ML18078A591: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
(Created page by program invented by StriderTol)
Line 17: Line 17:


=Text=
=Text=
{{#Wiki_filter:U.S. NUCLEAR REGULATURY COMMISSION e LICENSEE EVENT REPORT e CONTROL BLOCK: !o-1 __ . .._I _.__....____._....__..j
{{#Wiki_filter:e    LICENSEE EVENT REPORT U.S. NUCLEAR REGULATURY COMMISSION e
: 0) 1 " (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI
CONTROL BLOCK:             !o-1_ _..._I_.__....____._....__..j 0)                     (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI 1                                      "
[§J2J IN IJ Is I G Is I 1 101 a I a I -I a I a I a I o I a I -I o I a IG)l 4 I 1I1I1 I 1 IG)I I I© 7 8 9
[§J2J IN IJ Is I G Is I 1 101 a I aI - I a I a I aI o I a I - I o I a IG)l                                                       4 I 1I1I1 I 1 IG)I                   I I© 7     8   9
* LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT 58 CON'T CITTI 7 8 LlJ© I o I s I o I a I a I 2 I 1 I 2 !GI 1 I 2 I o I i I 1 I a I© I 1 I 2 I 2 I s . I 1 I s 1 G) 60 . 61 DOCKET NUMBER 6a 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES  
* LICENSEE CODE                 14         15                 LICENSE NUMBER                       25     26     LICENSE TYPE         JO   57 CAT 58 CON'T CITTI 7     8
@ . . !During normal operation, No. 12 S/G level Channel III was found to be inoperable.  
                    ~~~~~      LlJ© I o I s I oI a I aI 2 I 1 I 2 !GI 1                                     I 2 Io I i I 1 I a I© I 1 I 2 I 2 Is .I 1 I s 1G) 60   .         61                 DOCKET NUMBER               6a   69       EVENT DATE           74       75       REPORT DATE         80 EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES                                     @             .                                                   .
!]]]] !Performance Department was notified and the channel bistables were tripped as !]]]] 1required by T/S 3.3.1.1, Action 7. The channel was repaired and returned to service 09 [[]]] 112-6-78 and the Action Statement was terminated.
            !During normal operation, No. 12 S/G level Channel III was found to be inoperable.
Two other 12 S/G level channel [§]]] !redundancy was available throughout this occurrence.
  !]]]]     !Performance Department was notified and the channel bistables were tripped as
This is the first occurrence of !]]:I] !this type. -[]]]] 7 B 9 [ill] 7 B SYSTEM cooE I IIA I@ 9 10 /;:;\ l.ER!RQ LVENTYEAR REPORT I 7 I 8 I NUMBER 21 22. CAUSE CAUSE COMP. CODE suBCODE COMPONENT cooE suBCODE I.LI w@ 1r1N 1s1TIRIU1e 11 12 13 18 19 SEQUENTIAL OCCURRENCE REPORT REPORT NO. COOE TYPE I I Io I 7 I 9 I I /I I o I 3 I L1J 23 24 26 27 28 29 30 VALVE SUBCOOE 20 l.=l 31 PRIME COMP. REVISION NO. Lo.J 32 COMPONENT so oW$CJ.JT HOURS c22'i W@W@ 12J@) I 01 o I ojO I L:.J@ L::J@ ACTION FUTURE TAKEN ACTION SUPPLIER MANUFACTURER 33 34 JS 36 37 40 41 42 I Bl 0 I 8 I 0 I@ CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS @ 43 44 47 [I]]] I The level sensor failure was caused by partially clogged sensing lines. The sensing lines were blown down, the transmitter was recalibrated and the channel was returned to service. The other S/G level sensing lines were blown down to prevent reoccurrenc9
  !]]]] 1required by T/S 3.3.1.1, Action 7.                                                 The channel was repaired and returned to service                                         09
[JJ]J I of this problem. IJJII 1 a s FACILITY l3c)\ STATUS % POWER OTHER STATUS v::::J IIITJ I O I 9 I 4 l@I .... __ N-...l ...... A;;..... _ __... 1
[[]]] 112-6-78 and the Action Statement was terminated.                                                             Two other 12 S/G level channel
* a s 10 12 11 ACTIVITY CONTENT REl.EASEO OF REl.EASE AMOUNT OF ACTIVITY IJJI] lli.J @ LI.J@) I N /A 1 a s 10 11 so METHOD OF DISCOVERY DESCRIPTION
[§]]] !redundancy was available throughout this occurrence.                                                               This is the first occurrence of
@ OISCOVERY I l.!J@I 0Eerational Check 44 45 46 BO LOCATION OF REI.EASE @ NiA ** 44 45 80 PERSONNEL EXPOSURES NUMBER (.;;\TYPE DESCRIPTION
  !]]:I] !this type.
[!JI] I o I o I o
- []]]]
__ N..;..:./_A
7     B 9                                                                                                                                                                             so SYSTEM                    CAUSE        CAUSE                                                      COMP.          VALVE cooE                      CODE      suBCODE                  COMPONENT cooE                  suBCODE          SUBCOOE
______________________
[ill]
--..1 1 a s 11 12 13 PERSONNEL INJURIES f,;'<l 80 NUMBER IIli] I olol ol@)._, _______ .
7     B I IIA I@
1 0 s 11 12 80 LOSS OF OR DAMAGE TO FACILITY 1.i3' TYPE OESCRIPTION  
9             10 I.LI w@
\::;:J
11          12 1r1N 1s1TIRIU1e ~ ~@
______________________________
13                             18         19               20 SEQUENTIAL                           OCCURRENCE           REPORT                       REVISION
..;.... __________________________  
            /;:;\  l.ER!RQ LVENTYEAR                                          REPORT NO.                               COOE               TYPE                         NO.
....lao PUBLICITY C\ ISSUED I.:".;\ OESCRIPTION NAC use ON Ly IJI2] Lzje,. ___________
            ~ REPORT NUMBER I7 I 8I 21            22
N...__A _________________________
                                                    .          I 23 I      Io I 7 I 9 I 24              26 I /I 27 I oI 28 3I 29 L1J 30 l.=l 31 Lo.J 32 ACTION FUTURE                                                                                                                        PRIME COMP.            COMPONENT TAKEN ACTION                    oW$CJ.JT               s~~~~~~N                  HOURS c22'i AJJ'~~~~T            F~~~~a.          SUPPLIER            MANUFACTURER W@W@                               ~@                    12J@)         I 01 o I ojO I L:.J@                         L::J@             ~@              I Bl   0 I 8 I 0 I@
__, I I I I I II I II II J a 9 10 SB 69 eo
33          34                    JS                    36          37                      40    41              42                43              44                47 CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS                               @
__ 790l030113 PHONE: (609)365-7000 Salen Ext. 628}}
[I]]] I     The level sensor failure was caused by partially clogged sensing lines.                                                                           The sensing lines were blown down, the transmitter was recalibrated and the channel was returned to service.                   The other S/G level sensing lines were blown down to prevent reoccurrenc9
[JJ]J I       of this problem.
IJJIIa 1         s                                                                                                                                                                       so FACILITY                                                                 l3c)\       METHOD OF STATUS             % POWER                               OTHER STATUS   v::::J     OISCOVERY                            DISCOVERY DESCRIPTION          @
IIITJ     ~@              I OI 9 I 4 l@I...._ _N-...l......A;;....._ __...I l.!J@I 0Eerational Check 1
* a s                 10                 12         11                               44    45          46                                                                    BO ACTIVITY       CONTENT                                                 ~
REl.EASEO OF REl.EASE                             AMOUNT OF ACTIVITY                                                       LOCATION OF REI.EASE        @
IJJI] lli.J @ LI.J@) I                                             N /A                                                                     NiA **
1   a s                 10           11                                               44           45                                                                           80 PERSONNEL EXPOSURES                                     ~
NUMBER         (.;;\TYPE               DESCRIPTION
[!JI] I oI o I o l~W@.____N..;..:./_A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _--..1 1   a s                   11       12               13                                                                                                                           80 PERSONNEL INJURIES                         f,;'<l NUMBER               DESCRIPTION~
IIli] sI olol ol@)._,_______. ~N~A-..:-------------------------------------------i 1     0                   11       12                                                                                                                                           80 LOSS OF OR DAMAGE TO FACILITY                   1.i3' TYPE       OESCRIPTION                         \::;:J
  ~ ~(&sect;)~10:------.-------------N..._A.._______________________________..;....__________________________....lao PUBLICITY                 C\
ISSUEDI.:".;\ OESCRIPTION         ~                                                                                                                  NAC use ON Ly IJI2] Lzje,. ___________N...__A___________________________,                                                                                           I I I I I II I II II           J a   9           10                                                                                                                       SB   69                           eo NAMEOFPREPARER------A_._w_._K_a~p~p-l_e_ _~---                                                          PHONE:       (609)365-7000 Salen Ext.
790l030113                                                                                                                                                                628}}

Revision as of 16:44, 21 October 2019

LER 78-079/03L-0 on 781201:steam Generator 12,level Channel III Found to Be Inoperable;Channel Bistables Tripped Per Tech Specs.Caused by Partially Clogged Sensing Lines
ML18078A591
Person / Time
Site: Salem PSEG icon.png
Issue date: 12/28/1978
From: Kapple A
Public Service Enterprise Group
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18078A589 List:
References
LER-78-079-03L, LER-78-79-3L, NUDOCS 7901030173
Download: ML18078A591 (1)


Text

e LICENSEE EVENT REPORT U.S. NUCLEAR REGULATURY COMMISSION e

CONTROL BLOCK: !o-1_ _..._I_.__....____._....__..j 0) (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI 1 "

[§J2J IN IJ Is I G Is I 1 101 a I aI - I a I a I aI o I a I - I o I a IG)l 4 I 1I1I1 I 1 IG)I I I© 7 8 9

  • LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE JO 57 CAT 58 CON'T CITTI 7 8

~~~~~ LlJ© I o I s I oI a I aI 2 I 1 I 2 !GI 1 I 2 Io I i I 1 I a I© I 1 I 2 I 2 Is .I 1 I s 1G) 60 . 61 DOCKET NUMBER 6a 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION ANO PROBABLE CONSEQUENCES @ . .

!During normal operation, No. 12 S/G level Channel III was found to be inoperable.

!]]]] !Performance Department was notified and the channel bistables were tripped as

!]]]] 1required by T/S 3.3.1.1, Action 7. The channel was repaired and returned to service 09

[[]]] 112-6-78 and the Action Statement was terminated. Two other 12 S/G level channel

[§]]] !redundancy was available throughout this occurrence. This is the first occurrence of

!]]:I] !this type.

- []]]]

7 B 9 so SYSTEM CAUSE CAUSE COMP. VALVE cooE CODE suBCODE COMPONENT cooE suBCODE SUBCOOE

[ill]

7 B I IIA I@

9 10 I.LI w@

11 12 1r1N 1s1TIRIU1e ~ ~@

13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION

/;:;\ l.ER!RQ LVENTYEAR REPORT NO. COOE TYPE NO.

~ REPORT NUMBER I7 I 8I 21 22

. I 23 I Io I 7 I 9 I 24 26 I /I 27 I oI 28 3I 29 L1J 30 l.=l 31 Lo.J 32 ACTION FUTURE PRIME COMP. COMPONENT TAKEN ACTION oW$CJ.JT s~~~~~~N HOURS c22'i AJJ'~~~~T F~~~~a. SUPPLIER MANUFACTURER W@W@ ~@ 12J@) I 01 o I ojO I L:.J@ L::J@ ~@ I Bl 0 I 8 I 0 I@

33 34 JS 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION ANO CORRECTIVE ACTIONS @

[I]]] I The level sensor failure was caused by partially clogged sensing lines. The sensing lines were blown down, the transmitter was recalibrated and the channel was returned to service. The other S/G level sensing lines were blown down to prevent reoccurrenc9

[JJ]J I of this problem.

IJJIIa 1 s so FACILITY l3c)\ METHOD OF STATUS  % POWER OTHER STATUS v::::J OISCOVERY DISCOVERY DESCRIPTION @

IIITJ ~@ I OI 9 I 4 l@I...._ _N-...l......A;;....._ __...I l.!J@I 0Eerational Check 1

  • a s 10 12 11 44 45 46 BO ACTIVITY CONTENT ~

REl.EASEO OF REl.EASE AMOUNT OF ACTIVITY LOCATION OF REI.EASE @

IJJI] lli.J @ LI.J@) I N /A NiA **

1 a s 10 11 44 45 80 PERSONNEL EXPOSURES ~

NUMBER (.;;\TYPE DESCRIPTION

[!JI] I oI o I o l~W@.____N..;..:./_A_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _--..1 1 a s 11 12 13 80 PERSONNEL INJURIES f,;'<l NUMBER DESCRIPTION~

IIli] sI olol ol@)._,_______. ~N~A-..:-------------------------------------------i 1 0 11 12 80 LOSS OF OR DAMAGE TO FACILITY 1.i3' TYPE OESCRIPTION \::;:J

~ ~(§)~10:------.-------------N..._A.._______________________________..;....__________________________....lao PUBLICITY C\

ISSUEDI.:".;\ OESCRIPTION ~ NAC use ON Ly IJI2] Lzje,. ___________N...__A___________________________, I I I I I II I II II J a 9 10 SB 69 eo NAMEOFPREPARER------A_._w_._K_a~p~p-l_e_ _~--- PHONE: (609)365-7000 Salen Ext.

790l030113 628