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| SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 91-038-00 January 16, 1992 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations lOCFR 50.73(a) (2) (ii). This report is required to be issued within thirty (30) days of event discovery. | | SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 91-038-00 January 16, 1992 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations lOCFR 50.73(a) (2) (ii). This report is required to be issued within thirty (30) days of event discovery. |
| MJP:pc Distribution The Energy People_ 9201280186 920116 PDR ADOCK 05000272 S PDR Sine ely yours, C. A Vondra General Manager -Salem Operations 95-2189 (10M) 12-89 | | MJP:pc Distribution The Energy People_ 9201280186 920116 PDR ADOCK 05000272 S PDR Sine ely yours, C. A Vondra General Manager -Salem Operations 95-2189 (10M) 12-89 |
| ., NRC FORM366 (6.S9l U.S. NUCLEAR REGULATORY COMMISSION | | ., NRC FORM366 (6.S9l U.S. NUCLEAR REGULATORY COMMISSION |
| :APPROVEO OMB NO. J150_-0104 EXPIRES: 4/30/92 , , LICENSEE EVENT REPORT (LERI '* FACILITY NAME (11 Salem Generating Station_-Unit 1 *ESTIMATED BURDEN i>*ER RESPONSE .TD COMP.LY WTH. THls INFORMATION | | :APPROVEO OMB NO. J150_-0104 EXPIRES: 4/30/92 , , LICENSEE EVENT REPORT (LERI '* FACILITY NAME (11 Salem Generating Station_-Unit 1 *ESTIMATED BURDEN i>*ER RESPONSE .TD COMP.LY WTH. THls INFORMATION |
| 'COLLECTION REQUEST: 50.0 -HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO*THE RECORDS . AND REPORTS MANAGEMENT BRANCH (P-630l;U.S. | | 'COLLECTION REQUEST: 50.0 -HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO*THE RECORDS . AND REPORTS MANAGEMENT BRANCH (P-630l;U.S. |
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| ' PLANT AND SYSTEM IDENTIFICATION: | | ' PLANT AND SYSTEM IDENTIFICATION: |
| .. Pressurized | | .. Pressurized |
| .. *,, .-* -. "*-:*, .... , .. .. . .. Energy Industry Identification-System_. (EilS) codes are -identified in the teXt as. ( xX I .; . IDENTIFICATION OF.OCCURRENCE: . _-.: ... -_.,...:. ..... . . '. -_. . ' . --Control Room habitability | | .. *,, .-* -. "*-:*, .... , .. .. . .. Energy Industry Identification-System_. (EilS) codes are -identified in the teXt as. ( xX I .; . IDENTIFICATION OF.OCCURRENCE: . _-.: ... -_.,...:. ..... . . '. -_. . ' . --Control Room habitability |
| :concjern from .postulated | | :concjern from .postulated |
| ,.t*iydroxide release Discovery Date: *12/19/9i | | ,.t*iydroxide release Discovery Date: *12/19/9i |
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| The analysis was prepared by Stone & Webster Engineering Corporation (SWEC) using the "VAPOR" computer program. Ammonium hydroxide is used to maintain_ | | The analysis was prepared by Stone & Webster Engineering Corporation (SWEC) using the "VAPOR" computer program. Ammonium hydroxide is used to maintain_ |
| secondary plant pH control (i.e., Chemical Feed System [KDJ). In accordance with Regulatory Guide 1.78, the maximum concentration release was postulated from a catastrophic failure of the largest storage tank of ammonium hydroxide (27.5 wt%). The liquid ammonium hydroxide would vaporize to ammonia upon release, exhaust to the environment (from the Turbine Building Ventilation System), and disperse to the Control Room air supply intakes. The VAPOR calculation indicated that the Regulatory Guide 1.78 toxic limit for ammonia (100 ppm) would be exceeded. | | secondary plant pH control (i.e., Chemical Feed System [KDJ). In accordance with Regulatory Guide 1.78, the maximum concentration release was postulated from a catastrophic failure of the largest storage tank of ammonium hydroxide (27.5 wt%). The liquid ammonium hydroxide would vaporize to ammonia upon release, exhaust to the environment (from the Turbine Building Ventilation System), and disperse to the Control Room air supply intakes. The VAPOR calculation indicated that the Regulatory Guide 1.78 toxic limit for ammonia (100 ppm) would be exceeded. |
| On December 19, 1991, at 1530 hours, the Nuclear Regulatory Commission (NRC) was notified in accordance with Code of Federal Regulations 10CFR50.72(b) | | On December 19, 1991, at 1530 hours, the Nuclear Regulatory Commission (NRC) was notified in accordance with Code of Federal Regulations 10CFR50.72(b) |
| (1) (ii). An ammonium hydroxide habitability concern was first identified by an NRC inspector on September 9, 1991 (reference NRC Inspection Report 50-272/91-25, dated September 26, 1991). A preliminary assessment was conducted using the "CHARM" computer program, developed by Radian Corporation. | | (1) (ii). An ammonium hydroxide habitability concern was first identified by an NRC inspector on September 9, 1991 (reference NRC Inspection Report 50-272/91-25, dated September 26, 1991). A preliminary assessment was conducted using the "CHARM" computer program, developed by Radian Corporation. |
| From the preliminary assessment, PSE&G concluded that no significant safety concern would exist; however, to support this conclusion, a more detailed computer program (VAPOR) was used. VAPOR identified a safety concern as discussed above. Additional discussion is contained in the Analysis of Occurrence section. | | From the preliminary assessment, PSE&G concluded that no significant safety concern would exist; however, to support this conclusion, a more detailed computer program (VAPOR) was used. VAPOR identified a safety concern as discussed above. Additional discussion is contained in the Analysis of Occurrence section. |
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| on the s'tored -*hazardous chemical (UFSAR Section 2 ._2) . . UFSAR Section 6. 4, : does not address. ammonium :hydroxide impact on.control room habitability. | | on the s'tored -*hazardous chemical (UFSAR Section 2 ._2) . . UFSAR Section 6. 4, : does not address. ammonium :hydroxide impact on.control room habitability. |
| The AEC 'standard format (dated 1966) did-not contain a section requiring discussfons of.*coritrol room habitability | | The AEC 'standard format (dated 1966) did-not contain a section requiring discussfons of.*coritrol room habitability |
| *. During the Unit 2 FSAR .. review. (to support._Unit 2 licensing) r "NRc Question. | | *. During the Unit 2 FSAR .. review. (to support._Unit 2 licensing) r "NRc Question. |
| : 9. 60. did ask .how Salem Is . design complied with Guide 1. 78; bu:t it *was -asked relat:'J .. ve to offsite r1ver. accidents | | : 9. 60. did ask .how Salem Is . design complied with Guide 1. 78; bu:t it *was -asked relat:'J .. ve to offsite r1ver. accidents |
| *.. ---_;-. -. . <**': . --.-; . ' . . -,_. When the concern was first .in September | | *.. ---_;-. -. . <**': . --.-; . ' . . -,_. When the concern was first .in September |
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| on *the. same sit.e as Salem Generating Station, was notified .*bf the -Salem Contro1-: 0:Room habitability concern for potential impact at Hope Creek Geperating | | on *the. same sit.e as Salem Generating Station, was notified .*bf the -Salem Contro1-: 0:Room habitability concern for potential impact at Hope Creek Geperating |
| *. Station. CORRECTIVE ACTION .. *_: The following compensatory actions were* taken t:o .controi room habitability under postulated accident conditions (per VAPOR) : . . . . :*. , 1. A temperature indicator with placed. in the proximity of the storage vessel to -mC:>nitor temperature in the tank area. Aiitmonia i;-elease is. te:mperature depe.ndent 27.5 wt% ammonium hydroxide solution.has a boiling point of 82° F) ... 2. The maximlim allowable storage volumes for 27.5 wt% ammonium hydroxide were determined for-temperatures up to 75°F and transmitted to the Salem Operations and Chemistry.. | | *. Station. CORRECTIVE ACTION .. *_: The following compensatory actions were* taken t:o .controi room habitability under postulated accident conditions (per VAPOR) : . . . . :*. , 1. A temperature indicator with placed. in the proximity of the storage vessel to -mC:>nitor temperature in the tank area. Aiitmonia i;-elease is. te:mperature depe.ndent 27.5 wt% ammonium hydroxide solution.has a boiling point of 82° F) ... 2. The maximlim allowable storage volumes for 27.5 wt% ammonium hydroxide were determined for-temperatures up to 75°F and transmitted to the Salem Operations and Chemistry.. |
| -departments. | | -departments. |
| : 3. Precautionary administrative controls, for ta_nker. truck delivery, have been initiated. | | : 3. Precautionary administrative controls, for ta_nker. truck delivery, have been initiated. |
| They will be *detailed in a revision to Chemistry procedure* | | They will be *detailed in a revision to Chemistry procedure* |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
Text
e Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555
Dear Sir:
SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 LICENSEE EVENT REPORT 91-038-00 January 16, 1992 This Licensee Event Report is being submitted pursuant to the requirements of the Code of Federal Regulations lOCFR 50.73(a) (2) (ii). This report is required to be issued within thirty (30) days of event discovery.
MJP:pc Distribution The Energy People_ 9201280186 920116 PDR ADOCK 05000272 S PDR Sine ely yours, C. A Vondra General Manager -Salem Operations 95-2189 (10M) 12-89
., NRC FORM366 (6.S9l U.S. NUCLEAR REGULATORY COMMISSION
- APPROVEO OMB NO. J150_-0104 EXPIRES: 4/30/92 , , LICENSEE EVENT REPORT (LERI '* FACILITY NAME (11 Salem Generating Station_-Unit 1 *ESTIMATED BURDEN i>*ER RESPONSE .TD COMP.LY WTH. THls INFORMATION
'COLLECTION REQUEST: 50.0 -HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO*THE RECORDS . AND REPORTS MANAGEMENT BRANCH (P-630l;U.S.
NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 'THE PAPERWORK
- REDUCTION PROJECT (3150-01041, OFFICE OF MANAGEMENT AND BUDG_ET, WASHINGTON; DC 20503. * !DOCKET NUMBER .(21
- I .PAGE (31 . 0 I 5 'i 0 I 0 I 0 12 17 12 1 I OF 0 5 TITLE (41 Control Habitabjlity Concern From Postulated Ammonium Hydroxide Release EVENT DATE _(61 LER NUMBER 161 " REPORT DATE 171 OTHER FACILITIES INVOLVED ,Ill MONTH DAY YEAR YEAR tl tl MONTH . DAY YEAR FACILITY NAMES DOCKET NUMBERISI . . o I 51 O .I O j O t3 I 11 1 Salem Unit *2 .* O 1S10-10101 I I OPERATING MODE (Ill l THIS REPORT IS SUBMITTED PURSUANT TD THE OF 10 CFR §: (Ch<<k ono or mor0 of tho_ foilowin11J (111 20.402(bl 20.405lcl 60.731all2lli*I 73.71(bl POWER l LEVEL l I Q
- Q _,..,. 1101 I *" -*--20.4051*111 IUI 60.38(cll11 60.731all21M 73.711cl ---20.4051*11111111 60.381cll21 60.731all21Mil OTHER (Spocify in Abrtroct -IHlow *nd In T*xt. NRC Form --20.40lll*ll1 lliill 60.731*1121111 60.73(allZIMllllAI 366AJ --20.406i*ll1 lllvl x 60.73(*112lliil 60.731oll21Cvllll IBI --20.4061*1111 M 60.731*112lliiil
&0.731*112lhil LICENSEE CONTACT FOR THIS LER 1121 NAME TELEPHONE NUMBER M. Pollack -*LER Coordinator 6 I 01 9 3 I 31 9 I-I 2 I 0 I 21 2 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 1131 CAUSE SYSTEM COMPONENT I I I I I I I I MANUFAC* TUR ER *I* I I I I I SUPPLEMENTAL REPORT EXPECTED 1141 rl YES (If yor, comploto EXPECTED SUBMISSION DATE/ ABSTRACT (Limit ta 1400 ipact11. I.* .* *pproitim*r.ly fiftHn 1inglt1-1pace limn} 118) COMPONENT I I I I I I MANUFAC* TUR ER I I I . 1
- I I EXPECTED SUBMISSION DATE 1151 MONTH _DAY YEA I I I On 12/19/91, an interim calculation concluded tha*t a Control Room habitability concern was possible, to postulated failure of a 300Q gallon capacity Turbine Building ammonium hydroxide storage tank. In accordance with Regulatory Guide 1.78, the maximum*concentration release was postulated from a catastrophic failure of the largest storage tank of ammonium hydroxide (27.5 wt%). The liquid ammonium hydroxide would vaporize to ammonia upon release, exhaust to the environment (from the Turbine Building Ventilation System), and disperse to the Control Room air supply intakes. Calculations indicate that the Regulatory Guide 1.78 toxic limit for ammonia (100 ppm) would be exceeded.
The root cause of this event is attributed to inadequate design review during the preparation of the Final Safety Analysis Report (FSAR). Compensatory actions have been taken to ensure control room habitability under postulated accident conditions including the addition of a temperature indicator with chart recorder by the storage vessel and administrative controls for ammonium hydroxide tanker receipt. A survey for additional hazardous chemical on-site storage concerns was conducted.
An Engineering Evaluation, including a 10CFR50.59 Safety Evaluation, will be completed to address the ammonium hydroxide and any other applicable hazardous chemical issues. The UFSAR will be updated as applicable.
Evaluations will be completed of the chemical control program and procedures.
NRC Form 366 16-891
,.. , -. LICENSEE EVENT REPORT* (LER) TEXT CONTINUATION
,, ' :. -. z**-....... -
-'--. -.. -'--'--*_ . .... Salem Generating Station DOCKET NuMBER *LER NUMBER Unit 1 . _____ 5_0 __
__ _ *.PAGE *
' PLANT AND SYSTEM IDENTIFICATION:
.. Pressurized
.. *,, .-* -. "*-:*, .... , .. .. . .. Energy Industry Identification-System_. (EilS) codes are -identified in the teXt as. ( xX I .; . IDENTIFICATION OF.OCCURRENCE: . _-.: ... -_.,...:. ..... . . '. -_. . ' . --Control Room habitability
- concjern from .postulated
,.t*iydroxide release Discovery Date: *12/19/9i
-. --: .. -, : '-* Report Date: 1/16/92 This report was initiated by Incident No.* ..
- CONDITIONS PRIOR TO Unit 1: Unit 2: Mode 1 Reactor Power.100%
-Unit* Load 1158 Mwe* Defueled -6th Refueling in progress On December 19, 1991, an interim calculation concluded that a Control Room.habitability concern was possible due, to postulated failure of a 3000 gallon capacity ammonium hydroxide storage tank (1CrE24), located on 120' El. Unit 1 Turbine Building.
The analysis was prepared by Stone & Webster Engineering Corporation (SWEC) using the "VAPOR" computer program. Ammonium hydroxide is used to maintain_
secondary plant pH control (i.e., Chemical Feed System [KDJ). In accordance with Regulatory Guide 1.78, the maximum concentration release was postulated from a catastrophic failure of the largest storage tank of ammonium hydroxide (27.5 wt%). The liquid ammonium hydroxide would vaporize to ammonia upon release, exhaust to the environment (from the Turbine Building Ventilation System), and disperse to the Control Room air supply intakes. The VAPOR calculation indicated that the Regulatory Guide 1.78 toxic limit for ammonia (100 ppm) would be exceeded.
On December 19, 1991, at 1530 hours0.0177 days <br />0.425 hours <br />0.00253 weeks <br />5.82165e-4 months <br />, the Nuclear Regulatory Commission (NRC) was notified in accordance with Code of Federal Regulations 10CFR50.72(b)
(1) (ii). An ammonium hydroxide habitability concern was first identified by an NRC inspector on September 9, 1991 (reference NRC Inspection Report 50-272/91-25, dated September 26, 1991). A preliminary assessment was conducted using the "CHARM" computer program, developed by Radian Corporation.
From the preliminary assessment, PSE&G concluded that no significant safety concern would exist; however, to support this conclusion, a more detailed computer program (VAPOR) was used. VAPOR identified a safety concern as discussed above. Additional discussion is contained in the Analysis of Occurrence section.
- , LICENS.EE EVENT REPORT (LER) _TEXT CONTINUATION*
__ --Salem Generating Station Unit 1 APPARENT CAUSE-OF OCC'(}RRENCE DOCKET NUMBER LE;R NUMBER.
________
6 __ The root c_ause _ofc this event. is :attributed to _inadE!quate-dej;ign _ review. The original design identified-the current storage used for secondary water chemistry control as containing morpholine.
Prior*to issuance of an operating iicense, secondary water treatment was changed*and the tank designated to store ammonium-hydroxide.
Review of licensing basis documents indicate that FSAR Section io.2.1.6, Chemical Feed_ System discusses -morpholine for pH *con_trol.
FSAR Figure 10. 2-9, Feedwater Chemical Treatmen_t Sys'tem identifies the storage tank for H6wever, a side note states the system is designed for use of either.Ammonia or Morpholine.<
FSAR Section 10.2.1.6 and Figure 10.-2-9 were revised by Amendment
-37 dated April 5, 1976. No discussion of control room habitability for ammonium hydroxide was* included in the FSAR. Discussions involve other hazardous chemicals, airborne radiation, smoke and fir_e. -Further research identified the tank's vendor drawing which-shows it was revised from morpholine to ammonium hydroxide in April 1971. Morpholine is less_ toxic than ammonia and has a higher boiling point. Morpholine and ammonium hydroxide are not specifically listed in Regulatory Guide 1.78. -Additionally, the original FSAR was developed
- in-accordance -with the June 30, 1966 AEC Guide for the Organization and Contents of Safety Analysis Reports and AEC General Design Criteria dated July 10, 1967. These documents did not require review and-evaluation of site hazards to the degree required after Salem was licensed.
The FSAR made no commitment to Regulatory Guide 1.78 dated June 1974, but did evaluate the effects from accidents involving potential hazardous materials stored on-site a*s a result of FSAR Review Question 2.11. During the licensing of Unit 2 the response to FSAR Review Question 9.60 and NUREG-0737 TMI Action Item III.D.3.4 stated that plant and site were evaluated for compliance with Regulatory 1.78 and Standard Review Plan Sections 2.2 and 6.4. An internal engineering memorandum (Engineering memo dated September 14, 1977) addresses a preliminary judgement for compliance with Regulatory Guide 1.78. It specifically addresses ammonium hydroxide being stored in sufficient quantities to be a potential concern; however, the memo states, "there should be little problem in maintaining a habitable environment in the Salem Unit 2 Control Room following a postulated hazardous chemical release".
This conclusion was based on, "our ability to meet the intent of Control Room ventilation design with respect to 10CFR50 Apnendix A Design Criteria 19". Documentation has not been found which identifies the specific characteristics of ammonium hydroxide and its as-built storage conditions in relation to the Engineering memo's conclusions.
The preliminary assessment, conducted in September 1991, supported the conclusion that the Control Room habitability would not be impacted upon failure of the ammonium hydroxide storage tank. However, this assessment was considered preliminary and a more
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Salem Generating Station Unit 1 DOCKET NUMBER -LER NUMBER *PAGE 5Q_Q_Q 21
__ _ APPARENT CAUSE OF OCCURRENCE: (cont'd) detailed analysis.
would be required.
As -*a result of the-. December -'199]_ subsequent analysis it was that toxic :limits' could be exceeded * . ANALYSIS .OF-OCCURRENCE . . -In July 1980, a review and evaluation of the plant and site was -conducted per NUREG-0737 Action Item .III.D. 3. 4. The -Action Item required identification of potential material and a_ determination that the-control room was *adequately protected., The review the control room was.adequately protected sinc*e* *11 no cheniical . hazards: exist-" -based on previous*.
- responses to NRC inquiries. Updated Final *safety Analysis Report. (UFSAR) not include hydroxide.
on the s'tored -*hazardous chemical (UFSAR Section 2 ._2) . . UFSAR Section 6. 4, : does not address. ammonium :hydroxide impact on.control room habitability.
The AEC 'standard format (dated 1966) did-not contain a section requiring discussfons of.*coritrol room habitability
- . During the Unit 2 FSAR .. review. (to support._Unit 2 licensing) r "NRc Question.
- 9. 60. did ask .how Salem Is . design complied with Guide 1. 78; bu:t it *was -asked relat:'J .. ve to offsite r1ver. accidents
- .. ---_;-. -. . <**': . --.-; . ' . . -,_. When the concern was first .in September
This assessment involved the use of the :"CHARM" computer program.
- Results i_ndi.cated that the toxic limit for ammonia gas, listed in Regulatory guide 1.78, woutd not be exceeded.
The CHARM computer program methodology is based on an Agency (EPA) accepted model. The program model takes into accourit varying dispersive phenomena, release scenarios and the chemical's physical characteristics.
- A second assessment was contracted in which the VAPOR computer program was used. VAPOR is based on the methodology presented in NUREG-0570 dated June 1979 which utilizes ve_ry conservative assumptions.
The VAPOR program determined that the two (2) minute toxic limit of Regulatory Guide 1.78 could be exceeded and render the control room uninhabitable.
UFSAR and licensing correspondence contain no commitment nor any analysis performed by PSE&G for ammonium hydroxide release using NUREG-0570 methodology.
Also, the NRC did not review the acceptability of Salem's design using the methodology of NUREG-0570.
The Safety Evaluation Reports and their supplements do not reference this document.
Comparison of the VAPOR and CHARM models identified differences in approaches to heat transfer, mass transfer, and atmospheric modeling.
The VAPOR program is being reviewed and will be verified.
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Salem Generating_Station Unit 1 ANALYSIS OF OCCURRENCE:
DOCKET NUMBER *LER NUMBER PAGE 5b00272 5 of 6 ------*-----4-----
-. (cont'd) Hope Creek. Generating Stat.ion, locatt3d.
on *the. same sit.e as Salem Generating Station, was notified .*bf the -Salem Contro1-: 0:Room habitability concern for potential impact at Hope Creek Geperating
- . Station. CORRECTIVE ACTION .. *_: The following compensatory actions were* taken t:o .controi room habitability under postulated accident conditions (per VAPOR) : . . . . :*. , 1. A temperature indicator with placed. in the proximity of the storage vessel to -mC:>nitor temperature in the tank area. Aiitmonia i;-elease is. te:mperature depe.ndent 27.5 wt% ammonium hydroxide solution.has a boiling point of 82° F) ... 2. The maximlim allowable storage volumes for 27.5 wt% ammonium hydroxide were determined for-temperatures up to 75°F and transmitted to the Salem Operations and Chemistry..
-departments.
- 3. Precautionary administrative controls, for ta_nker. truck delivery, have been initiated.
They will be *detailed in a revision to Chemistry procedure*
- 'Receipt of Ammonium Hydroxide Tank Trucks". A survey for additional hazardous chem1cal on-site* storage concerns was conducted.
Results identified two (2) additional.chemicals with the potential to impact Control Room They are 35 wt% hydrazine (stored in a 300 gallon vessel on 120'-El. Unit 1 Turbine Building) and 50 wt% sodium hydroxide whose largest' single container is one of the two (2) 4000 gallon tanks located on 88' El. Unit 1 Turbine Building.
Preliminary assessment indicates an impact on Control Room habitability is not expected upon release of these two (2) chemicals.
This assessment will be finalized using the VAPOR program. An Engineering Evaluation, including a 10CFR50.59 Safety Evaluation, will be completed to address the following ammonium hydroxide issues. 1. The final VAPOR program calculation review; 2. A determination of whether 15 wt% ammonium hydroxide can be used, instead of 27.5 wt%; and 3. An evaluation for design modifications to correct Control Room habitability concerns.
The UFSAR will be updated to include ammonium hydroxide as a potential accident hazard along with any other chemicals identified.
Evaluations will be completed of the chemical control program and
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___ . -*-*--* f?_ .-'?t __ .§_ __ CORRECTIVE ACTION procedures to identify programmatic/procedure revisions or development of new procedures to ensure evaluation of chemicals for their impact on control room habitability.
MJP:pc SORC Mtg.92-007 General Manager -Salem Operations