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Line 39: |
Line 39: |
| Calorimetric (Heat Balance) Calculations Not Performed Within The specif Surveillance Interval On Both Units ' . Event Dates: (Unit 2) 1/8/94, 7/5/94, 7/8/94, 9/12/94, and 10/13/94 (Unit 1) 2/26/94, 3/5/94, arid 9/2/94 Discovery Date: 10/13/94 Report Date: | | Calorimetric (Heat Balance) Calculations Not Performed Within The specif Surveillance Interval On Both Units ' . Event Dates: (Unit 2) 1/8/94, 7/5/94, 7/8/94, 9/12/94, and 10/13/94 (Unit 1) 2/26/94, 3/5/94, arid 9/2/94 Discovery Date: 10/13/94 Report Date: |
| * 11/14/94 This report was initiated by Incident Report No. 94-304. DESCRIPTION OF OCCURRENCES: | | * 11/14/94 This report was initiated by Incident Report No. 94-304. DESCRIPTION OF OCCURRENCES: |
| At approximately 0951 on October 12, 1994, the requirements of Technical Specification (TS) Tabl.e 4. 3-1, Item 2, for daily calibration of power range instrumentation | | At approximately 0951 on October 12, 1994, the requirements of Technical Specification (TS) Tabl.e 4. 3-1, Item 2, for daily calibration of power range instrumentation |
| {IG} when above 15% of RATED THERMAL POWER, were met through satisfactory completion of the caloriinetric (heat balance-) | | {IG} when above 15% of RATED THERMAL POWER, were met through satisfactory completion of the caloriinetric (heat balance-) |
| calculation. | | calculation. |
Line 53: |
Line 53: |
| between the prior NIS calibration and when RTP was 15%. Other instances occurred on both Units where the maximum allowable extension for the required NIS power range calibration was exceeded; Unit' 2*-two hours, 55 minutes; five hours,* 25 minutes; six hours, 19 minutes; and eight hours, 14 minutes; and Unit 1 -two hours, 42 minutes; 9 minutes; and three hours. APPARENT CAUSE OF OCCURRENCES: | | between the prior NIS calibration and when RTP was 15%. Other instances occurred on both Units where the maximum allowable extension for the required NIS power range calibration was exceeded; Unit' 2*-two hours, 55 minutes; five hours,* 25 minutes; six hours, 19 minutes; and eight hours, 14 minutes; and Unit 1 -two hours, 42 minutes; 9 minutes; and three hours. APPARENT CAUSE OF OCCURRENCES: |
| These events are attributed to "Personnel Error", as classified in Appendix B of NUREG_-1022. | | These events are attributed to "Personnel Error", as classified in Appendix B of NUREG_-1022. |
| The event of October 13, 1994 resulted from failure of the Nuclear Control Operator (NCO) to follow procedure | | The event of October 13, 1994 resulted from failure of the Nuclear Control Operator (NCO) to follow procedure |
| [Step 5.16 of SC.OP-DD.ZZ-OD40(Z)] | | [Step 5.16 of SC.OP-DD.ZZ-OD40(Z)] |
| combined with failure of the Nuclear Shift Supervisor (NSS) to adequately review the completed shift routines. | | combined with failure of the Nuclear Shift Supervisor (NSS) to adequately review the completed shift routines. |
Line 64: |
Line 64: |
| * which did not permit the required stable conditions to.allow* | | * which did not permit the required stable conditions to.allow* |
| completion of the surveillance. | | completion of the surveillance. |
| Corrective action included an Operations Night Order Book {NOB) entry on 1/28/78, instructing the Senior Nuclear Shift Supervisor | | Corrective action included an Operations Night Order Book {NOB) entry on 1/28/78, instructing the Senior Nuclear Shift Supervisor |
| {SNSS) of the necessity to perform the _surveillance. | | {SNSS) of the necessity to perform the _surveillance. |
| This NOB entry directed the SNSS to stop a load change, if required, to permit completion of the surveillanc.e within th_e required till\e frame. SAFETY SIGNIFICANCE: | | This NOB entry directed the SNSS to stop a load change, if required, to permit completion of the surveillanc.e within th_e required till\e frame. SAFETY SIGNIFICANCE: |
| These events are reportable pursuant to 10CFR50.73{a) | | These events are reportable pursuant to 10CFR50.73{a) |
| (2) (i) (B), due to failure to comply with the Limiting Condition For Operation requirements of TS Table 4.3-1, as well as TS 3.0.2, due to failure to perform the surveillance requirements within the.maximum allowable extension. | | (2) (i) (B), due to failure to comply with the Limiting Condition For Operation requirements of TS Table 4.3-1, as well as TS 3.0.2, due to failure to perform the surveillance requirements within the.maximum allowable extension. |
| The safety signif of October 13 event is minimal as the approximate six hours 53 minutes the Unit operated until the requirements of TS no longer applied (i.e. entry into.MODE | | The safety signif of October 13 event is minimal as the approximate six hours 53 minutes the Unit operated until the requirements of TS no longer applied (i.e. entry into.MODE |
| : 3) is bounded by the requirements of TS 3.0.3.. The safety significance of the other occurrences is minimal based upon satisfactory completion of the surveillance following each event. In addition, in accordance with procedure, reaqtor power is maintained less than 100% and verified by an on-line calorimetric computer readout. The inputs to the on-line calorimetric computer readout are the same as the manual surveillance calculation. | | : 3) is bounded by the requirements of TS 3.0.3.. The safety significance of the other occurrences is minimal based upon satisfactory completion of the surveillance following each event. In addition, in accordance with procedure, reaqtor power is maintained less than 100% and verified by an on-line calorimetric computer readout. The inputs to the on-line calorimetric computer readout are the same as the manual surveillance calculation. |
| CORRECTIVE ACTION: All Licensed personnel involved in the October 13 event have been counseled concerning their *actions and Management expectations regarding procedure compliance. | | CORRECTIVE ACTION: All Licensed personnel involved in the October 13 event have been counseled concerning their *actions and Management expectations regarding procedure compliance. |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
[Table view] |
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_;... p,., }t' \:) . e Public Service Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038 Salem Generating Station U. S. Nuclear Regulatory Cormnission Document Control Desk Washington, DC 20555 Attn.: Document Control Desk SALEM GENERATING STATION LICENSE NO. DPR-75 DOCKET NO. 50-311 UNIT NO. 2 LICENSEE EVENT REPORT NO. 94-012-00 November 14, 1994 This Licensee Event Report is being submitted pursuant to the requirements of Code of Federal Regulation 10CFR50. 73 (a) (2) (i) (B). Issuance of this report is required within thirty (30) days of event discovery.
Sincerely, MJPJ:vs C -Distribution LER File 9411210395 941114 PDR ADDCK 05000311 {p?) / S PDR l he power in y1JUT han.3-. 95-2189 REV 7-92 NRC FORM 366 (5-92) .S. NUCLl;AR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104
-. EXPIRES 5/31/95 LICENSEE EVENT REPORT (LER) (See reverse for required number of digits/characters for each block) ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH (MNBB 7714), U.S. NUCLEAR REGULATORY .COMMISSION, .WASHINGTON, De 20555*0001, AND TO THE PAPERWORK REDUCTION .PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, DC 20503. FACILITY NAME (1) DOCKET NUMBER (2) PAGE (31 1 OF05 Salem Generating Station Unit 2 05000 311 TtTLE(4) La.LOrimer:ric
\,Heat tlal.anceJ .L;al.cul.at.ions Not Performed Within the Specified Surveillance Interval On Both Units -. EVENT DATE (5) LEA NUMBER (6 REPORT NUMBER '71 OTHER FACILITIES INVOLVED (8 SEQUENTIAL MONTH DAY YEAR NUMBER 10 13 94 94 012 REVISION NUMBER 00 MONTH ' 11 .VEAR 14 . 94 FACILITY NAME DOCKET NUMBER Salem Unit 1 05000?72 FACILITY NAME DOCKET NUMBER 05000 OPERATING 1 THIS REPORT IS SUBMITTED PURSUANT TO'THE REQUIREMENTS OF 10 CFR §: {Check one or more (11 MODE (9) 20.402(b) 20.405{c) 50.73{a)(2)(iv) 73.71 (b) POWER 100% 20.405(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.71 (c) LEVEL (10) 20.405(a)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vii)
OTHER -. 20.405(a)(1)(iii) 50.73(a)(2)(i) 50.73(a)(2)(viii)(A) (Specify in Abstract n-+--.:....:....:...:...,:.....:._
__ ___; __ 4.......-1--__:_..:....:....:..:_:,.----__,.+_,...+--:....:_:...:.,:__:_::_.:_---t below and in Text, NRC
X 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B)
Form 366A) ,,,.,. 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LEA (12\ NAME Michael J. Pastva -LER Coordinator TELEPHONE NUMBER (Include Area Code) 609 339-5165 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13\ CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TONPRDS SUPPLEMENTAL REPORT EXPECTED (14\ EXPECTED MONTH DAY YEAR I YES X NO . . (If yes, complete EXPECTED SUBMISSION DATE) SUBMISSION DATE (15) _ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16) On 10/13/94, required daily calibration of power range instrumentation was not performed.
Investigation revealed that during 1994 qn 1/8,, 7/5, 7/8, and 9/12 (Unit 2), and 2/26, 3/5, and 9/2 (Unit 1), the calibration was performed beyond the allowable.extension Technical Specification (TS) 4.0.2. These events are attributed to personnel error due to failure to follow procedure.
contributors to the 10/13 event were focus upon ongoing activities and common mis-perception (applicable to all the events) that the surveillance could be completed within 'the confines of a calendar day. Licensed personnel from the 10/13 event were counseled concerning their actions and Management expectations.
Operations Night Order Book entries were made to explain* the surveillance requirement and a procedure revision to enhance/clarify the surveillance interval.
All Licensed personnel and select Technical Department personnel, will review these events to ensure their understanding of the surveillance,interval.
During the present re-qualification cycle, all licensed personnel will receive
- training specific to these events. By additional procedure enhancement will be made to provide more focus on TS requirements and address human factors tied to procedure performance and review. NRC FORM 366 (5*92) e REQUIRED OF DIGITS/CHARACTE.
FOR EACH BLOCK -BLOCK NUMBER OF NUMBER DIGITS/CHARACTERS TITLE ' 1 UP TO 46 FACILITY NAME 2 8 TOTAL 3 IN ADDITION TO 05000 DOCKET NUMBER 3 VARIES PAGE NUMBER 4 UP TO 76 TITLE 5 6 TOTAL 2 PER BLOCK EVENT DATE 7 TOTAL 6 2 FOR YEAR 3 FOR SEQUENTIAL NUMBER LER NUMBER _ 2 FOR REVISION NUMBER 7 6 TOTAL 2 PER BLOCK REPORT DATE UP TO 18 -FACILITY NAME 8 8 TOTAL -DOCKET NUMBER OTHER FACILITIES INVOLVED 3 IN ADDITION TO 05000 9 1 OPERATING MODE 10 3 POWER LEVEL 11 1 CHECK BOX THAT APPLIES REQUIREMENTS OF 10 CFR 12 UP TO 50 FOR NAME 14 FOR TELEPHONE LICENSEE CONT ACT CAUSE VARIES 2 FOR SYSTEM 13 4 FOR COMPONENT EACH COMPONENT FAILURE 4 FOR MANUFACTURER
' NPRDS VARIES 14 , CHECK BOX THAT APPLIES -SUPPLEMENTAL REPORT EXPECTED 15 6 TOTAL 2 PER BLOCK EXPECTED SUBMISSION DATE
,* LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating Station Unit 2 DOCKET NUMBER 5000311 PLANT AND SYSTEM IDENTIFICATION:.
Westinghouse
-Pressurized Water Reactor LER NUMBER* 94-012-00 PAGE 2 of 5 Energy Industry Identification System (EIIS) codes are identified in the text as {xx} IDENTIFICATION OF OCCURRENCES:
Calorimetric (Heat Balance) Calculations Not Performed Within The specif Surveillance Interval On Both Units ' . Event Dates: (Unit 2) 1/8/94, 7/5/94, 7/8/94, 9/12/94, and 10/13/94 (Unit 1) 2/26/94, 3/5/94, arid 9/2/94 Discovery Date: 10/13/94 Report Date:
- 11/14/94 This report was initiated by Incident Report No.94-304. DESCRIPTION OF OCCURRENCES:
At approximately 0951 on October 12, 1994, the requirements of Technical Specification (TS) Tabl.e 4. 3-1, Item 2, for daily calibration of power range instrumentation
{IG} when above 15% of RATED THERMAL POWER, were met through satisfactory completion of the caloriinetric (heat balance-)
calculation.
At 0530 hours0.00613 days <br />0.147 hours <br />8.763227e-4 weeks <br />2.01665e-4 months <br /> on October 13, 1994, with reactor power at 100%, a controlled reactor shutdown, at 5% per hour, was begun in preparation for refueling outage 2R8. At approximately 2200 hours0.0255 days <br />0.611 hours <br />0.00364 weeks <br />8.371e-4 months <br /> (same day), decrease to 15% power was achieved and, at 2244 hours0.026 days <br />0.623 hours <br />0.00371 weeks <br />8.53842e-4 months <br /> (same day), the Unit was placed in MODE 3 (HOT STANDBY).
On October 13, 1994, the surveillance requirements of TS Table 4.3-1, Item 2, (including the maximum allowable extension per TS 4.0.2) were not met, due to failure to perform the once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> calibration of power range instrumentation.
Event discovery occurred on October 14, 1994. Investigation revealed other instances on both Units during 1994, where the surveillance requirements of TS Table 4.3-1 were performed beyond the allowable extension per TS 4.0.2: Unit 2 -January 8 *(reactor power 98.8%), July 5 (reactor power 43.3%), July 8 (reactor power 72.7%), and September 12 (reactor power 93.8%) and Unit 1 -February 26 (reactor power 70.6%), March 5 (99.0%) and September 2 (reactor power , ' I I
.. LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating station Unit 2 ANALYSIS OF OCCURRENCES:
DOCKET NUMBER 5000311 LER NUMBER 94-012-00 PAGE 3 of 5 TSs specify that the nuclear instrumentation system (NIS) power range calibration be performed at least once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, whenever rated thermal power (RTP) is greater than 15%. Procedure S2.RE-ST.ZZ-0001(Q), "CALORIMETRIC"CALCULATION", is used to complete this calibration.
In addition, during Monday through Friday, the Technical Department assists the Operations Department in the performance of this procedure.
The "DAILY ROUTINES" checklist log of Operations Directive Procedure, SC.OP-DD.ZZ-OD40(Z), "SHIFT ROUTINES", Step 5.16, specifies the time frame for surveillance performance as oaoo-1200 hours. In addition, the procedure description for Step 5.16 states "The interval between calorimetrics shall not exceed 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />".
- On October 13, 1994, Unit 2 operated above 15% power for approximately six hours and 53 minutes beyond the maximum allowable extension for the required .NISpower range calibration.
As such, approximately 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> transpired*
between the prior NIS calibration and when RTP was 15%. Other instances occurred on both Units where the maximum allowable extension for the required NIS power range calibration was exceeded; Unit' 2*-two hours, 55 minutes; five hours,* 25 minutes; six hours, 19 minutes; and eight hours, 14 minutes; and Unit 1 -two hours, 42 minutes; 9 minutes; and three hours. APPARENT CAUSE OF OCCURRENCES:
These events are attributed to "Personnel Error", as classified in Appendix B of NUREG_-1022.
The event of October 13, 1994 resulted from failure of the Nuclear Control Operator (NCO) to follow procedure
[Step 5.16 of SC.OP-DD.ZZ-OD40(Z)]
combined with failure of the Nuclear Shift Supervisor (NSS) to adequately review the completed shift routines.
A contributor was focus upon activities related to the ongoing Unit power reduction and removal the Unit from_service for the upcoming refueling outage. Another contributor was a common mis-perception that the surveillance interval was once per calendar day and that the surveillance could be delayed within the confines of a calendar day, until establishing a stable plant condition which would allow performance of the surveillance.
Existence of this misperception is reinforced by discovery of the additional events where the surveillance was not completed with the required time period. Analysis of failed barriers indicates the personnel errors were the result of less than adequate knowledge and training.
Thi? was evidenced by the misunderstanding the once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> surveillance requirement.
1-.. I. I --LICENSEE EVENT REPORT (LER) TEXT CONTINUATION
- Salem Generating Station Unit 2 PREVIOUS OCCURRENCES:
DOCKET NUMBER 5000311 LER NUMBER 94-012-00 PAGE 4 of 5 Previous events involving the.failure to perform the required daily NIS calibration occurred on December 8, 15, 16, and 26, 1977. These were identified as an.infraction in a Notice of Violation in NRC Inspection Report 50-272/78-02, dated February 17, 1978. The cause of these occurrences was attributed to ongoing Unit load transients,
- which did not permit the required stable conditions to.allow*
completion of the surveillance.
Corrective action included an Operations Night Order Book {NOB) entry on 1/28/78, instructing the Senior Nuclear Shift Supervisor
{SNSS) of the necessity to perform the _surveillance.
This NOB entry directed the SNSS to stop a load change, if required, to permit completion of the surveillanc.e within th_e required till\e frame. SAFETY SIGNIFICANCE:
These events are reportable pursuant to 10CFR50.73{a)
(2) (i) (B), due to failure to comply with the Limiting Condition For Operation requirements of TS Table 4.3-1, as well as TS 3.0.2, due to failure to perform the surveillance requirements within the.maximum allowable extension.
The safety signif of October 13 event is minimal as the approximate six hours 53 minutes the Unit operated until the requirements of TS no longer applied (i.e. entry into.MODE
- 3) is bounded by the requirements of TS 3.0.3.. The safety significance of the other occurrences is minimal based upon satisfactory completion of the surveillance following each event. In addition, in accordance with procedure, reaqtor power is maintained less than 100% and verified by an on-line calorimetric computer readout. The inputs to the on-line calorimetric computer readout are the same as the manual surveillance calculation.
CORRECTIVE ACTION: All Licensed personnel involved in the October 13 event have been counseled concerning their *actions and Management expectations regarding procedure compliance.
An Operations NOB entry, explaining the surveillance requirement, was issued on.October 26, 1994. SC.OP-DD.ZZ-OD40{Z) has been revised to enhance arid clarify the definition of. the surveillance interval.
Additionally, a NOB entry was made on November 8, 199*4, describing the procedure change and requiring all Senior Shift Supervisors to review this change with their licensed personnel.
- .e LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Salem Generating station Unit 2 CORRECTIVE ACTION: (cont'd) DOCKET NUMBER 5000311 LER NUMBER 94-012-00 PAGE 5 of 5 As a result of these events, a review of all Operations TS surveillance requirements with frequencies of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> or less was performed to ensure TS compliance.
This review identified four surveillances that, although presently adequate, will be procedurally enhanced as part of the SC.OP-DD.ZZ-OD40(Z) revision effort. To ensure a clear understanding of the surveillance requirement, it has been specified, verbatim, in S1(2).RE-ST.ZZ-OOOl(Q).
This procedure change has been discussed with select Technical Department personnel, who perform this requirement.
- Based on interviews with involved personnel, Operations Management will revise SC.OP-DD.ZZ-OD40(Z), by February 28, 1995, to separate TS surveillance requirements from other routine evolutions.
This change is intended.to provide more focus on TS requirements and-address human factors tied to performance and review of the procedure.
All Licensed personnel and select members of the Technical Department, will review these events to ensure their understanding of
- the surveillance interval.
During the present re-qualification cycle, all licensed personnel will receive training specific to these events and TS surveillance interval requirements.
Additionally, the Training Department will review the initial Program -to ensure proper focus on TS interval requirements.
The aforementioned training and review will encompass both Salem and Hope Creek programs.
MJPJ:pc SORC Mtg.94-087