center section.The adaptor assembly was removed and a large amoun't of oxidation was found on~the thrust bearing..The oxidation caused the snubber malfunction.
I
FLORIDA POWER 8, LIGHT COMPANY June 10, 1976 PRN-LI-76-143 Mr.Norman C.Moseley, Director, Region II Office of Inspection and Enforcement U.S.Nuclear Regulatory Commission 230 Peachtree Street, N.W., Suite 818 Atlanta, Georgia 30303
                                              //
H
                                                                      '~>>'          >~I.:.','a.l. ///yygx-FLORIDA POVsER        B LiGHT GOl:> <<t!Y cg//g~                             June 10, 1976 Co~ 1$R Rg0I      77                PRN-LI-76-143 5gpN I0RL Mr. Norman C; Moseley, Director, Region                II                00CKOEO Office of Inspection and Enforcement                                      VS'>P U. S. Nuclear Regulatory Commission 230 Peachtree Street, N. N., Suite 818.                                        5oel'>>>>>
Atlanta, Georgia ,30303                                                  gob~   C4>I>,
 
==Dear Mr. Moseley:==
REPORTABLE OCCURRENCE            335-76-9 ST. LUCIE UNIT 1 DATE OF OCCURRENCE:            MARCH  31'976 MECHANICAL PIPE RESTRAINTS SUPPLEMENTARY REPORT NO. 1 The attached    Licensee Event Report is being submitted to supplement our initial report of April 12, 1976.
Very  truly yours, Vice President Power Resources MAS/cpc At tachment cc:    Jack R. Newman, Esquire
      -Director, Office of. Inspection and Enforcement                  (40)
Director,.- Office of Management Information and Program Control (3)
 
r I h
Ui IJ
 
LICENSEE EVENT REPORT CONTROL BLOCK:                                                                        Sf PRINT ALL RfQUIRE 0    INFORMATION) 1                        6
                      . UCENSEE                                                                                  UCENSE              EVENT
                      '/'AME
  ~01      FLSLZ1                                    0 0        00000 UCENSE NUMBER 00              41 TYPE 1    11L000~1I TYPE
                    ~
7 89                                      14    15                                              25    26                30    31    32 REPOAT,        REPORT CATEOORY          TYPE      SOURCE              OOCKET NUMBER              ~         EVENT OATC                  AEPORT OATE
[001j coN'r                        T          ~L        0    5 0    0          3 3 5          0    3 3 1       7 6        0     6 1      0 7      6 7   8           57      58        59          60      61                                68    69                    74    75                        80 EVENT OESCRIPTION Qg8 7       9 P      o      rational testin                     of    i in      restraints            snubbers        was    bein          er-80 Qg'ormed durin the                                     heatu      for Post Core Hot Functional testin . At the 7    89                                                                                                                                                80
[GD4]      260'F heatu                        lateau        five INC mechanical snubbers were found to be 7   8 9                                                                                                                                               80 Qo  5      locked u . The immediate action was to replace the defective snubbers 7   8 9 toad      with o erable snubbers. All of the INC snubbers have since been replace 80 7   8 9                                                                   PRME                                                                        60 SYSTEM        CAUSE                                            COMPOI4ENT          COMPONENT COOE          COOE                  COMPONENT COOE              SUPPUER            MANUFACTURER
[oa~j 7 8 9 10
          ~zz              ~z                      A N    G    E R          ~A            'B    2 1      0        'N 11         12                           17        43          44              47 CAUSE OESCFIIPTION Qg8 7       9 As          reviousl                re orted          it  was determined that oxidation of internal 80 to09        corn onents was the cause of the occurrence.                                                Subse uent factory labora-7 8 9                                                                                                                                                  80 tor testin and anal sis showed the followin 7    89    FACVPf                                                                METHOO OF 80 STATUS            9fi  POWER                  OTHER STATUS          06COVERY                    OISCOVEAY OESCRIPTION Q~g            0            Loaoo            J              N A                              Preo    erational Test Procedure 7 8          9              10                12 13                          44      45      46                                                      80 FORM OF ACTIVITY        COATENT RELEASEO        OF RELEASE                'AMOUNT OF ACTIVITY                                        LOCATION OF RELEASE t11g          ~Z                Z                      N/A                                                        N/A 7     8      9                10          11                                  44        45                                                            80 PERSONNEL EXPOSURES 7   8 9                 11    12          13                                                                                                          80 PERSONNEL INJURIES 7
  ~4 8 9 0'0            11 0ESCRIPTION 12 N A 80 P>QQ~LE          CONSEQUENCES N A 7    8 9                                                                                                                                                80 LOSS OR OAMAGE TO FACILITY TYPE        OESCAIPTION EE L~l 7 89              10 N A 80 PUBLICITY N/A 7    8 9                                                                                                                                                80 AOOITIONAL FACTORS See Pa es                2
                                        '18 and     3  for continuation of Event                      &  Cause    Descriptions.
7    89                                                                                                                                                80 7    89                                                                                                                                                80 NAMEI    M. A. Schop man                                                          PHONE    305/552-3779 GPO  IIAI~ 6/7
 
REPORTABLE OCCURRENCE    335-7 6-9 SUPPLEMENTARY LER NO.
PAGE TWO l
Event Descri    tion (Continued) by Pacific Scientific snubbers.
C Cause. Descri  tion (Continued)
S/N 000377 The  front. and rear caps of the snubber were removed. A thin layer of oxidation was found on the inside of both caps, and there was water inside the rear cap. The ball screw was opera-tional, and clearances between'internal components were normal. However, there was a large amount of rust sludge and water inside the center section which, caused rotational binding.
The rotational binding resulted in resistance to thermal move-
~
ment.
Also, the thrust bearing was installed incorrectly at .the factory, but this did not cause the snubber malfunction.
S/N 000343 This snubber was found to have an improper end fitting (i.e.,
no  ball bushing), and its indicator bar was slightly bent.
With the correct- end fitting, the snubber was opeiational, therefore,  it  was not disassembled.
S/N 000525 The front and rear caps were removed and the snubber interior was found to be clean. .The ball screw was operational, and the clearances  between internal components were normal.
slight, rotational binding in the center section.
However,'here was When the adaptor assembly was rotated one revolution, the. snubber began to operate,. but with a higher .than normal resistance to movement. The adaptor assembly was removed and a small amount of oxidation was found on the thrust bearing. The amount of oxidation was considered large enough to have caused the snubber malfunction.
S/N 000695 Same  description  as for  000525.
 
i
                              ~'
REPORTABLE OCCURRENCE 335-76-9 SUPPLEMENTARY LER NO.. 1 PAGE THREE Cause'escri tion (Continued)
S/N 000632
  ": The'ront      and  rear caps were'removed.and'he snubber -interior
:was found  to  be clean. 'The ball screw. was operational, and the clearances between internal components were normal; However,
    ;  there -was rotational binding in the center section. The adaptor assembly was removed and a large amoun't of oxidation was found on
  ~
the thrust bearing.. The oxidation caused the snubber malfunction.
 
FLORIDA POWER 8, LIGHT COMPANY June 10, 1976 PRN-LI-76-143 Mr. Norman C. Moseley,    Director, Region  II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N. W., Suite 818 Atlanta, Georgia 30303
 
==Dear Mr. Moseley:==
 
REPORTABLE OCCURRENCE 335-76-9 ST. LUCXE UNIT 1 DATE OF OCCURRENCE:  MARCH 31, 1976 MECHANICAL PIPE RESTRAXNTS SUPPLEMENTARY REPORT NO. 1 The attached  Licensee Event. Report is being submitted to supplement our initial report of April 12, 1976.
Very  truly yours, Vice President Power Resources MAS/cpc Attachment cc:  Jack R. Newman, Esquire Director, Office of Inspection and Enforcement      (40)
Director, Office of Management Xnformation and Program Control (3)
HELPING BUILD FLORIDA
 
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4  1 ~
                          ~ ~
                      ~.
P                  I I
      ~~~f' hl
 
LICENSEE EVENT REPORT CONTROL BLOCK:                                                                  [PLEASE PRINT ALL REQUIRED INFORMATION) 6 UCENSEE                                                                                    UCENSE                EVENT
  ~01FLSLS100 7 89 NAME                                      UCENSE NUMBEA 0 0      0 0      0  0      0        41 TYPE.
1    11          ~01 TYPE
                    ~
14      15                                          25    26                  3Q      31    32 REPORT    REPORT
  ~01 cON'T 7 8 CATEGORY 57        58 TYPE
                                        ~T 59 SOURCE L
60 0
61
                                                                  ~
5
                                                                    ~ OOCKET NUMBER 0  0        3 3 5 68    69 033176EVENT OATS 74 0
75 REPORT OATE 6 1      0 7      6 80 I
EVENT OESCRIPTION erational testin of i in restraints snubbers was bein er-1 Q58          Prep 7        9                                                                                                                                                  80
        . foimed durin the heatu for Post Core Hot Functional testin . At the 7 89                                                                                                                                                          80
  ~04          260'F heatu                        lateau, five INC mechanical snubbers were found to be 7 8 9                                                                                                                                                        80 .
Qo  g      .locked              u  .      The        immediate      action      was    to  replace      the    defective            snubbers 7 8.9                                                                                                                                                        80 Qo  6        with operable snubbers. All of the .INC snubbers have since been replace 7    8 9                                                                      WPAE                                                                          80 SYSTEM          CAUSE                                          COMPONENT            COMPONENT 7
[oa']    ~ZZ 8 9 10 COBE          COOE
                            ~S 11        12 ANGERA COMPONENT COOE 17 SUPPUER 43 B
MANUFACTUAER 2 1      0 47 N
48 CAUSE OESCRIPTION 7    8 9 As        reviousl                re orted          it  was determined that oxidation of internal 80 Qg8          corn onents was the cause of the occurrence.                                                Subse uent. factory labora-7        9                                                                                                                                                    80 Qg          tor testin and anal sis showed the followin 7    89                                                                                                                                                      80 FAC~                                                                  METHOO OF STATUS                % POWER                  OTHER STATUS          OISCOVEAY                    OISCOVEAY OESCAIPTION Em            L~l      .                                        N A                      C        Preo    erational        Test, Procedure 7    8        9                '10              12 13                          44      45      46                                                        80 FORM OF ACTIVITY          CONTENT RELEASEO          OF RELEASE                AMOUNT OF ACTIVITY                                        LOCATION OF RELEASE t11I          ~Z
                              .      Z                    N/A                                                        N/A 7    8        9                    10      11                                    44      45                                                              80 P
PERSONNEL EXPOSURES N A 7    89                  11        12      13                                                                                                            , 80 PERSONNEL INJURIES NUMBER,              OESCRIPTION 7    8'9
          ~00          0 12
                                                  '~4 N A 11                                                                                                                                80 PROBABLE CONSEQUENCES N A 7    89                                                                                                                                                    80 LOSS OR OAMAGE TO FACILITY TYPE        OESCRIPTION Z                                                                        N A
: 7.  '8  9          '10                                                                                                                                      80 PU8LICITY N/A 7    8 9                                                                                                                                                  "80 AOOITIONAL FACTORS
[]is]        See Pa es 2 and 3                          for continuation of Event                      &  Cause    Descriptions.
7    8 9                                                                                                                                                    80 7    89 M. A. Schop              man'HONE,                                            3 05/552        377 9 eFO 80 eeS- eeT
 
v, ~
REPORTABLE OCCURRENCE  335-76-9 SUPPLEMENTARY LER NO. l PAGE TWO Event Descri  tion (Continued) by  Pacific Scientific snubbers.
Cause Descri  tion (Continued)
S/N 000377 The  front and rear caps of the snubber were removed. A thin layer of oxidation was found on the inside of both caps, and there was water inside the rear cap. The ball screw was opera-tional, and clearances between internal components were normal. However, there was a large amount of rust. sludge and water inside the center section which caused rotational binding.
The rotational binding resulted in resistance to thermal move-ment.
Also, the thrust bearing was installed incorrectly at the factory, but this did not cause the snubber malfunction.
S/N 000343 This snubber was found to have an improper end fitting (i.e.,
no  ball bushing), and its indicator bar was slightly bent.
With the correct end fitting, the snubber was operational, therefore,  it  was not disassembled.
S/N 000525 The front and rear caps were removed and the snubber interior was found to be clean. The ball screw was operational, and the clearances between internal components were normal. However, there was slight rotational binding in the center section.
When the adaptor assembly was rotated one revolution, the snubber began to operate, but with a higher than normal resistance to movement. The adaptor assembly was removed and a small amount of oxidation was found on the thrust bearing. The amount of oxidation was considered large enough to have caused the snubber malfunction.
S/N 000695 Same  description  as for  000525.
 
REPORTABLE OCCURRENCE 335-76-9 SUPPLEMENTARY LER NO. 1 PAGE THREE Cause Descri  tion (Continued)
S/N 000632 The front and rear caps were removed and the snubber interior was found to be clean. The ball screw was operational, and the clearances  between internal components were normal. However, there  was rotational binding in the center section. The adaptor assembly was removed and a large amount, of oxidation was found on the thrust bearing. The oxidation caused the snubber malfunction.


==Dear Mr.Moseley:==
REPORTABLE OCCURRENCE 335-76-9 ST.LUCXE UNIT 1 DATE OF OCCURRENCE:
MARCH 31, 1976 MECHANICAL PIPE RESTRAXNTS SUPPLEMENTARY REPORT NO.1 The attached Licensee Event.Report is being submitted to supplement our initial report of April 12, 1976.Very truly yours, Vice President Power Resources MAS/cpc Attachment cc: Jack R.Newman, Esquire Director, Office of Inspection and Enforcement (40)Director, Office of Management Xnformation and Program Control (3)HELPING BUILD FLORIDA 0 r 4 1~~.~~P I I hl~~~f' CONTROL BLOCK: LICENSEE EVENT REPORT[PLEASE PRINT ALL REQUIRED INFORMATION) 6 UCENSEE'NAME~01FLSLS100 7 89 14 15 UCENSE NUMBEA 0 0 0 0 0-0 0 25 UCENSE TYPE.EVENT TYPE 41 1 11~01 26 3Q 31 32 REPORT REPORT CATEGORY TYPE SOURCE~01 cON'T~~T L 0 7 8 57 58 59 60 61 EVENT OESCRIPTION Q5 Prep erational testin~~OOCKET NUMBER 5 0-0 3 3 5 EVENT OATS 033176 REPORT OATE 0 6 1 0 7 6 68 69 74 75 80 1 of i in restraints snubbers was bein er-7 8 9 80 I.foimed durin the heatu for Post Core Hot Functional testin.At the 7 89~04 260'F heatu lateau, five INC mechanical snubbers were found to be 80 7 8 9 80.Qo g.locked u.The immediate action was to replace the defective snubbers 7 8.9 80 Qo 6 with operable snubbers.All of the.INC snubbers have since been replace 7 8 9 SYSTEM CAUSE COBE COOE[oa']~ZZ~S 7 8 9 10 11 12 CAUSE OESCRIPTION As reviousl COMPONENT COOE WPAE COMPONENT SUPPUER COMPONENT MANUFACTUAER ANGERA 17 43 B 2 1 0 N 47 48 re orted it was determined that oxidation of internal 80 7 8 9 80 Qg corn onents was the cause of the occurrence.
Subse uent.factory labora-7 89 FAC~STATUS%POWER Em L~l.7 8 9'10 12 13 FORM OF ACTIVITY CONTENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY t11I~Z.Z N/A 7 8 9 10 11 PERSONNEL EXPOSURES 7 89 11 12 13 PERSONNEL INJURIES NUMBER, OESCRIPTION
'~4~00 0 7 8'9 11 12 OTHER STATUS N A PROBABLE CONSEQUENCES METHOO OF OISCOVEAY OISCOVEAY OESCAIPTION C Preo erational Test, Procedure 44 45 46 LOCATION OF RELEASE N/A 44 45 P N A N A 7 8 9 Qg tor testin and anal sis showed the followin 80 80 80 80 , 80 80 7 89 LOSS OR OAMAGE TO FACILITY TYPE OESCRIPTION Z 7.'8 9'10 PU8LICITY 7 8 9 N A N A N/A 80 80"80 AOOITIONAL FACTORS[]is]See Pa es 2 and 3 for continuation of Event&Cause Descriptions.
7 8 9 80 7 89 M.A.Schop man'HONE, 3 05/552 377 9 80 eFO eeS-eeT v,~
REPORTABLE OCCURRENCE 335-76-9 SUPPLEMENTARY LER NO.l PAGE TWO Event Descri tion (Continued) by Pacific Scientific snubbers.Cause Descri tion (Continued)
S/N 000377 The front and rear caps of the snubber were removed.A thin layer of oxidation was found on the inside of both caps, and there was water inside the rear cap.The ball screw was opera-tional, and clearances between internal components were normal.However, there was a large amount of rust.sludge and water inside the center section which caused rotational binding.The rotational binding resulted in resistance to thermal move-ment.Also, the thrust bearing was installed incorrectly at the factory, but this did not cause the snubber malfunction.
S/N 000343 This snubber was found to have an improper end fitting (i.e., no ball bushing), and its indicator bar was slightly bent.With the correct end fitting, the snubber was operational, therefore, it was not disassembled.
S/N 000525 The front and rear caps were removed and the snubber interior was found to be clean.The ball screw was operational, and the clearances between internal components were normal.However, there was slight rotational binding in the center section.When the adaptor assembly was rotated one revolution, the snubber began to operate, but with a higher than normal resistance to movement.The adaptor assembly was removed and a small amount of oxidation was found on the thrust bearing.The amount of oxidation was considered large enough to have caused the snubber malfunction.
S/N 000695 Same description as for 000525.
REPORTABLE OCCURRENCE 335-76-9 SUPPLEMENTARY LER NO.1 PAGE THREE Cause Descri tion (Continued)
S/N 000632 The front and rear caps were removed and the snubber interior was found to be clean.The ball screw was operational, and the clearances between internal components were normal.However, there was rotational binding in the center section.The adaptor assembly was removed and a large amount, of oxidation was found on the thrust bearing.The oxidation caused the snubber malfunction.
At I}}
At I}}

Latest revision as of 03:26, 3 February 2020

LER 1976-09-00 for St. Lucie Unit 1, Mechanical Pipe Restraints Supplementary Report No. 1
ML18113A439
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 06/10/1976
From: Schmidt A
Florida Power & Light Co
To: Moseley N
NRC/IE, NRC/RGN-II
References
PRN-LI-76-143 LER 1976-09-00
Download: ML18113A439 (14)


Text

NIIC FOflM 195 U.S. NUCLGAA flGOULATOIIVCOMMIS ION DOCKET NUMOEf1 I 2-701 50-336

~t FILE NUMOL'll NBC DISTBIOUTION Fol I ART 50 DOCKET MATERIAL INCIDI',NT REPORT N.C. Mgs'eley FRoM:Flordia Power. 8'ight Co. DATE OF DOCUMENT Miami, Flordia 6-10-76 A.D. Schmidt DATE RECEIVED 6-17-.76 QLCTTEA ONOTOAIZGD PROP INPUT FOAM NUMOGA OF COPIES AGCEIVFD QOAIGINAL

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@UNCLASSIFIED EICOPV DESCRIPTION ENCLOSURE Ltr.. trans the Licensee Event Report (R.O. 76-9) on.,3-31-76

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Concerning Mechanical Pipe Restraints Supplementary Report 81 .......

(30 Carbon Signed Cys. Received)

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ACKNOWLEDGED, .

D>>OT aZMOVz PLANT NAME: St. Lucie 8 1 NOTE: IF PERSONNEL EfiPOSURE XS 'INVOLVED.,

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'~>>' >~I.:.','a.l. ///yygx-FLORIDA POVsER B LiGHT GOl:> <<t!Y cg//g~ June 10, 1976 Co~ 1$R Rg0I 77 PRN-LI-76-143 5gpN I0RL Mr. Norman C; Moseley, Director, Region II 00CKOEO Office of Inspection and Enforcement VS'>P U. S. Nuclear Regulatory Commission 230 Peachtree Street, N. N., Suite 818. 5oel'>>>>>

Atlanta, Georgia ,30303 gob~ C4>I>,

Dear Mr. Moseley:

REPORTABLE OCCURRENCE 335-76-9 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: MARCH 31'976 MECHANICAL PIPE RESTRAINTS SUPPLEMENTARY REPORT NO. 1 The attached Licensee Event Report is being submitted to supplement our initial report of April 12, 1976.

Very truly yours, Vice President Power Resources MAS/cpc At tachment cc: Jack R. Newman, Esquire

-Director, Office of. Inspection and Enforcement (40)

Director,.- Office of Management Information and Program Control (3)

r I h

Ui IJ

LICENSEE EVENT REPORT CONTROL BLOCK: Sf PRINT ALL RfQUIRE 0 INFORMATION) 1 6

. UCENSEE UCENSE EVENT

'/'AME

~01 FLSLZ1 0 0 00000 UCENSE NUMBER 00 41 TYPE 1 11L000~1I TYPE

~

7 89 14 15 25 26 30 31 32 REPOAT, REPORT CATEOORY TYPE SOURCE OOCKET NUMBER ~ EVENT OATC AEPORT OATE

[001j coN'r T ~L 0 5 0 0 3 3 5 0 3 3 1 7 6 0 6 1 0 7 6 7 8 57 58 59 60 61 68 69 74 75 80 EVENT OESCRIPTION Qg8 7 9 P o rational testin of i in restraints snubbers was bein er-80 Qg'ormed durin the heatu for Post Core Hot Functional testin . At the 7 89 80

[GD4] 260'F heatu lateau five INC mechanical snubbers were found to be 7 8 9 80 Qo 5 locked u . The immediate action was to replace the defective snubbers 7 8 9 toad with o erable snubbers. All of the INC snubbers have since been replace 80 7 8 9 PRME 60 SYSTEM CAUSE COMPOI4ENT COMPONENT COOE COOE COMPONENT COOE SUPPUER MANUFACTURER

[oa~j 7 8 9 10

~zz ~z A N G E R ~A 'B 2 1 0 'N 11 12 17 43 44 47 CAUSE OESCFIIPTION Qg8 7 9 As reviousl re orted it was determined that oxidation of internal 80 to09 corn onents was the cause of the occurrence. Subse uent factory labora-7 8 9 80 tor testin and anal sis showed the followin 7 89 FACVPf METHOO OF 80 STATUS 9fi POWER OTHER STATUS 06COVERY OISCOVEAY OESCRIPTION Q~g 0 Loaoo J N A Preo erational Test Procedure 7 8 9 10 12 13 44 45 46 80 FORM OF ACTIVITY COATENT RELEASEO OF RELEASE 'AMOUNT OF ACTIVITY LOCATION OF RELEASE t11g ~Z Z N/A N/A 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES 7 8 9 11 12 13 80 PERSONNEL INJURIES 7

~4 8 9 0'0 11 0ESCRIPTION 12 N A 80 P>QQ~LE CONSEQUENCES N A 7 8 9 80 LOSS OR OAMAGE TO FACILITY TYPE OESCAIPTION EE L~l 7 89 10 N A 80 PUBLICITY N/A 7 8 9 80 AOOITIONAL FACTORS See Pa es 2

'18 and 3 for continuation of Event & Cause Descriptions.

7 89 80 7 89 80 NAMEI M. A. Schop man PHONE 305/552-3779 GPO IIAI~ 6/7

REPORTABLE OCCURRENCE 335-7 6-9 SUPPLEMENTARY LER NO.

PAGE TWO l

Event Descri tion (Continued) by Pacific Scientific snubbers.

C Cause. Descri tion (Continued)

S/N 000377 The front. and rear caps of the snubber were removed. A thin layer of oxidation was found on the inside of both caps, and there was water inside the rear cap. The ball screw was opera-tional, and clearances between'internal components were normal. However, there was a large amount of rust sludge and water inside the center section which, caused rotational binding.

The rotational binding resulted in resistance to thermal move-

~

ment.

Also, the thrust bearing was installed incorrectly at .the factory, but this did not cause the snubber malfunction.

S/N 000343 This snubber was found to have an improper end fitting (i.e.,

no ball bushing), and its indicator bar was slightly bent.

With the correct- end fitting, the snubber was opeiational, therefore, it was not disassembled.

S/N 000525 The front and rear caps were removed and the snubber interior was found to be clean. .The ball screw was operational, and the clearances between internal components were normal.

slight, rotational binding in the center section.

However,'here was When the adaptor assembly was rotated one revolution, the. snubber began to operate,. but with a higher .than normal resistance to movement. The adaptor assembly was removed and a small amount of oxidation was found on the thrust bearing. The amount of oxidation was considered large enough to have caused the snubber malfunction.

S/N 000695 Same description as for 000525.

i

~'

REPORTABLE OCCURRENCE 335-76-9 SUPPLEMENTARY LER NO.. 1 PAGE THREE Cause'escri tion (Continued)

S/N 000632

": The'ront and rear caps were'removed.and'he snubber -interior

was found to be clean. 'The ball screw. was operational, and the clearances between internal components were normal; However,
there -was rotational binding in the center section. The adaptor assembly was removed and a large amoun't of oxidation was found on

~

the thrust bearing.. The oxidation caused the snubber malfunction.

FLORIDA POWER 8, LIGHT COMPANY June 10, 1976 PRN-LI-76-143 Mr. Norman C. Moseley, Director, Region II Office of Inspection and Enforcement U. S. Nuclear Regulatory Commission 230 Peachtree Street, N. W., Suite 818 Atlanta, Georgia 30303

Dear Mr. Moseley:

REPORTABLE OCCURRENCE 335-76-9 ST. LUCXE UNIT 1 DATE OF OCCURRENCE: MARCH 31, 1976 MECHANICAL PIPE RESTRAXNTS SUPPLEMENTARY REPORT NO. 1 The attached Licensee Event. Report is being submitted to supplement our initial report of April 12, 1976.

Very truly yours, Vice President Power Resources MAS/cpc Attachment cc: Jack R. Newman, Esquire Director, Office of Inspection and Enforcement (40)

Director, Office of Management Xnformation and Program Control (3)

HELPING BUILD FLORIDA

r 0

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P I I

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LICENSEE EVENT REPORT CONTROL BLOCK: [PLEASE PRINT ALL REQUIRED INFORMATION) 6 UCENSEE UCENSE EVENT

~01FLSLS100 7 89 NAME UCENSE NUMBEA 0 0 0 0 0 0 0 41 TYPE.

1 11 ~01 TYPE

~

14 15 25 26 3Q 31 32 REPORT REPORT

~01 cON'T 7 8 CATEGORY 57 58 TYPE

~T 59 SOURCE L

60 0

61

~

5

~ OOCKET NUMBER 0 0 3 3 5 68 69 033176EVENT OATS 74 0

75 REPORT OATE 6 1 0 7 6 80 I

EVENT OESCRIPTION erational testin of i in restraints snubbers was bein er-1 Q58 Prep 7 9 80

. foimed durin the heatu for Post Core Hot Functional testin . At the 7 89 80

~04 260'F heatu lateau, five INC mechanical snubbers were found to be 7 8 9 80 .

Qo g .locked u . The immediate action was to replace the defective snubbers 7 8.9 80 Qo 6 with operable snubbers. All of the .INC snubbers have since been replace 7 8 9 WPAE 80 SYSTEM CAUSE COMPONENT COMPONENT 7

[oa'] ~ZZ 8 9 10 COBE COOE

~S 11 12 ANGERA COMPONENT COOE 17 SUPPUER 43 B

MANUFACTUAER 2 1 0 47 N

48 CAUSE OESCRIPTION 7 8 9 As reviousl re orted it was determined that oxidation of internal 80 Qg8 corn onents was the cause of the occurrence. Subse uent. factory labora-7 9 80 Qg tor testin and anal sis showed the followin 7 89 80 FAC~ METHOO OF STATUS  % POWER OTHER STATUS OISCOVEAY OISCOVEAY OESCAIPTION Em L~l . N A C Preo erational Test, Procedure 7 8 9 '10 12 13 44 45 46 80 FORM OF ACTIVITY CONTENT RELEASEO OF RELEASE AMOUNT OF ACTIVITY LOCATION OF RELEASE t11I ~Z

. Z N/A N/A 7 8 9 10 11 44 45 80 P

PERSONNEL EXPOSURES N A 7 89 11 12 13 , 80 PERSONNEL INJURIES NUMBER, OESCRIPTION 7 8'9

~00 0 12

'~4 N A 11 80 PROBABLE CONSEQUENCES N A 7 89 80 LOSS OR OAMAGE TO FACILITY TYPE OESCRIPTION Z N A

7. '8 9 '10 80 PU8LICITY N/A 7 8 9 "80 AOOITIONAL FACTORS

[]is] See Pa es 2 and 3 for continuation of Event & Cause Descriptions.

7 8 9 80 7 89 M. A. Schop man'HONE, 3 05/552 377 9 eFO 80 eeS- eeT

v, ~

REPORTABLE OCCURRENCE 335-76-9 SUPPLEMENTARY LER NO. l PAGE TWO Event Descri tion (Continued) by Pacific Scientific snubbers.

Cause Descri tion (Continued)

S/N 000377 The front and rear caps of the snubber were removed. A thin layer of oxidation was found on the inside of both caps, and there was water inside the rear cap. The ball screw was opera-tional, and clearances between internal components were normal. However, there was a large amount of rust. sludge and water inside the center section which caused rotational binding.

The rotational binding resulted in resistance to thermal move-ment.

Also, the thrust bearing was installed incorrectly at the factory, but this did not cause the snubber malfunction.

S/N 000343 This snubber was found to have an improper end fitting (i.e.,

no ball bushing), and its indicator bar was slightly bent.

With the correct end fitting, the snubber was operational, therefore, it was not disassembled.

S/N 000525 The front and rear caps were removed and the snubber interior was found to be clean. The ball screw was operational, and the clearances between internal components were normal. However, there was slight rotational binding in the center section.

When the adaptor assembly was rotated one revolution, the snubber began to operate, but with a higher than normal resistance to movement. The adaptor assembly was removed and a small amount of oxidation was found on the thrust bearing. The amount of oxidation was considered large enough to have caused the snubber malfunction.

S/N 000695 Same description as for 000525.

REPORTABLE OCCURRENCE 335-76-9 SUPPLEMENTARY LER NO. 1 PAGE THREE Cause Descri tion (Continued)

S/N 000632 The front and rear caps were removed and the snubber interior was found to be clean. The ball screw was operational, and the clearances between internal components were normal. However, there was rotational binding in the center section. The adaptor assembly was removed and a large amount, of oxidation was found on the thrust bearing. The oxidation caused the snubber malfunction.

At I