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| issue date = 11/05/1993
| issue date = 11/05/1993
| title = LER 93-029-00:on 930805,discovered Primary Coolant Steam Leak.Caused by Weld Defect.Weld Crack Repaired on 930806. Weld Record for Applicable Weld Also Reviewed & No Discrepancies Identified
| title = LER 93-029-00:on 930805,discovered Primary Coolant Steam Leak.Caused by Weld Defect.Weld Crack Repaired on 930806. Weld Record for Applicable Weld Also Reviewed & No Discrepancies Identified
| author name = FIES C L
| author name = Fies C
| author affiliation = WASHINGTON PUBLIC POWER SUPPLY SYSTEM
| author affiliation = WASHINGTON PUBLIC POWER SUPPLY SYSTEM
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:LICENSEE EVEOREPORT (LER)ACILITY NAHE (I)Washin ton Nuclear Plant-Unit 2 DCKET HUHB R ()PAGE (3)0 5 0 0 0 3 9 7 I DF 4 ITLE (4)STEAM LINE FLO%ELEMENT SENSING LINE PINHOLE LEAK EVENT DATE (5)LER NUNBER 6 REPORT DATE 7 OTHER FACILITIES INVOLVED 8 NONTH DAY YEAR SEQUENTIAL HUHBER EV I 5 ION UNBER HDNTN DAY YEAR FACILITY NANES CKET NUMB R (S)0 8 0 5 9 3 9 3 0 2 9 0 0 0 5 9 3 05 05 0 0 0 000 P ERAT ING DDE (9)HIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREHEHTS OF 10 CFR E: (Check one or more of the following)
{{#Wiki_filter:LICENSEE EVEOREPORT (LER)
(11)3 OWER LEVEL (10)0.402(b)0.405(a)(1)(i) 0.405(a)(1)(ii) 20.405(a)(1)(iii) 20.405(a)(l)(iv) 0.405(a)(1)(v) 0.405(C)0.36(c)(1) 0.36(c)2)X 50.73(a)2)(i)5D.73(a)2)(ii)50.73(a)(2)(iii)0.73(a)(2)(iv) 0.73 a)(2)(v)0.73 a)(2)(vii) 0.73 a)(2)(viii)(A) 50.73 a)(2)(viii)(B) 50.73(a)(2)(x) 77.71(b)73.73(c)THER (Specify in Abstract elow and in Text.NRC Form 366A)AHE LICENSEE CONTACT FOR THIS LER 12 C.L.Fies, Licensing Engineer REA CODE TELEPHONE HUHBER 0 9 7 7-4 1 4 7 COHPLETE OHE LINE FOR EACH COHPOHEHT FAILURE DESCRIBED IH THIS REPORT (13)CAUSE SYSTEH COHPOHEHT HANUFACTURER EPORTABLE 0 HPRDS CAUSE SYSTEH CONPOHEHT NAHUFACTURER REPORTABLE TO HPRDS SUPPLEHEHTAL REPORT EXPECTED (14)YES (If yes, coapiete EXPECTED SUBHISSIOH DATE)X HO TRACT eel EXPECTED SUBHISSIOH HOHTH DAY YEAR ATE (15)On August 5, 1993, with the plant in Mode 3 (Hot Shutdown)a system engineer discovered a small steam leak of reactor coolant located upstream of the"A" Inboard Main Steam Isolation Valve inside the Primary Containment.
ACILITY NAHE       (I)                                                                               DCKET HUHB R ( )                       PAGE (3)
The steam flow was from an unisolatable pinhole leak at a flow element sensing line weld.Control Room personnel immediately initiated a plant cooldown from Mode 3 to Mode 4 (Cold Shutdown)to allow repair of the leak.The root cause of the steam leak was a weld defect.A defect introduced into the root of the weld during installation served as the initiation point with subsequent crack propagation due to fatigue.The weld crack was repaired on August 6, 1993.This event posed no threat to the safety of the public or plant personnel.
Washin ton Nuclear Plant -                  Unit  2                                            0   5   0   0     0   3     9   7     I   DF   4 ITLE (4)
9311100114 931105 PDR ADOCK 05000397 S PDR LICENSEE EVENT REPORT'R)TEXT CONTINUATION ACIL1TY NANF (1)Washington Nuclear Plant-Unit 2 DOCKET NUMBER (2)0 5 0 0 0 3 9 7 LER NURSER (8)ear umber ev.No.3 029 i 00 AGE (3)2 OF'4 ITLE (4)STEAMLINE FLOW ELEMENT SENSING LINE PINHOLE LEAK Pl t ni'n Power Level-0%Plant Mode-3 (Hot Shutdown)Even D ri tion On August 5, 1993, with the plant in Mode 3 (Hot Shutdown), a system engineer discovered a small unisolatable steam leak of primary coolant.The leak was discovered during ongoing work associated with recovery from a reactor scram (see LER 93-027).The leak was located in the Containment Drywell upstream of the"A" Main Steam Isolation Valve (MSIV), MS-V-22A.The steam flow was from an unisolatable pinhole leak emanating from the"A" Main Steam Line Flow Element, MS-FE-SA, sensing line weld.Imrr,edi rr iv A in On August 5, 1993, at 0846 hours, Control Room personnel initiated a plant cooldown from Mode 3 to Mode 4 (Cold Shutdown)to maintain compliance with Technical Specifications associated with PRESSURE BOUNDARY LEAKAGE in Modes 1, 2, or 3.Further Ev 1 ti n R e nd rr iv A in Further Ev lu ti n On August 5, 1993, at approximately 0838 hours, this event was reported to the NRC by telephone in accordance with 10CFR50.72(b)(2)(i).
STEAM LINE FLO% ELEMENT SENSING LINE PINHOLE LEAK EVENT DATE     (5)               LER NUNBER 6                 REPORT DATE     7                 OTHER FACILITIES INVOLVED 8 NONTH       DAY             YEAR     SEQUENTIAL     EV I 5 ION   HDNTN     DAY   YEAR FACILITY NANES                                   CKET NUMB R   (S)
This event is also reportable under 10CFR50.73(a)(2)(i)(A),"The completion of any nuclear plant shutdown required by the plant's Technical Specifications." The WNP-2 Technical Specifications do not permit any reactor coolant pressure boundary leakage.2.An Engineering review of the instrument line calculation was completed.
HUHBER        UNBER 05  0 0 0 0    8   0     5 9   3   9   3     0   2   9     0     0               0   5 9   3                                               05 000 P ERAT ING               HIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREHEHTS OF 10 CFR E: (Check one             or   more of the following) (11)
Stresses were calculated to be well below the ASME Code allowables for all deadweight, thermal, and dynamic loading conditions.
DDE  (9)             3 OWER   LEVEL                 0.402(b)                       0.405(C)                     0.73(a)(2)(iv)                   77.71(b)
3.The weld record for this weld was reviewed and no discrepancies were identified.
(10)                           0.405(a)(1)(i)                 0.36(c)(1)                   0.73 a)(2)(v)                    73.73(c) 0.405(a)(1)(ii)                0.36(c) 2)                   0.73 a)(2)(vii)                 THER  (Specify in Abstract 20.405(a)(1)(iii)             X 50.73(a)   2)(i)             0.73 a)(2)(viii)(A)             elow and in Text. NRC 20.405(a)(l)(iv)               5D.73(a)   2)(ii)           50.73 a)(2)(viii)(B)             Form 366A) 0.405(a)(1)(v)                50.73(a)(2)(   iii)         50.73(a)(2)(x)
L LICENSEE EVENT REPORTR)TEKl CONTINUATION-ACILITY NAME (1)Washington Nuclear Plant-Unit 2 DOCKET NUMBER (2)0 5 0 0 0 3 9 7 LER NUMBER (8)ear umbel'v.No.3 029 00 AGE (3)3 OF 4 iTLE (4)STEANLINE FLOW ELEMENT SENSING LINE PINHOLE LEAK 4.Materials and Welding personnel performed a failure analysis on the weld and determined that the cracking had initiated at an undetectable construction defect at the root of the weld.The propagation of the crack from the root was attributed to fatigue.WNP-2 has had fatigue failures of socket welds in the past.The stress concentrations in a socket weld are at the root of the weld and the toe of the weld.If an anomaly exists at the root of the weld;the cyclic loading, if high enough, will tend to propagate the defect.If no anomalies exist at the root of the weld, the cyclic loading, if high enough, will initiate cracking at the toe of the weld.In this case, the root defect, which was not detectable by the required surface examinations, had propagated by fatigue to the weld surface.5.No intergranular stress corrosion cracking was identified at this weld joint.~Retype The root cause of the steam leak was a weld defect.A defect'introduced into the root of the weld during installation acted as an initiation point for the fatigue failure.F her rrective Ac ion 2.The weld crack was repaired in accordance with Maintenance Work Request AP4900 and ASME Section XI Plan 2-0975 on August 6, 1993.Engineering has an on going program for-identifying candidates for fatigue cracking on the small break LOCA boundaries, with the main emphasis on the primary coolant/containment pressure boundary.The program, however, focuses on high probability failure locations.
LICENSEE CONTACT FOR THIS LER         12 AHE                                                                                                                            TELEPHONE HUHBER C. L. Fies, Licensing Engineer                                                               REA CODE 0   9       7   7   -   4   1   4   7 COHPLETE OHE LINE FOR EACH COHPOHEHT FAILURE DESCRIBED IH THIS REPORT             (13)
Socket welded process piping similar to this failure have not historically been a problem area.Cantilevered socket welded vent, drain, and test connections continue to be replaced on a priority basis during annual outages.f i nifi n The steam leak was very small and it was concluded the weld defect did not challenge plant safety in that it represented a leakage well within the ability to provide makeup of primary coolant inventory.
CAUSE         SYSTEH     COHPOHEHT     HANUFACTURER   EPORTABLE             CAUSE   SYSTEH       CONPOHEHT         NAHUFACTURER     REPORTABLE 0  HPRDS                                                                        TO HPRDS SUPPLEHEHTAL REPORT EXPECTED     (14)                                   EXPECTED SUBHISSIOH        HOHTH  DAY    YEAR ATE (15)
In addition, the steam plume did not challenge safety-related equipment.
YES    (If yes,   coapiete EXPECTED SUBHISSIOH DATE)     X   HO TRACT eel On August 5, 1993, with the plant in Mode 3 (Hot Shutdown) a system engineer discovered a small steam leak of reactor coolant located upstream of the "A" Inboard Main Steam Isolation Valve inside the Primary Containment. The steam flow was from an unisolatable pinhole leak at a flow element sensing line weld.
Plant records documenting drywell floor drain leakage from August 2, 1993, to August 6, 1993, report zero leakage confirming the character of the leak.Leak before break was demonstrated and if the crack had opened up during further plant operation the unidentifiable leak rate would have eventually increased identifying a problem within the containment.
Control Room personnel immediately initiated a plant cooldown from Mode 3 to Mode 4 (Cold Shutdown) to allow repair of the leak.
LICENSEE EVENT REPORT QR)TEXT CONTINUATlON ACILITY NANE (I)Washington Nuclear Plant-Unit 2 DOCKET NUMBER (2)0 5 0 0 0 3 9 7 LER NUNBER (8)eer umber ev.No.3 029 OO AGE (3)4 OF 4.ITLE.(4)STEAMLINE FLOW ELEtIlENT SENSING LINE PINHOLE LEAK imilar event The Supply System has had other small bore fatigue failures associated with socket welded vent, drain and test connections which are a cantilever beam type design as reported in LERs 90-028 and 91-030..These, as mentioned above, are being addressed under an ongoing engineering program.There have been only two other instrumentation line failures inside containment, one failure mechanism was indeterminate and the other was due to intergranular stress corrosion.
The root cause of the steam leak was a weld defect. A defect introduced into the root of the weld during installation served as the initiation point with subsequent crack propagation due to fatigue.
These two failures were not reportable as LERs because they were found during plant outages.EII Informa i n*f/@~tern~monent Main Steam Isolation Valve Primary Containment Steam Line Flow Element, MS-FE-5A SB BT SB V FE}}
The weld crack was repaired on August 6, 1993.
This event posed no threat to the safety of the public or plant personnel.
9311100114 931105 PDR     ADOCK 05000397 S                         PDR
 
LICENSEE EVENT REPORT 'R)
TEXT CONTINUATION ACIL1TY NANF (1)                             DOCKET NUMBER   (2)             LER NURSER   (8)        AGE (3) ear     umber         ev. No.
Washington Nuclear Plant - Unit      2 0  5  0    0  0 3 9 7 3     029      i  00        2 OF '4 ITLE (4)
STEAMLINE FLOW ELEMENT SENSING LINE PINHOLE LEAK Pl   t   ni'n Power Level - 0%
Plant Mode - 3 (Hot Shutdown)
Even D       ri tion On August 5, 1993, with the plant in Mode 3 (Hot Shutdown), a system engineer discovered a small unisolatable steam leak of primary coolant. The leak was discovered during ongoing work associated with recovery from a reactor scram (see LER 93-027). The leak was located in the Containment Drywell upstream of the "A" Main Steam Isolation Valve (MSIV), MS-V-22A. The steam flow was from an unisolatable pinhole leak emanating from the "A" Main Steam Line Flow Element, MS-FE-SA, sensing line weld.
Imrr,edi         rr   iv A in On August 5, 1993, at 0846 hours, Control Room personnel initiated a plant cooldown from Mode 3 to Mode 4 (Cold Shutdown) to maintain compliance with Technical Specifications associated with PRESSURE BOUNDARY LEAKAGE in Modes 1, 2, or 3.
Further Ev     1 ti n   R     e nd   rr   iv A     in Further Ev lu ti     n On August 5, 1993, at approximately 0838 hours, this event was reported to the NRC by telephone in accordance with 10CFR50.72(b)(2)(i). This event is also reportable under 10CFR50.73(a)(2)(i)(A), "The completion of any nuclear plant shutdown required by the plant's Technical Specifications." The WNP-2 Technical Specifications do not permit any reactor coolant pressure boundary leakage.
: 2.     An Engineering review of the instrument line calculation was completed. Stresses were calculated to be well below the ASME Code allowables for all deadweight, thermal, and dynamic loading conditions.
: 3.     The weld record for this weld was reviewed and no discrepancies were identified.
 
L LICENSEE EVENT REPORTR)
TEKl CONTINUATION ACILITY NAME (1)                                 DOCKET NUMBER (2)               LER NUMBER (8)       AGE (3)
Washington Nuclear Plant - Unit          2 ear     umbel'v.     No.
0  5  0  0  0 3 9  7 3      029       00       3 OF 4 iTLE (4)
STEANLINE FLOW ELEMENT SENSING LINE PINHOLE LEAK
: 4.       Materials and Welding personnel performed a failure analysis on the weld and determined that the cracking had initiated at an undetectable construction defect at the root of the weld. The propagation of the crack from the root was attributed to fatigue. WNP-2 has had fatigue failures of socket welds in the past. The stress concentrations in a socket weld are at the root of the weld and the toe of the weld. Ifan anomaly exists at the root of the weld; the cyclic loading, if high enough, will tend to propagate the defect. If no anomalies exist at the root of the weld, the cyclic loading, if high enough, will initiate cracking at the toe of the weld. In this case, the root defect, which was not detectable by the required surface examinations, had propagated by fatigue to the weld surface.
: 5.       No intergranular stress corrosion cracking was identified at this weld joint.
  ~Retype The root cause of the steam leak was a weld defect. A defect'introduced into the root of the weld during installation acted as an initiation point for the fatigue failure.
F   her     rrective Ac ion The weld crack was repaired in accordance with Maintenance Work Request AP4900 and ASME Section XI Plan 2-0975 on August 6, 1993.
: 2.      Engineering has an on going program for-identifying candidates for fatigue cracking on the small break LOCA boundaries, with the main emphasis on the primary coolant/containment pressure boundary. The program, however, focuses on high probability failure locations. Socket welded process piping similar to this failure have not historically been a problem area. Cantilevered socket welded vent, drain, and test connections continue to be replaced on a priority basis during annual outages.
f     i nifi n The steam leak was very small and it was concluded the weld defect did not challenge plant safety in that it represented a leakage well within the ability to provide makeup of primary coolant inventory. In addition, the steam plume did not challenge safety-related equipment. Plant records documenting drywell floor drain leakage from August 2, 1993, to August 6, 1993, report zero leakage confirming the character of the leak.
Leak before break was demonstrated and if the crack had opened up during further plant operation the unidentifiable leak rate would have eventually increased identifying a problem within the containment.
 
LICENSEE EVENT REPORT QR)
TEXT CONTINUATlON ACILITY NANE (I)                               DOCKET NUMBER (2)               LER NUNBER (8)        AGE (3) eer   umber       ev. No.
Washington Nuclear Plant - Unit        2 0  5  0  0  0 3 9  7 3   029         OO         4 OF 4
.ITLE .(4)
STEAMLINE FLOW ELEtIlENT SENSING LINE PINHOLE LEAK imilar event The Supply System has had other small bore fatigue failures associated with socket welded vent, drain and test connections which are a cantilever beam type design as reported in LERs 90-028 and 91-030.. These, as mentioned above, are being addressed under an ongoing engineering program. There have been only two other instrumentation line failures inside containment, one failure mechanism was indeterminate and the other was due to intergranular stress corrosion. These two failures were not reportable as LERs because they were found during plant outages.
EII Informa i n
                                                                                    *f
                                                                      /@~tern         ~monent Main Steam Isolation Valve                                 SB                V Primary Containment                                       BT Steam Line Flow Element, MS-FE-5A                         SB               FE}}

Latest revision as of 13:41, 29 October 2019

LER 93-029-00:on 930805,discovered Primary Coolant Steam Leak.Caused by Weld Defect.Weld Crack Repaired on 930806. Weld Record for Applicable Weld Also Reviewed & No Discrepancies Identified
ML17290A731
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 11/05/1993
From: Fies C
WASHINGTON PUBLIC POWER SUPPLY SYSTEM
To:
Shared Package
ML17290A730 List:
References
LER-93-029, LER-93-29, NUDOCS 9311100114
Download: ML17290A731 (5)


Text

LICENSEE EVEOREPORT (LER)

ACILITY NAHE (I) DCKET HUHB R ( ) PAGE (3)

Washin ton Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 I DF 4 ITLE (4)

STEAM LINE FLO% ELEMENT SENSING LINE PINHOLE LEAK EVENT DATE (5) LER NUNBER 6 REPORT DATE 7 OTHER FACILITIES INVOLVED 8 NONTH DAY YEAR SEQUENTIAL EV I 5 ION HDNTN DAY YEAR FACILITY NANES CKET NUMB R (S)

HUHBER UNBER 05 0 0 0 0 8 0 5 9 3 9 3 0 2 9 0 0 0 5 9 3 05 000 P ERAT ING HIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREHEHTS OF 10 CFR E: (Check one or more of the following) (11)

DDE (9) 3 OWER LEVEL 0.402(b) 0.405(C) 0.73(a)(2)(iv) 77.71(b)

(10) 0.405(a)(1)(i) 0.36(c)(1) 0.73 a)(2)(v) 73.73(c) 0.405(a)(1)(ii) 0.36(c) 2) 0.73 a)(2)(vii) THER (Specify in Abstract 20.405(a)(1)(iii) X 50.73(a) 2)(i) 0.73 a)(2)(viii)(A) elow and in Text. NRC 20.405(a)(l)(iv) 5D.73(a) 2)(ii) 50.73 a)(2)(viii)(B) Form 366A) 0.405(a)(1)(v) 50.73(a)(2)( iii) 50.73(a)(2)(x)

LICENSEE CONTACT FOR THIS LER 12 AHE TELEPHONE HUHBER C. L. Fies, Licensing Engineer REA CODE 0 9 7 7 - 4 1 4 7 COHPLETE OHE LINE FOR EACH COHPOHEHT FAILURE DESCRIBED IH THIS REPORT (13)

CAUSE SYSTEH COHPOHEHT HANUFACTURER EPORTABLE CAUSE SYSTEH CONPOHEHT NAHUFACTURER REPORTABLE 0 HPRDS TO HPRDS SUPPLEHEHTAL REPORT EXPECTED (14) EXPECTED SUBHISSIOH HOHTH DAY YEAR ATE (15)

YES (If yes, coapiete EXPECTED SUBHISSIOH DATE) X HO TRACT eel On August 5, 1993, with the plant in Mode 3 (Hot Shutdown) a system engineer discovered a small steam leak of reactor coolant located upstream of the "A" Inboard Main Steam Isolation Valve inside the Primary Containment. The steam flow was from an unisolatable pinhole leak at a flow element sensing line weld.

Control Room personnel immediately initiated a plant cooldown from Mode 3 to Mode 4 (Cold Shutdown) to allow repair of the leak.

The root cause of the steam leak was a weld defect. A defect introduced into the root of the weld during installation served as the initiation point with subsequent crack propagation due to fatigue.

The weld crack was repaired on August 6, 1993.

This event posed no threat to the safety of the public or plant personnel.

9311100114 931105 PDR ADOCK 05000397 S PDR

LICENSEE EVENT REPORT 'R)

TEXT CONTINUATION ACIL1TY NANF (1) DOCKET NUMBER (2) LER NURSER (8) AGE (3) ear umber ev. No.

Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 3 029 i 00 2 OF '4 ITLE (4)

STEAMLINE FLOW ELEMENT SENSING LINE PINHOLE LEAK Pl t ni'n Power Level - 0%

Plant Mode - 3 (Hot Shutdown)

Even D ri tion On August 5, 1993, with the plant in Mode 3 (Hot Shutdown), a system engineer discovered a small unisolatable steam leak of primary coolant. The leak was discovered during ongoing work associated with recovery from a reactor scram (see LER 93-027). The leak was located in the Containment Drywell upstream of the "A" Main Steam Isolation Valve (MSIV), MS-V-22A. The steam flow was from an unisolatable pinhole leak emanating from the "A" Main Steam Line Flow Element, MS-FE-SA, sensing line weld.

Imrr,edi rr iv A in On August 5, 1993, at 0846 hours0.00979 days <br />0.235 hours <br />0.0014 weeks <br />3.21903e-4 months <br />, Control Room personnel initiated a plant cooldown from Mode 3 to Mode 4 (Cold Shutdown) to maintain compliance with Technical Specifications associated with PRESSURE BOUNDARY LEAKAGE in Modes 1, 2, or 3.

Further Ev 1 ti n R e nd rr iv A in Further Ev lu ti n On August 5, 1993, at approximately 0838 hours0.0097 days <br />0.233 hours <br />0.00139 weeks <br />3.18859e-4 months <br />, this event was reported to the NRC by telephone in accordance with 10CFR50.72(b)(2)(i). This event is also reportable under 10CFR50.73(a)(2)(i)(A), "The completion of any nuclear plant shutdown required by the plant's Technical Specifications." The WNP-2 Technical Specifications do not permit any reactor coolant pressure boundary leakage.

2. An Engineering review of the instrument line calculation was completed. Stresses were calculated to be well below the ASME Code allowables for all deadweight, thermal, and dynamic loading conditions.
3. The weld record for this weld was reviewed and no discrepancies were identified.

L LICENSEE EVENT REPORTR)

TEKl CONTINUATION ACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (8) AGE (3)

Washington Nuclear Plant - Unit 2 ear umbel'v. No.

0 5 0 0 0 3 9 7 3 029 00 3 OF 4 iTLE (4)

STEANLINE FLOW ELEMENT SENSING LINE PINHOLE LEAK

4. Materials and Welding personnel performed a failure analysis on the weld and determined that the cracking had initiated at an undetectable construction defect at the root of the weld. The propagation of the crack from the root was attributed to fatigue. WNP-2 has had fatigue failures of socket welds in the past. The stress concentrations in a socket weld are at the root of the weld and the toe of the weld. Ifan anomaly exists at the root of the weld; the cyclic loading, if high enough, will tend to propagate the defect. If no anomalies exist at the root of the weld, the cyclic loading, if high enough, will initiate cracking at the toe of the weld. In this case, the root defect, which was not detectable by the required surface examinations, had propagated by fatigue to the weld surface.
5. No intergranular stress corrosion cracking was identified at this weld joint.

~Retype The root cause of the steam leak was a weld defect. A defect'introduced into the root of the weld during installation acted as an initiation point for the fatigue failure.

F her rrective Ac ion The weld crack was repaired in accordance with Maintenance Work Request AP4900 and ASME Section XI Plan 2-0975 on August 6, 1993.

2. Engineering has an on going program for-identifying candidates for fatigue cracking on the small break LOCA boundaries, with the main emphasis on the primary coolant/containment pressure boundary. The program, however, focuses on high probability failure locations. Socket welded process piping similar to this failure have not historically been a problem area. Cantilevered socket welded vent, drain, and test connections continue to be replaced on a priority basis during annual outages.

f i nifi n The steam leak was very small and it was concluded the weld defect did not challenge plant safety in that it represented a leakage well within the ability to provide makeup of primary coolant inventory. In addition, the steam plume did not challenge safety-related equipment. Plant records documenting drywell floor drain leakage from August 2, 1993, to August 6, 1993, report zero leakage confirming the character of the leak.

Leak before break was demonstrated and if the crack had opened up during further plant operation the unidentifiable leak rate would have eventually increased identifying a problem within the containment.

LICENSEE EVENT REPORT QR)

TEXT CONTINUATlON ACILITY NANE (I) DOCKET NUMBER (2) LER NUNBER (8) AGE (3) eer umber ev. No.

Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 3 029 OO 4 OF 4

.ITLE .(4)

STEAMLINE FLOW ELEtIlENT SENSING LINE PINHOLE LEAK imilar event The Supply System has had other small bore fatigue failures associated with socket welded vent, drain and test connections which are a cantilever beam type design as reported in LERs90-028 and 91-030.. These, as mentioned above, are being addressed under an ongoing engineering program. There have been only two other instrumentation line failures inside containment, one failure mechanism was indeterminate and the other was due to intergranular stress corrosion. These two failures were not reportable as LERs because they were found during plant outages.

EII Informa i n

  • f

/@~tern ~monent Main Steam Isolation Valve SB V Primary Containment BT Steam Line Flow Element, MS-FE-5A SB FE