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NRC FORM 366 (7 77)
NRC FORM 366 (7 77)
     ^
     ^
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[33Z jgl34X]@ ,lBl@
[33Z jgl34X]@ ,lBl@
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35                36            31                      40    di              42                  43                44                47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l
35                36            31                      40    di              42                  43                44                47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l
l i l o l l Main Steam Line Code Safety Valve SPl7A2 was found to have a loose spindle and was I
l i l o l l Main Steam Line Code Safety Valve SPl7A2 was found to have a loose spindle and was I
Q l gagged. Valve SPl7B2 was tested, f ound satisfactory, and declared operable on l
Q l gagged. Valve SPl7B2 was tested, f ound satisfactory, and declared operable on l
li;7; l February 13, 1979.
li;7; l February 13, 1979.
                                                                                                                                                            -
I i a I l
I i a I l
t i l41 l                                                                                                                                                                                80 7        8 9 OTHER STATUS              DISCO RY                                DISCOVERY DESCRIPTION A S                  % POWE R l
t i l41 l                                                                                                                                                                                80 7        8 9 OTHER STATUS              DISCO RY                                DISCOVERY DESCRIPTION A S                  % POWE R l
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: 9 6 9 Q @l          10
: 9 6 9 Q @l          10
                                   '                                                                                                                                  NRC USE ONLY                ,
                                   '                                                                                                                                  NRC USE ONLY                ,
isS 121 o 1 LNU[                      NA 8l DESCRIPTION 79030501 % @                                                                    l 68 69 i 111111 IiiiIl            60. E
isS 121 o 1 LNU[                      NA 8l DESCRIPTION 79030501 % @                                                                    l 68 69 i 111111 IiiiIl            60. E DVR 79-027                    NAME OF PREPARER PHONE:
                                                                                                                                                                                        *
* DVR 79-027                    NAME OF PREPARER
* PHONE:


.
  .
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLDfENTAL INFORMATION FOR LER NP-33-79-23 DATE OF EVENT:      January 30, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Main Steam Safety Valves SPl7A2 and SPl7B2 declared inoperable.
TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLDfENTAL INFORMATION FOR LER NP-33-79-23 DATE OF EVENT:      January 30, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Main Steam Safety Valves SPl7A2 and SPl7B2 declared inoperable.
Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 2550, and Load (Gross MWE) = 825.
Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 2550, and Load (Gross MWE) = 825.
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LER #79-018
LER #79-018


  '
e TOLEDO EDISON C0:IPANY                                                                (
,
e
                                                                                          ,
TOLEDO EDISON C0:IPANY                                                                (
DAVIS-LESSE NUCLEAR POWER STATION UNIT ONE                                  PAGE 2 SUPPLEMENTAL INFORMATION FOR LER NP-33-79-23 Failure Data:
DAVIS-LESSE NUCLEAR POWER STATION UNIT ONE                                  PAGE 2 SUPPLEMENTAL INFORMATION FOR LER NP-33-79-23 Failure Data:
Prior occurrences of main steam line code safety valves drif ting from their normal setpoints were previously reported in Licensee Event Reports NP-33-77-117 and NP-33-78-145.
Prior occurrences of main steam line code safety valves drif ting from their normal setpoints were previously reported in Licensee Event Reports NP-33-77-117 and NP-33-78-145.
LER #79-018
LER #79-018
                                                                                            ,
* e}}
* e}}

Latest revision as of 17:35, 1 February 2020

LER 79-018/03L-0:on 790130,valves SP17A2 & SP17B2 Lifted Below Setpoint Range & Declared Inoperable.Caused by Loose Spindle on Main Steam Line Code Safety Valve SP17A2.Valve SP17A2 Gagged & SP17B2 Tested Satisfactorily
ML19282A607
Person / Time
Site: Davis Besse Cleveland Electric icon.png
Issue date: 02/26/1979
From: Brown R
TOLEDO EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML19282A606 List:
References
LER-79-018-03L, LER-79-18-3L, NP-33-79-23, NUDOCS 7903050176
Download: ML19282A607 (3)


Text

. .

NRC FORM 366 (7 77)

^

LICENSEE EVENT REPORT COf4T ROL BLOCK: l 1

l l l l l 6

lh (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) l 0 l8 19 ] l 0l 11l D l B l S] 1l@l 0 l 0 l -l 0 ] 0 l N ] P l h F l 26 - l 0 l LICENSE 3 TY @lPE JO 4 l 1 57 l l

CAI 1 l@

bdl 1 l 1 l@l F LICENSEE CODE I4 15 LICENSE NuY8EH CON'T o i 3Q"c

" 7 l Lj@ 0l 5 l 0l -l 0] 3 l 4 l 6 68l@l630 ] llEVENT 3 lDATE 0l 719 @l 75012 REPORT 14 l 2 l D6l AT E 7 l 9Sol@

i 8 60 61 COCKET NU'.9E R EVENT DESCRIPTION AND PROBABLE CONSEQUENCES bio g lo121l On 1/29/79 load swings resulted in tee lifting of Main Steam Line Code Safety Valves SPl7A2 and SPl7B2. On 1/30/79, it was detemined that valves SPl7A2 and SPl7B2 lif tedj gg,3, g below their setpoint range and were declared inoperable. This placed the unit in the g

,g,,, g Action Statement of Tech Spec 3.7.1.1. Unit power was reduced to less than 90% power.

gg,,, g There was no

,o,3, g The high flux setpoints were reduced to 92.6% of rated thermal power. g g 7 g danger to the health and safety of the public or unit personnel. The remaining eightj code safety valves per main steam line are operable. (NP-33-79-23) l

,g,g, g 60 SUBC DE COMPONENT CODE SLBC DE SU DE DE CODE O 9 lC l Cl@ l El@ l B j@ lV l A lL lV lE lX h lP l@ 20 Bl@

f3 18 19 7 8 9 10 11 12 REVISION SEQUENTI AL OCCURRENCE REPORT CODE TYPE N O.

EVENT YE AR REPORT NO.

LE P 'RO O gRT l7 l9 21l 8 l0l1l8l ]/l l 01 3 lL l l-l l0 l 27 28 29 30 31 32 2J 24 26

_ 21 HOURS S8 ITT D FO EUB. SL PP LI E MAN FA TUF ER lN l@ lD l2 l4 3lg AKE A T ON O PL NT tETH Z

@ l l l l l lY l@ l y l@

[33Z jgl34X]@ ,lBl@

35 36 31 40 di 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l

l i l o l l Main Steam Line Code Safety Valve SPl7A2 was found to have a loose spindle and was I

Q l gagged. Valve SPl7B2 was tested, f ound satisfactory, and declared operable on l

li;7; l February 13, 1979.

I i a I l

t i l41 l 80 7 8 9 OTHER STATUS DISCO RY DISCOVERY DESCRIPTION A S  % POWE R l

l115 l [_EJ@ l 0 l 9 l 2 l@l NA l l C l@l Review of monitor data ACTIVITY CO TENT LOCATION OF RELEASE RETE AsEo OF RELEASE AMOUNT OF ACTIVITY l l NA l l1 l68 l9 J @ l Z l@l NA 7 10 11 44 +5 80 PERSONNEL EXPOSURES N U P.'R E R TYPE DE SCRIPTION li1711 01 0 Ol@l2 l@l NA PERSONNEL NJUfIES NUVBER DESCRIPTION NA l 7

1 s 8 9 l 0l 0l 0 @l 11 12 LO.iS OF OR DAVAGE TO FACILITY TYPE D E SC RIP TIO N NA 7

9 6 9 Q @l 10

' NRC USE ONLY ,

isS 121 o 1 LNU[ NA 8l DESCRIPTION 79030501 % @ l 68 69 i 111111 IiiiIl 60. E DVR 79-027 NAME OF PREPARER PHONE:

TOLEDO EDISON COMPANY DAVIS-BESSE NUCLEAR POWER STATION UNIT ONE SUPPLDfENTAL INFORMATION FOR LER NP-33-79-23 DATE OF EVENT: January 30, 1979 FACILITY: Davis-Besse Unit 1 IDENTIFICATION OF OCCURRENCE: Main Steam Safety Valves SPl7A2 and SPl7B2 declared inoperable.

Conditions Prior to Occurrence: The unit was in Mode 1, with Power (MWT) = 2550, and Load (Gross MWE) = 825.

Description of Occurrence: On January 29, 1979, during a unit startup, load swings re-sulted in the lif ting of Main Steam Line Code Safety Valves SP17A2 and SPl7B2. On Jan-uary 30,1979, during the review of the transient monitor data, it was determined that valves SPl7A2 and SPl7B2 lif ted below their setpoint range, 1050 psig + 1%. At 1645 hours0.019 days <br />0.457 hours <br />0.00272 weeks <br />6.259225e-4 months <br />, valves SPl7A2 and SP17B2 were declared inoperable. This placed the unit in the Action Statement of Technical Specification 3.7.1.1, which requires that with one or more main steam line code valves inoperable in Modes 1, 2, and 3, operation may proceed provided that within four hours, either the inoperable valve (s) is restored te operable status or the high flux trip setpoint is reduced per Table 3.7-1. Unit power was reduced ta less thaa 90% power. At 1715 hours, the high flux setpoints were reduced to 92.6% of rated thermal power.

Designation of Apparent Cause of Occurrence: Main Steam Line Code Safety Valve SP17A2 was f ound to have a loose spindle and was gagged. Valve SPl7B2 was tested, found satis-factory, and declared operable on February 13, 1979.

Analysis of Occurrence: There was no danger to the health and safety of the public or to unit personnel. The remaining eight code saf ety valves per main steam line are operable. These valves have the capacity to relieve steam pressure in case of a unit trip.

Corrective Action: Maintenance Work Order 79-1408 was issued to retest the required main steam safety valves. On February 13, 1979, SP17B2 was tested, found to be within the acceptable tolerance range, and was declared operable by 2330 hours0.027 days <br />0.647 hours <br />0.00385 weeks <br />8.86565e-4 months <br />. SPl7A2 lif ted at 955 psig when tested. When attempting to adjust the valve, it was observed that the top of the spindle was loose. No further attempts were made to adjust the valve and the valve was gagged, rendering it inoperable by 0045 hours5.208333e-4 days <br />0.0125 hours <br />7.440476e-5 weeks <br />1.71225e-5 months <br /> on February 14, 1979. SPl7A2 will be disassembled and repaired at the next suitable unit shutdown.

LER #79-018

e TOLEDO EDISON C0:IPANY (

DAVIS-LESSE NUCLEAR POWER STATION UNIT ONE PAGE 2 SUPPLEMENTAL INFORMATION FOR LER NP-33-79-23 Failure Data:

Prior occurrences of main steam line code safety valves drif ting from their normal setpoints were previously reported in Licensee Event Reports NP-33-77-117 and NP-33-78-145.

LER #79-018

  • e