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| * * **. NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (4-961 EXPIRES 04/30/98 LICENSEE EVENT REPORT (LER) ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COUECTION REQUEST: 50.0 HRS. REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED (Sae reverse for required number of BACK TO INDUSTRY. | | * * **. NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (4-961 EXPIRES 04/30/98 LICENSEE EVENT REPORT (LER) ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COUECTION REQUEST: 50.0 HRS. REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED (Sae reverse for required number of BACK TO INDUSTRY. |
| FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH digits/characters for each block) (T-6 F33J, U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001. | | FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH digits/characters for each block) (T-6 F33J, U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001. |
| AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC 20503. FACILITY NAME 111 DOCKET NUMBER 121 PAGE 131 SALEM GENERATING STATION, UNIT 1 05000272 1 OF 5 TITLE 141 Failure To Perform Radioactive Effluent Concentration Surveillance And Effluent Monitoring Instrument Channel Setpoint Determinations In Accordance With Technical Specifications EVENT DATE (5) LER NUMBER (6) REPORT DATE 171 OTHER FACILITIES INVOLVED (8) I FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL I REVISION MONTH DAY YEAR NUMBBI NUMBER Salem Unit 2 05000311 03 02 98 98 004 00 04 01 98 FACILITY NAME DOCKET NUMBBI ----OPERATING 4 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) 111 I MODE (9) 20.2201(b) 20.2203(a11211vl x 50. 73(a)(2)(i) | | AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC 20503. FACILITY NAME 111 DOCKET NUMBER 121 PAGE 131 SALEM GENERATING STATION, UNIT 1 05000272 1 OF 5 TITLE 141 Failure To Perform Radioactive Effluent Concentration Surveillance And Effluent Monitoring Instrument Channel Setpoint Determinations In Accordance With Technical Specifications EVENT DATE (5) LER NUMBER (6) REPORT DATE 171 OTHER FACILITIES INVOLVED (8) I FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL I REVISION MONTH DAY YEAR NUMBBI NUMBER Salem Unit 2 05000311 03 02 98 98 004 00 04 01 98 FACILITY NAME DOCKET NUMBBI ----OPERATING 4 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) 111 I MODE (9) 20.2201(b) 20.2203(a11211vl x 50. 73(a)(2)(i) |
| : 50. 73(a)(2)(viii) | | : 50. 73(a)(2)(viii) |
| POWER 000 20.2203(a)(1 I 20.2203(a)(3)(i) | | POWER 000 20.2203(a)(1 I 20.2203(a)(3)(i) |
| : 50. 73(a)(2)(iil 50.73(a)(2)(xJ LEVEL (101 20.2203(a)(2Jlil 20.2203(a)(3)(ii) | | : 50. 73(a)(2)(iil 50.73(a)(2)(xJ LEVEL (101 20.2203(a)(2Jlil 20.2203(a)(3)(ii) |
| : 50. 73(a)(2)(iii) 73.71 -20.2203(a)(2)(iil 20 .2203(11)(4) | | : 50. 73(a)(2)(iii) 73.71 -20.2203(a)(2)(iil 20 .2203(11)(4) |
| : 50. 73(a)(2)(iv) | | : 50. 73(a)(2)(iv) |
| OTHER 20.2203(a)(2Jliiil 50.36(c)(1) | | OTHER 20.2203(a)(2Jliiil 50.36(c)(1) |
| : 50. 73(a)(2)(v) | | : 50. 73(a)(2)(v) |
| Specify In Abetract below or In NRC Form 366A 20.2203(a)(2)(ivJ 50.36(c)(2) | | Specify In Abetract below or In NRC Form 366A 20.2203(a)(2)(ivJ 50.36(c)(2) |
| : 50. 73(e)(2J(viiJ LICENSEE CONTACT FOR THIS LER (12) NAME TELEPHONE NUMBBI Onolude Alu Code) Brooke Knieriem, Licensing Engineer (609) 339-1782 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM COMPONENT MANUFACT..ull REPORT AllLE I CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED (141 EXPECTED MONTH DAY YEAR IYES INO SUBMISSION (If yes. complete EXPECTED SUBMISSION DATE). DATE 115) ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 11ingle-11paced typeWTitten li11e11) (16) This LER documents the failure of Salem Units 1 and 2 to comply with the requirements of Technical Specifications (TS) 4.11.1.1.2, Radioactive Effluents, and TS 3 .3 .3. 8, Radioactive Liquid Effluent Monitoring and Instrumentation. | | : 50. 73(e)(2J(viiJ LICENSEE CONTACT FOR THIS LER (12) NAME TELEPHONE NUMBBI Onolude Alu Code) Brooke Knieriem, Licensing Engineer (609) 339-1782 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM COMPONENT MANUFACT..ull REPORT AllLE I CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED (141 EXPECTED MONTH DAY YEAR IYES INO SUBMISSION (If yes. complete EXPECTED SUBMISSION DATE). DATE 115) ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 11ingle-11paced typeWTitten li11e11) (16) This LER documents the failure of Salem Units 1 and 2 to comply with the requirements of Technical Specifications (TS) 4.11.1.1.2, Radioactive Effluents, and TS 3 .3 .3. 8, Radioactive Liquid Effluent Monitoring and Instrumentation. |
| TS 4.11.1.1.2 requires that the results of radioactivity analyses be used in accordance with the Off site Dose Calculation Manual (ODCM) to assure that the release concentrations are maintained within TS limits. Salem TS 3 .3 .3. 8 requires that radioactive effluent monitoring instrumentation channel alarm and trip setpoints be determined in accordance with the ODCM. Contrary to these requirements, release rate calculations and radioactive effluent monitoring channel setpoints were identified that employed a Safety Factor different from that specified by the ODCM. This event is reportable under 10CFRS0.73(a) | | TS 4.11.1.1.2 requires that the results of radioactivity analyses be used in accordance with the Off site Dose Calculation Manual (ODCM) to assure that the release concentrations are maintained within TS limits. Salem TS 3 .3 .3. 8 requires that radioactive effluent monitoring instrumentation channel alarm and trip setpoints be determined in accordance with the ODCM. Contrary to these requirements, release rate calculations and radioactive effluent monitoring channel setpoints were identified that employed a Safety Factor different from that specified by the ODCM. This event is reportable under 10CFRS0.73(a) |
| (2) (i) (B) I any operation or condition prohibited by the plant's TS. Although instances were identified in which the Safety Factor used was less conservative than the Safety Factor. in the ODCM, no instances were identified in which TS concentration limits for release were exceeded. | | (2) (i) (B) I any operation or condition prohibited by the plant's TS. Although instances were identified in which the Safety Factor used was less conservative than the Safety Factor. in the ODCM, no instances were identified in which TS concentration limits for release were exceeded. |
| The apparent cause of this event was an organizational deficiency in the implementation of the Radioactive Effluents/ODCM program. A contributing factor was a lack of understanding by station personnel of the role of the ODCM in the licensing basis. Corrective actions were taken to correctly document the Safety Factor in the ODCM and to correct Safety Factor discrepancies between the ODCM, the implementing procedure, and the Radioactive Effluents TS (RETS) software. | | The apparent cause of this event was an organizational deficiency in the implementation of the Radioactive Effluents/ODCM program. A contributing factor was a lack of understanding by station personnel of the role of the ODCM in the licensing basis. Corrective actions were taken to correctly document the Safety Factor in the ODCM and to correct Safety Factor discrepancies between the ODCM, the implementing procedure, and the Radioactive Effluents TS (RETS) software. |
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| LER 311/97-007-00 reported a violation to TS 3.3.3.8, Radioactive Liquid Effluent Monitoring Instrumentation. | | LER 311/97-007-00 reported a violation to TS 3.3.3.8, Radioactive Liquid Effluent Monitoring Instrumentation. |
| This violation was caused by the failure of station personnel to independently verify the radioactive liquid waste release valve lineup as a compensatory measure required by TS when the radioactive liquid effluent monitoring instrumentation is out of SAFETY CONSEQUENCES There were no safety consequences as a result of this event. A review of the releases performed between the implementation of Revision 10 to the ODCM on January 3, 1996, and the time that the discrepancy between the ODCM, the RETS software, and the procedure were corrected on October 23, 1997; and a review of the releases on January 3, 1998, revealed that in no case were the concentration limits of TS 3.11.1.1 exceeded. | | This violation was caused by the failure of station personnel to independently verify the radioactive liquid waste release valve lineup as a compensatory measure required by TS when the radioactive liquid effluent monitoring instrumentation is out of SAFETY CONSEQUENCES There were no safety consequences as a result of this event. A review of the releases performed between the implementation of Revision 10 to the ODCM on January 3, 1996, and the time that the discrepancy between the ODCM, the RETS software, and the procedure were corrected on October 23, 1997; and a review of the releases on January 3, 1998, revealed that in no case were the concentration limits of TS 3.11.1.1 exceeded. |
| Additionally, although Effluent Radiation Monitor setpoints were not set in accordance with the ODCM as required by TS, at no time were the setpoints set to a value that would have permitted the concentration limits of TS 3.11.l.1 to be exceeded for batch or continuous release. CORRECTIVE ACTIONS 1. The releases performed between the implementation of Revision 10 to the ODCM on January 3, 1996, and the time that the discrepancy between the ODCM, the RETS software, and the procedure was corrected on October 23, 1997; and the releases on January 3, 1998 were reviewed to verify that the concentration limits of TS 3.11.1.1 were not exceeded. | | Additionally, although Effluent Radiation Monitor setpoints were not set in accordance with the ODCM as required by TS, at no time were the setpoints set to a value that would have permitted the concentration limits of TS 3.11.l.1 to be exceeded for batch or continuous release. CORRECTIVE ACTIONS 1. The releases performed between the implementation of Revision 10 to the ODCM on January 3, 1996, and the time that the discrepancy between the ODCM, the RETS software, and the procedure was corrected on October 23, 1997; and the releases on January 3, 1998 were reviewed to verify that the concentration limits of TS 3.11.1.1 were not exceeded. |
| : 2. On March 14, 1998, the Safety Factor was corrected in the ODCM by implementation of Revision 11. Additionally, the implementing procedure and RETS software were revised to align with this change. NRC FORM 366A (4-95) | | : 2. On March 14, 1998, the Safety Factor was corrected in the ODCM by implementation of Revision 11. Additionally, the implementing procedure and RETS software were revised to align with this change. NRC FORM 366A (4-95) |
| * | | * |
| * NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) SALEM UNIT 1 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) LER NUMBER (6) YEAR I SEQUENTIAL I REVISION NUMBER NUMBE!I 05000272 98 *-004 00 TEXT (If more space is required, use additional copies of NRC Form 366A) ( 17) CORRECTIVE ACTIONS(Cont.) | | * NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) SALEM UNIT 1 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) LER NUMBER (6) YEAR I SEQUENTIAL I REVISION NUMBER NUMBE!I 05000272 98 *-004 00 TEXT (If more space is required, use additional copies of NRC Form 366A) ( 17) CORRECTIVE ACTIONS(Cont.) |
| PAGE (3) 5 OF 5 3. Radioactive liquid effluent monitors were declared inoperable because of the incorrect Safety Factor applied to their setpoint. | | PAGE (3) 5 OF 5 3. Radioactive liquid effluent monitors were declared inoperable because of the incorrect Safety Factor applied to their setpoint. |
| Following implementation of ODCM revision 11, the setpoints were restored to compliance with the ODCM. 4. Appropriate personnel involved with the errors have been held accountable in accordance with PSE&G's procedures and policies. | | Following implementation of ODCM revision 11, the setpoints were restored to compliance with the ODCM. 4. Appropriate personnel involved with the errors have been held accountable in accordance with PSE&G's procedures and policies. |
| : 5. Improvements to ODCM effluents program controls and review process will be implemented to ensure that adequate interface exists between design engineering, effluents software, radiation monitor set points, and the implementing procedures. | | : 5. Improvements to ODCM effluents program controls and review process will be implemented to ensure that adequate interface exists between design engineering, effluents software, radiation monitor set points, and the implementing procedures. |
| (00980224081, CRCA 12, to be completed by 6/15/98) 6. Training will be provided to appropriate personnel on the effluents program and its licensing basis. (00980224081, CRCA 04, to be completed by 6/15/98, CRCA 29, to be completed by 9/30/98.) | | (00980224081, CRCA 12, to be completed by 6/15/98) 6. Training will be provided to appropriate personnel on the effluents program and its licensing basis. (00980224081, CRCA 04, to be completed by 6/15/98, CRCA 29, to be completed by 9/30/98.) |
| : 7. An independent review of the ODCM will be performed to ensure that it is consistent with available regulatory guidance. | | : 7. An independent review of the ODCM will be performed to ensure that it is consistent with available regulatory guidance. |
| (00980224081, CRCA 17,to be completed by 7/15/98) 8. Ownership for the ODCM has been formally defined and assigned. | | (00980224081, CRCA 17,to be completed by 7/15/98) 8. Ownership for the ODCM has been formally defined and assigned. |
| NRC FORM 366A (4-95)}} | | NRC FORM 366A (4-95)}} |
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Category:LICENSEE EVENT REPORT (SEE ALSO AO
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Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:RO)
MONTHYEARML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0081998-12-24024 December 1998 LER 97-001-01:on 970215,failure to Perform TS Surveillance of Component Cooling Water Sys Check Valves Occurred.Caused by Inadequate Communication Between EOP Group & IST Reviewers.Procedure Revised.With 981224 Ltr ML18106B0021998-12-17017 December 1998 LER 98-015-01:on 980924,improper Installation of Test Equipment to RPS Occurred.Caused by Inadequate 10CFR50.59 Applicability Reviews During Past Revs.Revised Procedures. with 981217 Ltr ML18106A9551998-11-0303 November 1998 LER 96-013-01:on 960711,concluded That Current Gain & Bias Settings Had Rendered Overtemperature Delta Temp Protection Channels Inoperable.Caused by Scaling Error.Licensee Will Revise Scaling Calculations.With 981105 Ltr ML18106A9451998-10-30030 October 1998 LER 97-004-01:on 970408,failure to Comply with TS Action Statement,Dg Start & Inadequate Surveillance Testing,Was Noted.Caused by Inadequate Tracking of Inoperable Equipment. Discussed Event & Lessons Learned.With 981022 Ltr ML18106A9491998-10-22022 October 1998 LER 98-015-00:on 980924,identified Improper Installation of Test Equipment to Rps.Cause Indeterminate.Procedures for Installation of Test Equipment for Collection of State Point Data Were Placed on Administrative Hold.With 981022 Ltr ML18106A9301998-10-21021 October 1998 LER 98-014-00:on 980725,noted Improper Calibr of Liquid Radwaste Effluent Line Radiation Monitor.Caused by Inattention to Detail by Maint Personnel.Channel Calibr Was Successfully Performed on 1R18 on 980821.With 981019 Ltr ML18106A9071998-10-0101 October 1998 LER 98-014-00:on 980918,discovered That Fire Barrier Matl for HVAC Ducts Does Not Meet Required Level of Fire Resistance.Cause Indeterminate.Established Appropriate Compensatory Actions for Fire Barriers.With 981001 Ltr ML18106A8951998-09-28028 September 1998 LER 98-012-01:on 980725,noted That Afs Was Operated with Less than Required Number of Operable AFW Pumps.Caused by Improper Procedure Implementation.Runout Protection Pressure Device for 22 AFW Pumps Was Returned to Svc.With 980928 Ltr ML18106A8821998-09-21021 September 1998 LER 98-013-00:on 980820,noted Surveillance of Containment Penetration Overcurrent Protection Devices Missed.Caused by Human Error.Satisfactorily Tested Apprpriate Breakers & Disciplined Involved Personnel.With 980921 Ltr ML18106A8791998-09-16016 September 1998 LER 96-006-01:on 960717,determined That non-radioactive Liquid Basin Radwaste Monitor Inoperable During Low Head Conditions.Caused by Inadequate Design Change Package.Design Change 1EC3663-01 Has Been Installed.With 980916 Ltr ML18106A8801998-09-0808 September 1998 LER 98-013-00:on 980806,operation with TS Required Equipment OOS Was Noted.Caused by Human Error.Reviewed Processes & Practices Re Safety Sys Status Control,Procedure Rev & Extra Training.With 980908 Ltr ML18106A8531998-08-27027 August 1998 LER 98-007-00:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Cause of Event Has Not Yet Been Determined.Assembled Root Cause Team & Replaced Affected tubing.W/980827 Ltr ML18106A8521998-08-27027 August 1998 LER 98-011-00:on 980803,ESFA During a 4KV Automatic Transfer Test Was Noted.Caused by Premature Release of Control Console Pushbutton Due to Inadequate Procedural Step.Revised procedure.W/980827 Ltr ML18106A8421998-08-24024 August 1998 LER 98-012-00:on 980725,discovered That Plant Had Operated in Modes 1 & 2 w/twenty-two AFW Pumps Inoperable.Caused by Failure to Restore Pump Runout Protection Pressure Device to Svc.Returned Subject Device to svc.W/980824 Ltr ML18106A8431998-08-24024 August 1998 LER 98-009-00:on 980810,failure to Post Continuous Firewatch as Required by Fire Protection Plan Noted.Caused by Failure to Recognize Concurrent Conditions.Continuous Firewatch Was Posted Immediately & Repaired Smoke detectors.W/980824 Ltr ML18106A8141998-08-13013 August 1998 LER 98-010-00:on 980714,determined That Leakage from Boron Injection Tank Exceeded Max Allowable ECCS Leakage from Sources Outside Containment.Caused by Leaking 2SJ404 Manual Sample valve.2SJ404 Valve repaired.W/980813 Ltr ML18106A8201998-08-13013 August 1998 LER 98-012-00:on 980715,potential to Exceed Rating of Piping Due to Isolation of Overpressure Protection Line Was Noted. Caused by Inadequate Procedural Guidance.Appropriate Operations Dept Procedures Have Been revised.W/980813 Ltr ML18106A6931998-06-29029 June 1998 LER 98-003-00:on 980122,inappropriate Plugging of Tubes R9C60 & R10C60 in Salem Unit 2 Sg,Was Performed.Caused by Failure of Qualification,Verification & Validation Process. Tubes Reviewed to Verify No Others Inappropriately Plugged ML18106A6471998-06-0404 June 1998 LER 98-011-00:on 980505,improper Isolation of Single Cell Battery Charger from 125 Vdc Battery Was Noted.Caused by Inadequate 10CFR50.59 Applicability Review.Placed Procedure SC.MD-CM.ZZ-0024(Q) on Administrative hold.W/980604 Ltr ML18106A6421998-06-0101 June 1998 LER 98-010-00:on 931019,reactor Pressure Vessel Insp Plugs Were Out of Configuration,Was Noted.Caused by Personnel Error.Proper Configuration Was Restored Shortly After Discovery Prior to Entering Mode 2.W/980601 Ltr ML18106A6431998-05-29029 May 1998 LER 98-006-01:on 980227,determined Incorrect Scaling Error of First Stage Pressure Transmitter Existed.Caused by Human Error.Revised Setpoint Calculation SC-MS002-01 & Revised Associated Instrument Calibr Database info.W/980529 Ltr ML18106A6141998-05-18018 May 1998 LER 98-008-00:on 970814,failure to Test 21 & 22 AF 40 Valves in Closed Direction as Required by TS 4.0.5 Was Noted.Caused by Inadequate Design Mod Process.Motor Driven 21/22 AF 40 Valves Were Tested IAW Revised procedure.W/980518 Ltr ML18106A5901998-05-0101 May 1998 LER 98-009-00:on 980405,epoxy Missing from Terminals of H Analyzer Was Noted.Caused by Inadequate Development of Procedure.H Analyzers Were Repaired & Review of Other Safety Related Equipment in Containment Was performed.W/980501 Ltr ML18106A5611998-04-20020 April 1998 LER 98-008-00:on 980323,inadequate Testing of Salem Unit 1 Containment Air Locks Resulted in Entering TS 3.0.3.Caused by less-than-adequate Work Practices During Replacement of Equalizing Valve.Salem Unit 2 Airlocks Were Inspected ML18106A6061998-04-0101 April 1998 Corrected LER 98-004-00:on 980302,failure to Comply W/Tss 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Have Been Taken to Correctly Document Safety Factors.Corrects Prior Similar Occurrences ML18106A4451998-04-0101 April 1998 LER 98-004-00:on 980302,failure to Perform TS 4.11.1.1.2 & 3.3.3.8 Was Noted.Caused by Organizational Deficiency.Steps Were Taken to Correctly Document Safety factors.W/980401 Ltr ML18106A4351998-03-30030 March 1998 LER 98-006-00:on 980227,incorrect Scaling of First Stage Turbine Impulse Pressure Transmitters Noted.Cause Indeterminate.Implemented Procedure Changes & re-scaled Affected Turbine Impulse Pressure transmitters.W/980330 Ltr ML18106A3961998-03-20020 March 1998 LER 98-005-00:on 980219,inoperability of Twelve EDG Fuel Oil Transfer Pump (FOTP) Noted.Caused by Installation of Incorrect Control Switch.Installed Correct off-auto-manual Switch & Verified Operability of Twelve FOTP.W/980320 Ltr ML18106A5781998-03-20020 March 1998 Corrected LER 98-005-00:on 980219,inoperability of 12 Fuel Oil Transfer Pump (Fotp),Noted.Caused by Installation of Incorrect Control Switch.Field Insp Performed to Verify Configuration of Switches for 11,21 & 22 FOTPs ML18106A4021998-03-20020 March 1998 LER 98-007-00:on 980218,failure to Establish Containment Integrity (Closure) Prior to Fuel Movement Was Noted.Caused by Failure to Identify & Include Condensate Pot Vent in Appropriate Valve Lineup.Valves identified.W/980320 Ltr ML18106A4031998-03-20020 March 1998 LER 98-006-00:on 980221,ESF Actuation of 11 & 12 Auxiliary Feedwater Pumps Occurred.Caused by Human Error.Operators Promptly Established Feedwater to All SG & Restored Proper Water levels.W/980320 Ltr 1999-08-26
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217A9931999-09-30030 September 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data ML18107A5581999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 2.With 991014 Ltr ML18107A5571999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Salem,Unit 1.With 991014 Ltr ML18107A5301999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 2.With 990913 Ltr ML18107A5311999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Salem,Unit 1.With 990913 ML18107A5031999-08-26026 August 1999 LER 99-006-00:on 990729,determined That SG Blowdown RMs Setpoint Was non-conservative.Caused by Inadequate ACs for Incorporating Original Plant Licensing Data Into Plant Procedures.Blowdown Will Be Restricted.With 990826 Ltr ML18107A5201999-08-12012 August 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#9) Second Interval,Second Period, First Outage (96RF). ML18107A4811999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 1.With 990813 Ltr ML18107A4821999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Salem,Unit 2.With 990813 Ltr ML18107A4691999-07-28028 July 1999 LER 99-008-00:on 990714,determined That Limit Switch Cables Were Subject to Multiple Hot Shorts in Same Fire Area.Caused by Inadequate Original Post Fire Safe Shutdown Analysis.All Limit Switch Cables for MOVs Were Reviewed.With 990728 Ltr ML18107A4441999-07-0606 July 1999 LER 99-007-00:on 990605,surveillance for Quadrant Power Tilt Ratio (QPTR) Was Missed.Caused by Human Error.Qptr Calculation Was Performed & Personnel Involved Have Been Held Accountable IAW Pse&G Policies.With 990706 Ltr ML18107A4211999-07-0202 July 1999 LER 99-005-00:on 990605,11 Containment Declared Inoperable. Caused by Valves 11SW72 & 11SW223 Both Leaking.Procedure S1.OP-ST.SW-0010(Q) Was Enhanced to Provide Specific Instructions to Ensure Proper Sequencing.With 990702 Ltr ML18107A4331999-07-0101 July 1999 LER 99-002-01:on 990405,determined That 2SA118 Failed as Found Leakrate Test.Caused by Foreign Matl Found in 2SA118 valve.2SA118 Valve Was Cycled Several Times & Seat Area Was Air Blown in Order to Displace Foreign Matl.With 990701 Ltr ML18107A4321999-07-0101 July 1999 LER 99-006-01:on 990501,determined That There Was No Flow in One of Four Injection Legs.Caused by Sticking of Valve in Safety Injection Discharge Line to 21 Cold Leg.Valve Was Cut Out of Sys & Replaced.With 990701 Ltr ML18107A5211999-07-0101 July 1999 Rev 0 to Sgs Unit 2 ISI RFO Exam Results (S2RFO#10) Second Interval,Second Period,Second Outage (99RF). ML18107A4351999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 1.With 990713 Ltr ML18107A4341999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Salem,Unit 2.With 990713 Ltr ML20196H8621999-06-30030 June 1999 NRC Regulatory Assessment & Oversight Pilot Program, Performance Indicator Data, June 1999 Rept ML18107A3951999-06-17017 June 1999 LER 99-004-00:on 990520,reactor Tripped from 100% Power,Due to Negative Flux Trip Signal from Nuclear Instrumentation. Cause Has Not Been Determined.Discoloration Was Identified on One of Penetrations.With 990617 Ltr ML18107A3661999-06-0909 June 1999 LER 99-003-00:on 990513,unplanned Entry Into TS 3.0.3 Was Made.Caused by Human error.Re-positioned Creacs Supply Fan Selector Switches & Revised Procedures S1 & S2.OP-ST.SSP-0001(Q).With 990609 Ltr ML18107A3551999-06-0202 June 1999 LER 99-005-00:on 990504,failure to Meet TS Action Statement Requirements for High Oxygen Concentration in Waste Gas Holdup Sys Occurred.Caused by Inability of Operators. Existing Procedures Will Be Evaluated.With 990602 Ltr ML18107A3441999-06-0101 June 1999 Interim Part 21 Rept Re Premature Over Voltage Protection Actuation in Circuit Specific Application in Dc Power Supply.Testing & Evaluation Activities Will Be Completed on 990716 ML18107A3541999-06-0101 June 1999 LER 99-006-00:on 990501,HHSI Flow Balance Discrepancy Was Noted During Surveillance.Caused by Sticking of Check Valve in SI Discharge Line to 21 Cold Leg.Valve 21SJ17,was Cut Out of Sys & Replaced.With 990601 Ltr ML18107A3681999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 1.With 990611 Ltr ML18107A3721999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Salem Generating Station,Unit 2.With 990611 Ltr ML18107A2931999-05-12012 May 1999 LER 99-002-00:on 990413,determined That Number 12 Auxiliary Bldg Exhaust Fan Was Rotating Backwards.Caused by mis-wiring of Motor Due to Human Error by Maint technician.Mis-wiring Was Corrected & Fan Was Returned to Svc.With 990512 Ltr ML18107A2781999-05-10010 May 1999 LER 99-004-00:on 990411,automatic Actuation of ESF Occurred During Reactor Vessel Head Removal in Support of Refueling Operations.Caused by High Radiation Condition.Containment Atmosphere Was Monitored.With 990505 Ltr ML18107A2791999-05-0404 May 1999 LER 99-003-00:on 990406,all Salem Unit 2 Chillers Rendered Inoperable.Caused by Human Error.Lessons Learned from Event Were Communicated to All Operators by Including Them in Night Orders.With 990504 Ltr ML18107A2741999-05-0303 May 1999 LER 99-002-00:on 990405,determined That Containment Isolation Valve Failed as Found Leakrate Test.Caused by Foreign Matl Blocking Valves from Closing.Check Valve Mechanically Agitated.With 990504 Ltr ML18107A3711999-04-30030 April 1999 Corrected Monthly Operating Rept for Apr 1999 for Salem Generating Station,Unit 1 ML18107A3151999-04-30030 April 1999 Submittal-Only Screening Review of Salem Generating Station Individual Plant Exam for External Events (Seismic Portion), Rev 1 ML18107A2991999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 1.With 990514 Ltr ML18107A2971999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Salem Unit 2.With 990514 Ltr ML18107A2351999-04-23023 April 1999 LER 99-001-00:on 990330,MSSV Failed Lift Set Test.Caused by Setpoint Variance Which Is Result of Aging.Valves Were Adjusted & Retested to Ensure TS Tolerance.With 990423 Ltr ML18107A2881999-04-0707 April 1999 Rev 0 to NFS-0174, COLR for Salem Unit 2 Cycle 11. ML18107A1821999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 1.With 990414 Ltr ML18107A1831999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Salem,Unit 2.With 990414 Ltr ML18106B1471999-03-29029 March 1999 LER 99-001-00:on 990228,reactor Scram Was Noted as Result of Turbine Trip.Caused by Operator Error.Lesson Plans Revised to Explicitly Demonstrate Manner in Which Valve Functions. with 990329 Ltr ML18106B1021999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 2.With 990315 Ltr ML18106B1011999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Salem Unit 1.With 990315 Ltr ML18106B0931999-02-25025 February 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Caused by Crack Due to Improper Location of Heated Bar.Only One Part Out of 7396 Pieces in Forging Lot Was Found to Be Cracked.Affected Util,Notified ML18106B0701999-02-16016 February 1999 LER 98-015-00:on 981208,inadvertent Discharge Through RHR Relief Valve During Startup Was Noted.Caused by Operator Performing Too Many Tasks Simultaneously.Appropriate Actions Have Been Taken IAW Policies & Procedures.With 990216 Ltr ML18106B0551999-02-0101 February 1999 Part 21 Rept Re Possible Matl Defect in Swagelok Pipe Fitting Tee,Part Number SS-6-T.Defect Is Crack in Center of Forging.Analysis of Part Is Continuing & Further Details Will Be Provided IAW Ncr Timetables.Drawing of Part,Encl ML18106B0561999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 2.With 990212 Ltr ML18106B0571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for Salem Generating Station,Unit 1.With 990212 Ltr ML20205P1671999-01-31031 January 1999 a POST-PLUME Phase, Federal Participation Exercise ML18106B0441999-01-29029 January 1999 Part 21 Rept Re Possible Defect in Swagelok Pipe Fitting Tee Part Number SS-6-T.Caused by Crack in Center of Forging. Continuing Analysis of Part & Will Provide Details in Acoordance with NRC Timetables ML18106B0491999-01-28028 January 1999 LER 98-007-01:on 980730,reactor Coolant Instrument Line through-wall Leak Was Noted.Caused by Transgranular Stress Corrosion Cracking.Replaced Affected Tubing.With 990128 Ltr ML18106B0401999-01-18018 January 1999 LER 98-016-00:on 981219,ECCS Leakage Was Outside of Design Value.Caused by Leakage Past Seat of 21RH34 Manual Drain. Valve 21RH34 Was Reseated.With 990118 Ltr ML18106B0251998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Salem Unit 2.With 990115 Ltr 1999-09-30
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- Public Electric and Gas Company P.O. Box 236 Hancocks Bridge, New Jersey 08038-0236 Nuclear Business Unit U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 LER 272/98-004-00 APR 0 11998 LR-N980163 SALEM GENERATING STATION -UNIT 1 FACILITY OPERATING LICENSE NO. DPR-70 DOCKET NO. 50-272 Gentlemen:
This Licensee Event Report entitled "Failure To Perform Radioactive Effluent Concentration Surveillance And Effluent Monitoring Instrument Channel Setpoint Determinations In Accordance With Technical Specifications" is being submitted pursuant to the requirements of the Code of Federal Regulations
- 1OCFR50.73 ( a)(2)(i)(B)****.
Attachment RBK/ c Distribu'tion LER File 3.7 The power is in your hands. ,_ ....... '-' { Sincerely, A. C. Bakken Ill General Manager Salem Operations 95*2168 REV. 6/94
- * **. NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 (4-961 EXPIRES 04/30/98 LICENSEE EVENT REPORT (LER) ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH THIS MANDATORY INFORMATION COUECTION REQUEST: 50.0 HRS. REPORTED LESSONS LEARNED ARE INCORPORATED INTO THE LICENSING PROCESS AND FED (Sae reverse for required number of BACK TO INDUSTRY.
FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE INFORMATION AND RECORDS MANAGEMENT BRANCH digits/characters for each block) (T-6 F33J, U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555-0001.
AND TO THE PAPERWORK REDUCTION PROJECT (3150-0104), OFFICE OF MANAGEMENT AND BUDGET. WASHINGTON, DC 20503. FACILITY NAME 111 DOCKET NUMBER 121 PAGE 131 SALEM GENERATING STATION, UNIT 1 05000272 1 OF 5 TITLE 141 Failure To Perform Radioactive Effluent Concentration Surveillance And Effluent Monitoring Instrument Channel Setpoint Determinations In Accordance With Technical Specifications EVENT DATE (5) LER NUMBER (6) REPORT DATE 171 OTHER FACILITIES INVOLVED (8) I FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL I REVISION MONTH DAY YEAR NUMBBI NUMBER Salem Unit 2 05000311 03 02 98 98 004 00 04 01 98 FACILITY NAME DOCKET NUMBBI ----OPERATING 4 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check one or more) 111 I MODE (9) 20.2201(b) 20.2203(a11211vl x 50. 73(a)(2)(i)
- 50. 73(a)(2)(viii)
POWER 000 20.2203(a)(1 I 20.2203(a)(3)(i)
- 50. 73(a)(2)(iil 50.73(a)(2)(xJ LEVEL (101 20.2203(a)(2Jlil 20.2203(a)(3)(ii)
- 50. 73(a)(2)(iii) 73.71 -20.2203(a)(2)(iil 20 .2203(11)(4)
- 50. 73(a)(2)(iv)
OTHER 20.2203(a)(2Jliiil 50.36(c)(1)
- 50. 73(a)(2)(v)
Specify In Abetract below or In NRC Form 366A 20.2203(a)(2)(ivJ 50.36(c)(2)
- 50. 73(e)(2J(viiJ LICENSEE CONTACT FOR THIS LER (12) NAME TELEPHONE NUMBBI Onolude Alu Code) Brooke Knieriem, Licensing Engineer (609) 339-1782 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13) CAUSE SYSTEM COMPONENT MANUFACT..ull REPORT AllLE I CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED (141 EXPECTED MONTH DAY YEAR IYES INO SUBMISSION (If yes. complete EXPECTED SUBMISSION DATE). DATE 115) ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 11ingle-11paced typeWTitten li11e11) (16) This LER documents the failure of Salem Units 1 and 2 to comply with the requirements of Technical Specifications (TS) 4.11.1.1.2, Radioactive Effluents, and TS 3 .3 .3. 8, Radioactive Liquid Effluent Monitoring and Instrumentation.
TS 4.11.1.1.2 requires that the results of radioactivity analyses be used in accordance with the Off site Dose Calculation Manual (ODCM) to assure that the release concentrations are maintained within TS limits. Salem TS 3 .3 .3. 8 requires that radioactive effluent monitoring instrumentation channel alarm and trip setpoints be determined in accordance with the ODCM. Contrary to these requirements, release rate calculations and radioactive effluent monitoring channel setpoints were identified that employed a Safety Factor different from that specified by the ODCM. This event is reportable under 10CFRS0.73(a)
(2) (i) (B) I any operation or condition prohibited by the plant's TS. Although instances were identified in which the Safety Factor used was less conservative than the Safety Factor. in the ODCM, no instances were identified in which TS concentration limits for release were exceeded.
The apparent cause of this event was an organizational deficiency in the implementation of the Radioactive Effluents/ODCM program. A contributing factor was a lack of understanding by station personnel of the role of the ODCM in the licensing basis. Corrective actions were taken to correctly document the Safety Factor in the ODCM and to correct Safety Factor discrepancies between the ODCM, the implementing procedure, and the Radioactive Effluents TS (RETS) software.
Other corrective actions will be taken to address programmatic and personnel issues identified as a result of this event. NRC FORM 366 (4-961
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- NRC FORM 366A (4-96) U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER) . TEXT CONTINUATION FACILITY NAME 111 DOCKET NUMBER 121 SALEM UNIT 1 05000272 TEXT (If more space is required, use additional copies of NRC Form 366AI 11 7 I PLANT AND SYSTEM IDENTIFICATION Westinghouse
-Pressurized Water Reactor Liquid Waste System (LWS) {WD/-}* Chemical and Volume Control System (CVCS) {CB/-}* LER NUMBER 161 YEAR I SEQUENTIAL.
I RIMSON NUMBER NUWllR 98. -004 -00 PAGE 131 2 OF 5
- Energy Industry Identification System (EIIS) codes and component function identifier codes appear as {SS/CCC}.
CONDITIONS PRIOR TO OCCURRENCE At the time of occurrence, Salem Unit 1 was in Mode 4 (Hot Shutdown) and Unit 2 was in Mode 5 (Cold Shutdown) . DESCRIPTION OF OCCURRENCE During a root cause investigation of a related event that occurred on February 24, 1998, violations of Salem TS 4.11.1.1.2, Radioactive Effluents, and TS 3.3.3.8, Radioactive Liquid Effluent Monitoring And Instrumentation, were identified.
These violations first occurred on January 3, 1996, when the Offsite Dose Calculation Manual (ODCM) was revised by Revision 10 to add a Safety Factor to the radioactive effluent calculation used to determine radioactive liquid effluent monitor setpoints and release *rates. The Safety Factor was added to account for non-gamma emitting radionuclides that cannot be detected by installed radiation monitoring equipment.
Prior to this revision, the ODCM did not use a Safety Factor in these calculations.
However, a Safety Factor was used by the implementing procedure SC.CH-TI.ZZ-0140(Q), Radiological Liquid Effluent Discharges, and in the RETS software used to perform the calculations.
This did not constitute a violation of the TS requirement to perform these calculations in accordance with the ODCM because the calculation methodology the procedure and in the RETS software used the ODCM methodology, but added its own Safety Factor for additional conservatism.
At the time the revision to the ODCM was implemented, station personnel did not recognize that the Safety Factor used in the RETS effluent software, the radioactive effluent implementing procedures, and to determine the radioactive liquid effluept monitoring instrumentation setpoints, did not agree with the ODCM. Station personnel also did not recognize the impact of that condition on the licensing basis. Specifically the requirement of TS 4 .11. 1. 1. 2 to use the results of radioactivity analyses in accordanc.e with the ODCM to assure that release concentrations are maintained within TS limits; and the requirement of TS 3.3.3.8 to determine radioactive effluent monitoring instrumentation channel alarm setpoints in accordance with the ODCM was not recognized.
From the time that ODCM Revision 10 was implemented on January 3, 1996, until the Safety Factors in the ODCM, the procedure, and the software were brought into agreement on October 23, 1997, surveillances performed to satisfy TS 4.11.1.1.2 were not performed in accordance with the ODCM and therefore constituted violations of TS. Additionally, during that time period, radioactive effluent monitoring instrumentation channel alarm setpoints were not set accordance with the ODCM, constituting a violation of TS 3.3.3.8. During the implementation of ODCM Revision 10, the Safety Factor itself was incorrectly documented in the ODCM. The error in the O.DCM revision communicated the Safety Factor as [.25) vice [1-.25 or .75) and resulted in multiplying release rate and setpoint by [.25) NRC FORM 366A (4-95)
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- NRC FORM 366A 14-96) U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (11 SALEM UNIT 1 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER 121 LER NUMBER (61 YEAR 1
- SEQUENTIAL I RElllGION NUMBBI N\.r.elR 05000272 98 -004 -00 TEXT (If more space is required.
use additional copies of NRC Form 366AI (17) DESCRIPTION OF OCCURRENCE (Cont.) PAGE (31 3 OF 5 instead of [.75]. Since the link between the the ODCM and the TS was not recognized, the effect of this error was not immediately felt. The error was first identified on September 9, 1996, by a controls engineer.
This engineer determined that the conservative Safety Factor would likely result in numerous Control Room alarms because radiation monitor setpoints would be set to 25\ of their previous values. Based upon discussions with the author of ODCM Revision 10, the controls engineer determined that the intent of the revision was to use a Safety Factor with a value of [.75] and not [.25]. The controls engineer then used the "intended" value [.75] for .Safety F.actor and not the actual value of [. 25] for setpoint determination.
Again, the controls engineer did not recognize the link between the ODCM and the TS. Because the setpoints were changed to a value derived using the "intended" and not the actual Safety Factor value of the revision to the ODCM, the setpoints remained in a state of compliance with TS 3.3.3.8 until this discrepancy was corrected on March 14, 1998. When apprised of the Safety Factor error, the author of Revision 10 incorrectly concluded that the design engineers were using the Safety Factor outside of its intended purpose, that it was derived from radioactive liquid waste data, and that it was not intended for use with other radioactive waste monitors.
This demonstrated a clear lack of understanding that TS 3.3.3.8 encompasses all radioactive liquid effluent monitoring instrumentation and is not restricted to liquid waste effluent monitors.
From that point on, the author of the ODCM revision considered that this issue was restricted to the incorrectly docu'rnented Safety Factor in the ODCM and did not recognize that a condition adverse to quality existed. Although identified, the Safety Factor documentation error in the ODCM was not corrected at that time. On September 19, 1997, a Quality Assurance audit identified the safety Factor discrepancy between the ODCM, the procedure, and the RETS software.
However, the audit failed to recognize the relationship between the TS and the ODCM, or to identify that the station was not in compliance with TS. As a result of this audit, the RETS software was modified on September 19, 1997, to obtain agreement with the ODCM. In error the Safety Factor was changed to [.75] and not [.25] as documented in the ODCM. The Safety Factor in procedure SC.CH-TI.ZZ-0140(Q) was revised on September 23, to a value of [.25] to conform to the ODCM Safety Factor. The error in the Safety Factor in the RETS software was identified and was again changed in October 23, from [.75] to [.25] to conform with the ODCM. At that time the procedure and the RETS software were both in compliance with the Safety Factor in the ODCM. From that point forward, surveillances performed to satisfy TS 4.11.1.1.2 using the RETS software and procedure SC.CH-TI.ZZ-0140(Q) would comply with TS, but with an unneccesarily conservative Safety Factor. Radioactive liquid effluent monitor setpoints remained at values calculated using the [.75] Safety Factor. On January 3, 1998, during the preparation of two radioactive liquid release permits, Chemistry Department personnel altered the permits by changing the Safety Factor used by the RETS software from [.25] to [l]. The Safety Factor was changed to remove a quarterly dose projection "flag" that was generated by the RETS software.
The "flag" alerts Chemistry Department personnel when additional processing of the effluent is necessary prior to release to ensure that the dose limit is not exceeded.
The Safety Factor was changed as a work-around by the Chemistry Department personnel who recognized that the flag was caused by the overly conservative Safety Factor of [.25] used by the software.
Because the ODCM does not require the use of a Safety Factor in the dose calculation required by TS 4.11.1.3, this calculation was correctly performed to ensure that dose limits of TS 3.11.1.3 and 10CFR20 were not exceeded.
NRC FORM 366A (4-95)
- NRC FORM 366A (4-96) U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) SALEM UNIT 1 LICENSEE EVENT REPOR1" (LER) TEXT CONTINUATION DOCKET NUMBER 121 LER NUMBER (6) YEAR I SEQUENTIAL I REVISION NUMBER NLMll&I 05000272 98 -004 -00 TEXT (If more space is required, use additional copies of NRC Form 366A) (171 DESCRIPTION OF OCCURRENCE (Cont.) PAGE (3) 4 OF 5 The RETS software used the same formula to calculate the release rate. Because the release rate calculation in the ODCM (since the implementation of Revision 10) required the use of a [.25] Safety Factor, TS 4.11.1.1.2 was violated when the Safety Factor was changed to [1] . A subsequent review of these releases demonstrated that the concentration limits of TS 3.11.1.1 were not exceeded.
On March 14, 1998, ODCM revision 11 was approved which incorporated the [.75] Safety Factor into the setpoint calculation.
This brought the Safety Factor used to calculate release rate and radioactive liquid effluent monitor setpoints in the procedure, the RETS software, and the ODCM into agreement.
Addit.l.onally, this action brought Radioactive Liquid Effulent Monitor setpoints into alignment with the ODCM and TS 3.3.3.8 was satisfied.
CAUSE OF OCCURRENCE The apparent cause of this event is an organizational deficiency in the implementation of the Radioactive Effluents/ODCM program as evidenced by inadequate program monitoring and management as well as a lack of program evaluation.
Contributing to this occurrence was an overall lack of understanding by station personnel of the role of the ODCM in the station's licensing basis. PRIOR SIMILAR OCCURRENCES A review of LERs for Salem Units 1 and 2 issued in the last two years identified one LER that discussed a related occurrence.
LER 311/97-007-00 reported a violation to TS 3.3.3.8, Radioactive Liquid Effluent Monitoring Instrumentation.
This violation was caused by the failure of station personnel to independently verify the radioactive liquid waste release valve lineup as a compensatory measure required by TS when the radioactive liquid effluent monitoring instrumentation is out of SAFETY CONSEQUENCES There were no safety consequences as a result of this event. A review of the releases performed between the implementation of Revision 10 to the ODCM on January 3, 1996, and the time that the discrepancy between the ODCM, the RETS software, and the procedure were corrected on October 23, 1997; and a review of the releases on January 3, 1998, revealed that in no case were the concentration limits of TS 3.11.1.1 exceeded.
Additionally, although Effluent Radiation Monitor setpoints were not set in accordance with the ODCM as required by TS, at no time were the setpoints set to a value that would have permitted the concentration limits of TS 3.11.l.1 to be exceeded for batch or continuous release. CORRECTIVE ACTIONS 1. The releases performed between the implementation of Revision 10 to the ODCM on January 3, 1996, and the time that the discrepancy between the ODCM, the RETS software, and the procedure was corrected on October 23, 1997; and the releases on January 3, 1998 were reviewed to verify that the concentration limits of TS 3.11.1.1 were not exceeded.
- 2. On March 14, 1998, the Safety Factor was corrected in the ODCM by implementation of Revision 11. Additionally, the implementing procedure and RETS software were revised to align with this change. NRC FORM 366A (4-95)
- NRC FORM 366A (4-95) U.S. NUCLEAR REGULATORY COMMISSION FACILITY NAME (1) SALEM UNIT 1 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION DOCKET NUMBER (2) LER NUMBER (6) YEAR I SEQUENTIAL I REVISION NUMBER NUMBE!I 05000272 98 *-004 00 TEXT (If more space is required, use additional copies of NRC Form 366A) ( 17) CORRECTIVE ACTIONS(Cont.)
PAGE (3) 5 OF 5 3. Radioactive liquid effluent monitors were declared inoperable because of the incorrect Safety Factor applied to their setpoint.
Following implementation of ODCM revision 11, the setpoints were restored to compliance with the ODCM. 4. Appropriate personnel involved with the errors have been held accountable in accordance with PSE&G's procedures and policies.
- 5. Improvements to ODCM effluents program controls and review process will be implemented to ensure that adequate interface exists between design engineering, effluents software, radiation monitor set points, and the implementing procedures.
(00980224081, CRCA 12, to be completed by 6/15/98) 6. Training will be provided to appropriate personnel on the effluents program and its licensing basis. (00980224081, CRCA 04, to be completed by 6/15/98, CRCA 29, to be completed by 9/30/98.)
- 7. An independent review of the ODCM will be performed to ensure that it is consistent with available regulatory guidance.
(00980224081, CRCA 17,to be completed by 7/15/98) 8. Ownership for the ODCM has been formally defined and assigned.
NRC FORM 366A (4-95)