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| {{#Wiki_filter:LaSalle County Station Exelon Generation ~ 2601 North 2 1'1 Road Marseilles , IL 61341 815-415-2000 Telephon e www. exeloncorp.com RA19-034 1O CFR 50.55a(g) | | {{#Wiki_filter:LaSalle County Station Exelon Generation ~ 2601 North 2 1'1 Road Marseilles , IL 61341 815-415-2000 Telephon e www. exeloncorp.com RA19-034 10 CFR 50.55a(g) |
| June 7, 2019 United States Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555 LaSalle County Station, Unit 2 Renewed Facility Operating License No. NPF-18 NRG Docket No. 50-374 | | June 7, 2019 United States Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555 LaSalle County Station, Unit 2 Renewed Facility Operating License No. NPF-18 NRG Docket No. 50-374 |
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| ==Reference:== | | ==Reference:== |
| : 1. Letter from Susan R. Landahl (Exelon) to the U.S. Nuclear Regulatory Commission, "In Service Inspection (ISi) Intervals," dated September 22, 2006 Exelon Generation Company, LLC (EGG) provides the attached Post-Outage 90-Day lnservice Inspection (ISi) Summary Report for LaSalle County Station Unit 2, submitted in accordance with 1O CFR 50.55a, "Codes and Standards," and the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code Case N-532-5, "Repair/Replacement Activity Documentation Requirements and lnservice Inspection Summary Report Preparation and Submission Section XI, Division 1." | | : 1. Letter from Susan R. Landahl (Exelon) to the U.S. Nuclear Regulatory Commission, "In Service Inspection (ISi) Intervals," dated September 22, 2006 Exelon Generation Company, LLC (EGG) provides the attached Post-Outage 90-Day lnservice Inspection (ISi) Summary Report for LaSalle County Station Unit 2, submitted in accordance with 10 CFR 50.55a, "Codes and Standards," and the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code Case N-532-5, "Repair/Replacement Activity Documentation Requirements and lnservice Inspection Summary Report Preparation and Submission Section XI, Division 1." |
| The attached Post-Outage 90-Day ISi Summary Report is for examinations and repair/replacement activities performed between the end of LaSalle County Station Unit 2 sixteenth refueling outage on March 9, 2017, through the end of the seventeenth refueling outage (L2R17). This refueling outage started on February 18, 2019 and ended on March 9, 2019. This refueling outage was the first outage scheduled for the First Inspection Period of the Fourth lnservice Inspection Interval, and the Third Containment lnservice Inspection Interval, effective from October 1, 2017, through September 30, 2020, for LaSalle County Station Unit 2. | | The attached Post-Outage 90-Day ISi Summary Report is for examinations and repair/replacement activities performed between the end of LaSalle County Station Unit 2 sixteenth refueling outage on March 9, 2017, through the end of the seventeenth refueling outage (L2R17). This refueling outage started on February 18, 2019 and ended on March 9, 2019. This refueling outage was the first outage scheduled for the First Inspection Period of the Fourth lnservice Inspection Interval, and the Third Containment lnservice Inspection Interval, effective from October 1, 2017, through September 30, 2020, for LaSalle County Station Unit 2. |
| LaSalle County Station Unit 2 is owned and operated by EGG, whose address is: | | LaSalle County Station Unit 2 is owned and operated by EGG, whose address is: |
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Category:Inservice/Preservice Inspection and Test Report
MONTHYEARRA23-018, Post-Outage Inservice Inspection (ISI) Summary Report2023-06-27027 June 2023 Post-Outage Inservice Inspection (ISI) Summary Report RA22-051, Submittal of the Snubber Program Plan for the Fourth 10-Year Interval2022-11-16016 November 2022 Submittal of the Snubber Program Plan for the Fourth 10-Year Interval RA22-021, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2022-06-0808 June 2022 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report ML21196A5022021-07-15015 July 2021 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA21-017, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2021-04-0909 April 2021 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report NMP2L2711, Byron Station; Calvert Cliffs; Clinton Power Station; LaSalle County Station; Limerick Generating Station; and Nine Mile Point Nuclear Station - Proposed Alternative to Utilize Code Case N-8792019-10-16016 October 2019 Byron Station; Calvert Cliffs; Clinton Power Station; LaSalle County Station; Limerick Generating Station; and Nine Mile Point Nuclear Station - Proposed Alternative to Utilize Code Case N-879 RA19-034, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2019-06-0707 June 2019 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report NMP2L2700, Co. - Submittal of Proposed Alternative to Utilize Code Case N-879 for Plants2019-04-30030 April 2019 Co. - Submittal of Proposed Alternative to Utilize Code Case N-879 for Plants ML18200A0802018-07-18018 July 2018 Submittal of Fourth 10-Year Interval Inservice Testing (IST) Program Plan RA18-059, Inservice Testing Program Plan, Technical Position TP-052018-07-18018 July 2018 Inservice Testing Program Plan, Technical Position TP-05 ML17314A0082017-11-10010 November 2017 Submittal of Program Plan Associated with the Fourth Lnservice Inspection (ISI) Interval and the Third Containment Lnservice Inspection (Cisi) Interval RA17-055, Post-Outage 90-Day Lnservice Inspection (ISI) Summary Report2017-06-0707 June 2017 Post-Outage 90-Day Lnservice Inspection (ISI) Summary Report RA16-020, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2016-06-0808 June 2016 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA16-021, Cycle 17 Startup Test Report Summary2016-05-12012 May 2016 Cycle 17 Startup Test Report Summary RA15-028, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2015-06-26026 June 2015 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA15-035, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2015-05-28028 May 2015 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RS-15-011, Proposed Alternative to the Examination Requirements for Nozzle-to-Vessel Welds and Inner Radii Sections in Accordance with 10 CFR 50.55a(z)(1)2015-01-29029 January 2015 Proposed Alternative to the Examination Requirements for Nozzle-to-Vessel Welds and Inner Radii Sections in Accordance with 10 CFR 50.55a(z)(1) RA14-018, Post-Outage 90-Day Inservice (ISI) Summary Report2014-05-29029 May 2014 Post-Outage 90-Day Inservice (ISI) Summary Report ML14149A2732014-05-29029 May 2014 LaSalle County Station, Unit 1 - Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA13-023, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2013-05-31031 May 2013 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA12-052, Amended Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2012-10-26026 October 2012 Amended Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA12-018, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2012-06-0505 June 2012 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA11-024, Unit 2 - Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2011-06-0303 June 2011 Unit 2 - Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA10-023, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2010-06-0404 June 2010 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA09-041, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2009-05-0808 May 2009 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA08-070, Submittal of Third 10-Year Inservice Testing (IST) Interval Program Plan2008-12-17017 December 2008 Submittal of Third 10-Year Inservice Testing (IST) Interval Program Plan RA07-045, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2007-06-0101 June 2007 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA07-036, Submittal of Relief Requests Associated with the Third Inservice Inspection (ISI) Interval and the Second Containment Inservice Inspection (Cisi) Interval2007-04-30030 April 2007 Submittal of Relief Requests Associated with the Third Inservice Inspection (ISI) Interval and the Second Containment Inservice Inspection (Cisi) Interval RS-07-058, Amergen/Exelon Nuclear - Request for Relief - Use of the Boiling Water Reactor Vessel and Internals Project (BWRVIP) Guidelines in Lieu of Specific ASME Code Requirements2007-04-19019 April 2007 Amergen/Exelon Nuclear - Request for Relief - Use of the Boiling Water Reactor Vessel and Internals Project (BWRVIP) Guidelines in Lieu of Specific ASME Code Requirements RA06-063, Proposed Third Ten-Year Interval Inservice Testing Program2006-10-16016 October 2006 Proposed Third Ten-Year Interval Inservice Testing Program ML0629704302006-09-29029 September 2006 Proposed Third Ten-Year Interval Inservice Testing Relief Request RA06-038, Post-Outage 90-Day Inservice Inspection Summary Report2006-06-16016 June 2006 Post-Outage 90-Day Inservice Inspection Summary Report ML0518004412005-06-10010 June 2005 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report ML0429405252004-10-15015 October 2004 Amended 90-Day Post Outage ISI Summary Reports ML0414201292004-05-0707 May 2004 Post-Outage 90-Day Inservice Inspection Summary Report ML0314900182003-05-21021 May 2003 Post-Outage 90-Day Inservice Inspection Summary Report ML0213307432002-05-0606 May 2002 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report 2023-06-27
[Table view] Category:Letter type:RA
MONTHYEARRA23-072, Regulatory Commitment Change Summary Report2023-12-15015 December 2023 Regulatory Commitment Change Summary Report RA23-057, Registration of Use of Cask to Store Spent Fuel2023-08-11011 August 2023 Registration of Use of Cask to Store Spent Fuel RA23-055, Registration of Use of Cask to Store Spent Fuel2023-08-11011 August 2023 Registration of Use of Cask to Store Spent Fuel RA23-052, Registration of Use of Cask to Store Spent Fuel2023-08-0404 August 2023 Registration of Use of Cask to Store Spent Fuel RA23-051, Registration of Use of Cask to Store Spent Fuel2023-07-21021 July 2023 Registration of Use of Cask to Store Spent Fuel RA23-048, Registration of Use of Cask to Store Spent Fuel2023-07-14014 July 2023 Registration of Use of Cask to Store Spent Fuel RA23-045, Completion of License Renewal Activities Prior to Entering the Period of Extended Operation2023-06-30030 June 2023 Completion of License Renewal Activities Prior to Entering the Period of Extended Operation RA23-047, Registration of Use of Cask to Store Spent Fuel2023-06-30030 June 2023 Registration of Use of Cask to Store Spent Fuel RA23-018, Post-Outage Inservice Inspection (ISI) Summary Report2023-06-27027 June 2023 Post-Outage Inservice Inspection (ISI) Summary Report RA23-046, Registration of Use of Cask to Store Spent Fuel2023-06-23023 June 2023 Registration of Use of Cask to Store Spent Fuel RA23-042, Registration of Use of Cask to Store Spent Fuel2023-06-16016 June 2023 Registration of Use of Cask to Store Spent Fuel RA23-029, 2022 Annual Radiological Environmental Operating Report2023-05-12012 May 2023 2022 Annual Radiological Environmental Operating Report RA23-028, Submittal of 2022 Annual Radioactive Effluent Release Report2023-04-28028 April 2023 Submittal of 2022 Annual Radioactive Effluent Release Report RA23-027, Annual Dose Report for 20222023-04-21021 April 2023 Annual Dose Report for 2022 RA23-025, Post Accident Monitoring Report2023-04-0707 April 2023 Post Accident Monitoring Report RA23-013, Submittal of Triennial Chlorine Survey Report2023-03-30030 March 2023 Submittal of Triennial Chlorine Survey Report RA23-019, Cycle 20 Core Operating Limits Reports2023-03-21021 March 2023 Cycle 20 Core Operating Limits Reports RA22-066, 150 Day Submittal Cover Letter2022-12-0202 December 2022 150 Day Submittal Cover Letter RA22-060, Regulatory Commitment Change Summary Report2022-11-30030 November 2022 Regulatory Commitment Change Summary Report RA22-051, Submittal of the Snubber Program Plan for the Fourth 10-Year Interval2022-11-16016 November 2022 Submittal of the Snubber Program Plan for the Fourth 10-Year Interval RA22-041, Unit 2 Cycle 19 Core Operating Limits Report Revision2022-10-0505 October 2022 Unit 2 Cycle 19 Core Operating Limits Report Revision RA22-029, Cycle 20 Startup Test Report Summary2022-06-10010 June 2022 Cycle 20 Startup Test Report Summary RA22-021, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2022-06-0808 June 2022 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA22-020, Annual Radiological Environmental Operating Report2022-05-13013 May 2022 Annual Radiological Environmental Operating Report RA22-018, Annual Dose Report for 20212022-04-22022 April 2022 Annual Dose Report for 2021 RA22-010, Cycle 20 Core Operating Limits Reports2022-03-21021 March 2022 Cycle 20 Core Operating Limits Reports RA21-059, Regulatory Commitment Change Summary Report2021-11-30030 November 2021 Regulatory Commitment Change Summary Report RA21-050, Completion of License Renewal Activities Prior to Entering the Period of Extended Operation2021-11-0909 November 2021 Completion of License Renewal Activities Prior to Entering the Period of Extended Operation RA21-051, County Station Physical Security Plan (Revision 18)2021-09-29029 September 2021 County Station Physical Security Plan (Revision 18) RA21-052, Registration of Use of Cask Store Spent Fuel2021-09-17017 September 2021 Registration of Use of Cask Store Spent Fuel RA21-046, Registration of Use of Cask to Store Spent Fuel2021-08-0505 August 2021 Registration of Use of Cask to Store Spent Fuel RA21-043, Cycle 19 Startup Test Report Summary2021-07-15015 July 2021 Cycle 19 Startup Test Report Summary RA21-031, 2020 Annual Radiological Environmental Operating Report2021-05-13013 May 2021 2020 Annual Radiological Environmental Operating Report RA21-029, Unit 2 - 2020 Annual Radioactive Effluent Release Report2021-04-29029 April 2021 Unit 2 - 2020 Annual Radioactive Effluent Release Report RA21-026, Annual Dose Report for 20202021-04-22022 April 2021 Annual Dose Report for 2020 RA21-016, Netco Rack Insert 10-year Surveillance Report2021-04-15015 April 2021 Netco Rack Insert 10-year Surveillance Report RA21-017, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2021-04-0909 April 2021 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA21-019, Unit 2 Cycle 19 Core Operating Limits Reports2021-04-0707 April 2021 Unit 2 Cycle 19 Core Operating Limits Reports RA20-058, Licensee Post Exam Submittal Letter2020-12-0202 December 2020 Licensee Post Exam Submittal Letter RA20-044, Unit 2 - Unit 1 Cycle 19 Core Operating Limits Report2020-09-10010 September 2020 Unit 2 - Unit 1 Cycle 19 Core Operating Limits Report RA20-026, 2019 Annual Radiological Environmental Operating Report2020-05-13013 May 2020 2019 Annual Radiological Environmental Operating Report RA20-023, Annual Dose Report for 20192020-04-28028 April 2020 Annual Dose Report for 2019 RA20-016, Corrected Drawing for One-Line Electrical Power Supply for Containment Vent System Final Integrated Plan2020-03-24024 March 2020 Corrected Drawing for One-Line Electrical Power Supply for Containment Vent System Final Integrated Plan RA20-015, Triennial Chlorine Survey Report2020-03-20020 March 2020 Triennial Chlorine Survey Report RA20-014, Cycle 19 and Cycle 18 Core Operating Limits Reports2020-03-12012 March 2020 Cycle 19 and Cycle 18 Core Operating Limits Reports RA19-048, Registration of Use of Cask to Store Spent Fuel2019-09-0606 September 2019 Registration of Use of Cask to Store Spent Fuel RA19-045, Registration of Use of Cask to Store Spent Fuel2019-08-0909 August 2019 Registration of Use of Cask to Store Spent Fuel RA19-041, Registration of Use of Cask to Store Spent Fuel2019-07-0303 July 2019 Registration of Use of Cask to Store Spent Fuel RA19-039, Registration of Use of Cask to Store Spent Fuel2019-06-25025 June 2019 Registration of Use of Cask to Store Spent Fuel RA19-034, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2019-06-0707 June 2019 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report 2023-08-04
[Table view] |
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LaSalle County Station Exelon Generation ~ 2601 North 2 1'1 Road Marseilles , IL 61341 815-415-2000 Telephon e www. exeloncorp.com RA19-034 10 CFR 50.55a(g)
June 7, 2019 United States Nuclear Regulatory Commission Attention: Document Control Desk Washington, D.C. 20555 LaSalle County Station, Unit 2 Renewed Facility Operating License No. NPF-18 NRG Docket No. 50-374
Subject:
Post-Outage 90-Day lnservice Inspection (ISi) Summary Report
Reference:
- 1. Letter from Susan R. Landahl (Exelon) to the U.S. Nuclear Regulatory Commission, "In Service Inspection (ISi) Intervals," dated September 22, 2006 Exelon Generation Company, LLC (EGG) provides the attached Post-Outage 90-Day lnservice Inspection (ISi) Summary Report for LaSalle County Station Unit 2, submitted in accordance with 10 CFR 50.55a, "Codes and Standards," and the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code Case N-532-5, "Repair/Replacement Activity Documentation Requirements and lnservice Inspection Summary Report Preparation and Submission Section XI, Division 1."
The attached Post-Outage 90-Day ISi Summary Report is for examinations and repair/replacement activities performed between the end of LaSalle County Station Unit 2 sixteenth refueling outage on March 9, 2017, through the end of the seventeenth refueling outage (L2R17). This refueling outage started on February 18, 2019 and ended on March 9, 2019. This refueling outage was the first outage scheduled for the First Inspection Period of the Fourth lnservice Inspection Interval, and the Third Containment lnservice Inspection Interval, effective from October 1, 2017, through September 30, 2020, for LaSalle County Station Unit 2.
LaSalle County Station Unit 2 is owned and operated by EGG, whose address is:
Exelon Generation Company, LLC 200 Exelon Way Kennett Square, PA 19348 To the best of our knowledge and belief, the statements made in this report are correct, and the examinations and corrective measures, as applicable, conform to the rules of the ASME Boiler and Pressure Vessel Code,Section XI.
NRC RA 19-034 June 7, 2019 Page 2 of 2 There are no regulatory commitments contained in this report. Should you have any questions concerning this letter, please contact Mr. Daniel Mearhoff, Regulatory Assurance Manager, at (815) 415-2800.
Respectfully,
~~r.~
Joh~ }~ashko Site Vice President LaSalle County Station
Attachment:
Form OAR-1 Owner's Activity Report cc: Regional Administrator - NRC Region Ill NRC Senior Resident Inspector - LaSalle County Station
ATTACHMENT 1 FORM OAR-1 OWNER'S ACTIVITY REPORT Plant LaSalle County Station, 2601 North 21st Road, Marseilles, IL 61341-9757 Unit No. 2 Commercial Service Date October 17, 1984 Refueling Outage Number L2R17 (if applicable)
Current Inspection Interval Fourth Inspection Interval (ISi), Third Inspection Interval (Containment ISi)
(1 " , 2°*, 3'd, 4'". other)
Current Inspection Period First Inspection Period (ISi and Containment ISi)
(1, 2nd, 310 }
ASME Section XI 2001 Edition through 2003 Addenda, and Edition and Addenda of Section XI applicable to the inspection plans ASME Section XI 2007 Edition through 2008 Addenda Date and Revision of inspection plans October 9, 2014 Revision 3 (previous interval), November 20, 2017 Revision 0 (current interval)
Edition and Addenda of Section XI applicable to repair/replacement activities, if different than the inspection plans Same as above Code Cases used for inspection and evaluation: N-508-4, N-532-4, N-532-5, N-578, N-586-1, N-639, N-702, N-747, N-805 (if applicable, including cases *modified by Case N-532 and later revisions)
CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations and tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of L2R17 conform to the requirements of Section x1.* (refueling outage number)
Signed Fleet. I5I G1 )/Ice{ Date CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and employed by The Hartford Steam Boiler Inspection and Insurance Company of Hartford, Connecticut have inspected the items described in this Owner's Activity Report, and state that, to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.
By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report. Furthermore, neither the Inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.
Commissions rJ.8 lo 17). A.) I (Inspector's Signature) (National Board Number and Endorsement)
Date '// )11 I
- Reference Issue Reports 4251021 and 4252624 regarding deviation from Specification J-2582 for Cat ID 1777199-1.
Page 1 of 3
TABLE 2 ABSTRACT OF REPAIR/REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Code Item Description Date Repair/Replacement Class Description Of Work Completed Plan Number Indication on 28 Reactor Recirc Pump Lug (IR 4221690). Indication reduced to acceptable size per WO 4890185. EC 1 2B33-C001B 2/26/19 2-19-2228 627 440 evaluated no additional examinations required per Code Case N-586-1 (b)(2).
Loose bolting on pipe clamp for supports 2RR00-2060X 1 (IR 4222601 ). Tightened bolting and 2/27/19 WO 4618927-32 2RR00-2061 X performed scope expansion.
F.6 RPV Vent Mechanical thread damage on Flange WO 4680705-01 1 Piping Bolted F.6 studs (IR 4224239). Bolting was 3/8/19 2-19-2447 Connection replaced.
Loose jam nuts and bolt assembly on 1 2LP02-2801 C piping support (IR 4225739). Tightened 3/2/19 WO 4893645-02 boltinq and performed scope expansion.
Leak identified on header for 2VY03A cooler (IR 4139831 ). Temporary clamp installed per EC 624352 and WO WO 4787178 4787178. Cooler 2VY03A (which 3 2VY03A 2/27/19 WO 4633535 contained the temporary clamp) was 2-19-2258 replaced during L2R17 under WO 4633535. IR 4254693 for lost paperwork associated with clamp.
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TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Examination Item Item Description Evaluation Description Categorv Number Evaluated acceptable as-is, installed
~HG06-2103V Variable Support, spring can acceptable for this application, F-A F1 .20C installed spring can did not match
~CR 439856 to update drawing to reflect drawing (IA 4221583) installed condition.
Evaluated acceptable as-is, with 2RI01-2801 C Constant Support, capability for full movement of piping.
F-A F1.10 as-found cold setting not optimum WO 4893159 scheduled to adjust setting for range (IA 4224612) to optimize ranoe.
Evaluated acceptable as-is. The Replacement cooling coils for replacement cooling coils were built to the 1VY03A and 2VY03A did not have requirements of ASME Section Ill, and an Authorized Nuclear Inspector 0-B 02.10 passed all required testing and present during the hydrostatic examinations, with the exception of an testing at the manufacturer's ANI witness, and passed all post-facility. (IA 4252624) modification testino after installation.
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