ML19210D652: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(Created page by program invented by StriderTol)
 
(One intermediate revision by the same user not shown)
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:NRC FORM 366. .. , , (7 77)LICENSEE EVENT REPORT CONTROL BLOCK: l lllll(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
{{#Wiki_filter:. , ,
.1 6l0 HlDlBlSl1l@l0l@l-l0 0lNlPlFl-l0l3l@l4 1l1l1l1 @l 7 LA1 l@
NRC FORM 366 (7 77)
l0 1 5$3 7 8 9 LICENSEE CODE 14 15 LICENSE NLVtlEH 25 26 LICENSE TYPE JJ I0l1l 3[nc Ll@ dl5l0l- 0l314l6 @l1 0l2l2l7l9l@l1 l1 l2 l0 l7 l9 l@
LICENSEE EVENT REPORT
CON'T" "'7 8 60 61 DOCKET NUMBEH 68 69 EVENT D ATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h
              .          CONTROL BLOCK: l               l          l    l  l      l                (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1                              6 l
[_On October 22, 1979 at 0906 hours durine the perf ormance of ST 5071.01. "Anvilt,rv i o 2l Feedwatar System Monthlv Test". it was obset;t - that there was no oil level visible in) o 3lthe oil sight glass on the inboard bearinn of the Auxiliary Feed Pumn Turbine 1-1.
7 0        1 8 9 l0    HlDlBlSl1l@l0l@l-l0 LICENSEE CODE            14    15 0lNlPlFl-l0l3l@l4 LICENSE NLVtlEH                  25    1l1l1l1 26      LICENSE@l TYPE JJ  7 LA1 5        l@
I_o 4 o s This placed the unit in the Action Statement of Technical Soecifica tion 3.7.1.2.
                                                                                                                                                                            $3 CON'T I0l1l 7             8 3[nc         60 Ll@ dl5l0l- 0l314l6 @l1 0l2l2l7l9l@l1 l1 l2 l0 l7 l9 l@
I l o l6 ] l There was no danner to the health and safety of the oublic or station cercon*1.
61             DOCKET NUMBEH             68   69       EVENT D ATE           74       75     REPORT DATE         80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h i
""n n._]1017lsecond train. Auxiliary Feed Pumo 1-2. was ooerable.(NP-33-79-119) l I o a f 80 COMP.VA LV E SYSTEM CAUSE CAUSE CODE CODE SUBCODE COMPONENT CODE SU8 CODE SUSCODEl Cl11l@ lE j@ lB l@ l Pl U] Ml Pl X] Xl@ W@ W @
o      2    [_On October 22, 1979 at 0906 hours durine the perf ormance of ST 5071.01. "Anvilt,rv o       3      l Feedwatar System Monthlv Test". it was obset;t - that there was no oil level visible in)
l0l91 7 8 9 10 11 12 13 18 19 20 SEQUE NTI AL OCCURRENCE REPORT REVi?ON ,_ EVENT YE AR REPORT NO.
I o     4      lthe oil sight glass on the inboard bearinn of the Auxiliary Feed Pumn Turbine 1-1.
'CODE TYPE NO.l7 9ll_ll1 l0 2 ll/ll0l3]lL]l-lJ LE R RO h gU AEP RT_21 22 23 24 26 27 28 23 30 31 J2 K f ACT Of ON PL PT HOURS 22 S 8 IT O FO 1 B.S PP IE MA FA T RERlBlgl34z g lJ5Z lgl30Zl@l0 l0 l0 lV l lYlglNj@l Al@l Tl 1l4 l7 l@
I o       s       This placed the unit in the Action Statement of Technical Soecifica tion 3.7.1.2.
31 40 41 42 43 44 47 33 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS
                                                                                                                                                                                  ""n n._]
]The loss of oil was due to a loose sieht glass. The glass had apparent 1v vibrated i o.11 11)loose at its fitting. Under Maintenance Uork Order 79-3321 the sight class was 1l tightened and the oil replaced.
l o l6 ] l There was no danner to the health and safety of the oublic or station cercon*1.
Surveillance Test ST 071.01 was completed at 2004 1-1 7 J l i l 3 l l hours on October 22, 1979, and Auxiliary Feed Pump 1-1 was declared operable.
(NP-33-79-119)                                              l 1017l                second train. Auxiliary Feed Pumo 1-2. was ooerable.
lll i l 41 1 80'8 9 STA S% POWER OTHER STATUS ISCO iY DISCOVERY DESCRIPTION NAllB l@l Operator observation l~ l1l5l W @ l Ol 8l 8l hl ACTIVITY CONTENT LOCATION OF RELEASE RELE ASEO OF RELE ASE AMOUNT OF ACTIVITY lNAll NA.' l 1 16I W @[Zj@l 80 44 45 7 8 9 10._11 PERSONNEL EXPOSURES TYPE @[ DESCRIPTION lNUMBERl0]O Ol@l]NA[i 7''''',eRSONNE L iN;uLS
I o     a f                                                                                                                                                                 80 CAUSE                                                    COMP.           VA LV E SYSTEM           CAUSE                                                                                 SUSCODE SUBCODE               COMPONENT CODE                   SU8 CODE CODE            CODE l0l91                                  l Cl11l@ lE j@ lB l@ l Pl U] Ml Pl X] Xl@ W@ W @ 13                          18          19              20 8                       9         10         11           12                                                                                   REVi?ON 7                                                                                                                                REPORT SEQUE NTI AL                     OCCURRENCE CODE                TYPE                        NO.
'" 'oESCRiPTiONh lNuvsER~ Ii ls i 1010101@l NA 7 8 9 11 12 LOSS OF OR D AY AGE TO F ACILITY T gi E'~1wA X2 1"" i-i , e 60 iSSuI"@""'o'ESCR'PTiONO 7911270 g [
                                            ,_ EVENT YE AR                         REPORT NO.
l7 8 9 10 NR use ONLY
h gU LE R RO AEP RT        l7 9l              l_l          l1 l0 2 l 26 l/l 27 l0l3]
'*lllllllll l;lNf lNA 2 o 68 09 SJ ;7 H 3 10 W-M4M, M.M{DVR 79-155 Kevin Melstad pgoyg NAME OF PnEPAnEn
28      23 lL]
&e TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER ST.uION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-119 DATE OF EVENT: October 22, 1979
30 l-l 31 J
_FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Auxiliary Feed Pump 1-1 inoperable Conditions Prior to Occurrence:
J2
The unit was in Mode 1, with Power (MWT) = 2400, and Load (Gross FME) = 790.
_21        22         23         24 FO 1      B.      S PP IE            MA    FA T RER K f     ACT Of         ON PL PT                                 HOURS 22       S 8 IT O lBlgl34z g                     lJ5Z lg                        l0 l0 l0 lV 40l          lYlg            lNj@ l Al@ l Tl 1l4 l7 l@
._Description of Occurrence: At 0906 heres on October 22, 1979 while performing Surveil-lance Test ST 5071.01, " Auxiliary Feedwater System Monthly Test", it was found that the number one Auxiliary Feed Pump Turbine inbaard bearing had no visible oil level in the oil sight glass.
33                                            l30Zl@ 31                               41               42               43             44                 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i      o    ]The loss of oil was due to a loose sieht glass. The glass had apparent 1v vibrated 11 11) loose at its fitting. Under Maintenance Uork Order 79-3321 the sight class was                                                                                 1 l tightened and the oil replaced.                               Surveillance Test ST 071.01 was completed at 2004                                                 1 1 7 l
J l i l 3 l l hours on October 22, 1979, and Auxiliary Feed Pump 1-1 was declared operable.
l l i l 41 1                                                                                                                                                                   80
          '           8 9 ISCO iY                              DISCOVERY DESCRIPTION STA S               % POWER                     OTHER STATUS
    ~ l1l5l W @ l Ol 8l 8l hl                                           NA                      l  lB l@l Operator observation                                                            l ACTIVITY CONTENT                                                                                               LOCATION OF RELEASE RELE ASEO OF RELE ASE                     AMOUNT OF ACTIVITY
.' l 1 16I W @[Zj@l                                         NA                                  l          l NA                                                                        80 l
44           45 7         8 9               10._        11 PERSONNEL EXPOSURES NUMBER l
[             i 7          l0]O Ol@lTYPE                ]         @[  NA DESCRIPTION                                                                                                    '
                              ,eRSONNE L iN;uLS NuvsER              oESCRiPTiONh                                                                                                                              l NA
  ~ Ii ls i8 1010101@l 7             9                 11     12 LOSS OF OR D AY AGE TO F ACILITY
              , e          iT gi E'~
i 1wA           X2               60 1
7          8 9            10
                                          '*                                                                  7911270 g [                                        NR use ONLY lll l; 2 o          lNf l NA iSSuI"@""'o'ESCR'PTiONO 10 l
68 09 l    lll      ll SJ ;
7         H 3                                                                                                                       W-M4M, M.                         M DVR 79-155                         NAME OF PnEPAnEn Kevin Melstad                                           pgoyg                                                     {
 
  &                                                                                         e TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER ST.uION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-119 DATE OF EVENT: October 22, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Auxiliary Feed Pump 1-1 inoperable Conditions Prior to Occurrence:     The unit was in Mode 1, with Power (MWT) = 2400, and Load (Gross FME) = 790.
Description of Occurrence: At 0906 heres on October 22, 1979 while performing Surveil-lance Test ST 5071.01, " Auxiliary Feedwater System Monthly Test", it was found that the number one Auxiliary Feed Pump Turbine inbaard bearing had no visible oil level in the oil sight glass.
This placed the unit in the Action Statement of Technical Specification 3.7.1.2 which requires that with one pump inoperable, the isoperable pump be repaired within 72 hours or be in hot shutdown within the next 12 hours The Technical Specification requires operability of both Auxiliary Feed Pumps while 'n Modes 1, 2, and 3.
This placed the unit in the Action Statement of Technical Specification 3.7.1.2 which requires that with one pump inoperable, the isoperable pump be repaired within 72 hours or be in hot shutdown within the next 12 hours The Technical Specification requires operability of both Auxiliary Feed Pumps while 'n Modes 1, 2, and 3.
Designation of Apparent Cause of Occurrence: The casse of the occurrence was due to the oil level sight glass becoming loose due to vibracion of the Auxiliary Feed Pump Turbine. Oil drained from the loose fitting.
Designation of Apparent Cause of Occurrence: The casse of the occurrence was due to the oil level sight glass becoming loose due to vibracion of the Auxiliary Feed Pump Turbine. Oil drained from the loose fitting.
Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel.
Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. Auxiliary Feed Pump 1-2 was operable during this time.
Auxiliary Feed Pump 1-2 was operable during this time.
Corrective Action: Under Maintenance Work Order 79-3321, the bearing sight glass was tightened. The sight glass was found to be loose and not seating properly. The oil icvel has remained constant since tightening. Oil sight glasses will be installed using a sealing compound. Surveillance Test ST 5071.01 was completed at 2004 hours on October 22, 1979, and Auxiliary Feed Pump 1-1 was declared operable. The unit was removed from the Action Statement.
Corrective Action: Under Maintenance Work Order 79-3321, the bearing sight glass was tightened. The sight glass was found to be loose and not seating properly. The oil icvel has remained constant since tightening. Oil sight glasses will be installed using a sealing compound. Surveillance Test ST 5071.01 was completed at 2004 hours on October 22, 1979, and Auxiliary Feed Pump 1-1 was declared operable. The unit was removed from the Action Statement.
Failure Data: A similar occurrence with containment spray pump oil sight glass was reported in Licensee Event Report NP-33-79-83.
Failure Data: A similar occurrence with containment spray pump oil sight glass was reported in Licensee Event Report NP-33-79-83.
LER #79-102
LER #79-102 i798 ?93}}
.i798?93}}

Latest revision as of 05:15, 2 February 2020

LER 79-102/03L-0:on 791022,during Feedwater Sys Monthly Surveillance Test,No Oil Level Visible in Oil Sight Glass on Inboard Bearing of Auxiliary Feedpump Turbine 1-1.Caused by Loose Sight Glass.Glass Tightened & Oil Replaced
ML19210D652
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 11/20/1979
From: Melstad K
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19210D639 List:
References
LER-79-102-03L, LER-79-102-3L, NUDOCS 7911270428
Download: ML19210D652 (2)


Text

. , ,

NRC FORM 366 (7 77)

LICENSEE EVENT REPORT

. CONTROL BLOCK: l l l l l l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 l

7 0 1 8 9 l0 HlDlBlSl1l@l0l@l-l0 LICENSEE CODE 14 15 0lNlPlFl-l0l3l@l4 LICENSE NLVtlEH 25 1l1l1l1 26 LICENSE@l TYPE JJ 7 LA1 5 l@

$3 CON'T I0l1l 7 8 3[nc 60 Ll@ dl5l0l- 0l314l6 @l1 0l2l2l7l9l@l1 l1 l2 l0 l7 l9 l@

61 DOCKET NUMBEH 68 69 EVENT D ATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h i

o 2 [_On October 22, 1979 at 0906 hours0.0105 days <br />0.252 hours <br />0.0015 weeks <br />3.44733e-4 months <br /> durine the perf ormance of ST 5071.01. "Anvilt,rv o 3 l Feedwatar System Monthlv Test". it was obset;t - that there was no oil level visible in)

I o 4 lthe oil sight glass on the inboard bearinn of the Auxiliary Feed Pumn Turbine 1-1.

I o s This placed the unit in the Action Statement of Technical Soecifica tion 3.7.1.2.

""n n._]

l o l6 ] l There was no danner to the health and safety of the oublic or station cercon*1.

(NP-33-79-119) l 1017l second train. Auxiliary Feed Pumo 1-2. was ooerable.

I o a f 80 CAUSE COMP. VA LV E SYSTEM CAUSE SUSCODE SUBCODE COMPONENT CODE SU8 CODE CODE CODE l0l91 l Cl11l@ lE j@ lB l@ l Pl U] Ml Pl X] Xl@ W@ W @ 13 18 19 20 8 9 10 11 12 REVi?ON 7 REPORT SEQUE NTI AL OCCURRENCE CODE TYPE NO.

,_ EVENT YE AR REPORT NO.

h gU LE R RO AEP RT l7 9l l_l l1 l0 2 l 26 l/l 27 l0l3]

28 23 lL]

30 l-l 31 J

J2

_21 22 23 24 FO 1 B. S PP IE MA FA T RER K f ACT Of ON PL PT HOURS 22 S 8 IT O lBlgl34z g lJ5Z lg l0 l0 l0 lV 40l lYlg lNj@ l Al@ l Tl 1l4 l7 l@

33 l30Zl@ 31 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i o ]The loss of oil was due to a loose sieht glass. The glass had apparent 1v vibrated 11 11) loose at its fitting. Under Maintenance Uork Order 79-3321 the sight class was 1 l tightened and the oil replaced. Surveillance Test ST 071.01 was completed at 2004 1 1 7 l

J l i l 3 l l hours on October 22, 1979, and Auxiliary Feed Pump 1-1 was declared operable.

l l i l 41 1 80

' 8 9 ISCO iY DISCOVERY DESCRIPTION STA S  % POWER OTHER STATUS

~ l1l5l W @ l Ol 8l 8l hl NA l lB l@l Operator observation l ACTIVITY CONTENT LOCATION OF RELEASE RELE ASEO OF RELE ASE AMOUNT OF ACTIVITY

.' l 1 16I W @[Zj@l NA l l NA 80 l

44 45 7 8 9 10._ 11 PERSONNEL EXPOSURES NUMBER l

[ i 7 l0]O Ol@lTYPE ] @[ NA DESCRIPTION '

,eRSONNE L iN;uLS NuvsER oESCRiPTiONh l NA

~ Ii ls i8 1010101@l 7 9 11 12 LOSS OF OR D AY AGE TO F ACILITY

, e iT gi E'~

i 1wA X2 60 1

7 8 9 10

'* 7911270 g [ NR use ONLY lll l; 2 o lNf l NA iSSuI"@""'o'ESCR'PTiONO 10 l

68 09 l lll ll SJ ;

7 H 3 W-M4M, M. M DVR 79-155 NAME OF PnEPAnEn Kevin Melstad pgoyg {

& e TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER ST.uION UNIT ONE SUPPLEMENTAL INFORMATION FOR LER NP-33-79-119 DATE OF EVENT: October 22, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Auxiliary Feed Pump 1-1 inoperable Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 2400, and Load (Gross FME) = 790.

Description of Occurrence: At 0906 heres on October 22, 1979 while performing Surveil-lance Test ST 5071.01, " Auxiliary Feedwater System Monthly Test", it was found that the number one Auxiliary Feed Pump Turbine inbaard bearing had no visible oil level in the oil sight glass.

This placed the unit in the Action Statement of Technical Specification 3.7.1.2 which requires that with one pump inoperable, the isoperable pump be repaired within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in hot shutdown within the next 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> The Technical Specification requires operability of both Auxiliary Feed Pumps while 'n Modes 1, 2, and 3.

Designation of Apparent Cause of Occurrence: The casse of the occurrence was due to the oil level sight glass becoming loose due to vibracion of the Auxiliary Feed Pump Turbine. Oil drained from the loose fitting.

Analysis of Occurrence: There was no danger to the health and safety of the public or to station personnel. Auxiliary Feed Pump 1-2 was operable during this time.

Corrective Action: Under Maintenance Work Order 79-3321, the bearing sight glass was tightened. The sight glass was found to be loose and not seating properly. The oil icvel has remained constant since tightening. Oil sight glasses will be installed using a sealing compound. Surveillance Test ST 5071.01 was completed at 2004 hours0.0232 days <br />0.557 hours <br />0.00331 weeks <br />7.62522e-4 months <br /> on October 22, 1979, and Auxiliary Feed Pump 1-1 was declared operable. The unit was removed from the Action Statement.

Failure Data: A similar occurrence with containment spray pump oil sight glass was reported in Licensee Event Report NP-33-79-83.

LER #79-102 i798 ?93