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 Start dateReport dateSiteReporting criterionSystemEvent description
ENS 5723724 July 2024 12:02:00South Texas10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater

The following information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: A Notification of Unusual Event was declared by South Texas Project Unit 1 at 0718 CDT for emergency action level (EAL) SU.1, loss of all offsite power for greater than 15 minutes, following a fire in the switchyard. Unit 1 tripped following the loss of power and is stable in Mode 3. Unit 2 reduced power to 90 percent but was otherwise unaffected by this event. Offsite services responded to the switchyard fire. The fire was extinguished at 0925 CDT. There is no radioactive release and no threat to public safety. The licensee notified state and local authorities and the NRC senior resident inspector. Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email).

  • * * UPDATE ON 7/24/2024 AT 1154 EDT FROM CHRIS VAN FLEET TO ERNEST WEST * * *

The following information was provided by the licensee via phone and email: At 0702 CDT on 7/24/2024, with Unit 1 in Mode 1 at 100 percent power, the Unit 1 reactor automatically tripped due to loss of offsite power. The trip was not complex, with all systems responding normally post-trip. No equipment was inoperable prior to the event that contributed to the event or adversely impacted plant response to the scram. Operations responded and stabilized the plant. Decay heat is being removed by steam generator power operated relief valves (PORV). Unit 2 was reduced in power to approximately 90 percent power due to conditions in the switchyard. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. Notified R4DO (Azua)

  • * * UPDATE ON 7/24/2024 AT 1259 EDT FROM CHRIS MCRARY TO ERNEST WEST * * *

The following is a summary of information provided by the licensee via phone: At 1146 CDT, South Texas Project Unit 1 terminated the previously declared Notification of Unusual Event due to restoration of an offsite source of electrical power. Notified R4DO (Azua), NRR EO (McKenna), IR MOC (Crouch), DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email).

  • * * UPDATE ON 7/24/2024 AT 1555 EDT FROM CHRIS VAN FLEET TO ERNEST WEST * * *

The following information was provided by the licensee via phone and email: For the 10 CFR 50.72(b)(3)(iv)(A) reporting requirements: At 0702 CDT on 7/24/2024, with both Unit 1 and 2 in Mode 1 at 100 percent power, the South Texas Project (STP) north and south switchyard electrical buses were de-energized. In Unit 1, all emergency diesel generators (EDGs) 11, 12, and 13 automatically started in response to loss of offsite power on train `A', `B', and `C' engineered safety feature (ESF) buses. Also in Unit 1, trains `A', `B', and `C' of the auxiliary feedwater (AFW) system automatically started. In Unit 2, EDG 22 automatically started in response to loss of offsite power on the train `B' ESF bus. Also in Unit 2, train `B' of the AFW system automatically started. This event is reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in the valid actuation of a pressurized water reactor auxiliary feedwater system (50.72(b)(3)(iv)(B)(6)) and emergency alternating current (AC) electrical power system (50.72(b)(3)(iv)(B)(8)). There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. For the 10 CFR 50.72(b)(2)(xi) reporting requirement: A news release was completed at 1140 CDT on 7/24/2024, by South Texas Project on the declaration of the Unusual Event. This media release is being reported in accordance with 10 CFR 50.72(b)(2)(xi): Any event or situation, related to the health and safety of the public or onsite personnel, or protection of the environment, for which a news release is planned or notification to other government agencies has been or will be made. Notified R4DO (Azua)

ENS 5722110 July 2024 11:28:00Peach Bottom10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Protection System
Main Condenser
The following information was provided by the licensee via phone and email: At 0728 EDT on July 10, 2024, with Unit 2 in Mode 1 at 24 percent power, the reactor automatically scrammed due to a manual turbine trip. The (reactor) scram was not complex with all systems responding normally. Reactor vessel level reached the low-level set-point following the scram, resulting in valid Group 2 and Group 3 containment isolation signals. Due to the reactor protection system actuation while critical, this event is being reported as a four hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for the Group 2 and Group 3 isolations. Operations responded using emergency operating procedures and stabilized the plant in Mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 3 was not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 572159 July 2024 01:25:00Vogtle10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Steam Generator
Reactor Coolant System
Feedwater
Reactor Protection System
Residual Heat Removal
The following information was provided by the licensee via email: At 2125 EDT on 07/08/2024, with Unit 3 in Mode 1 at 100 percent power, the reactor was manually tripped due to main feedwater pump `A' miniflow valve failing open, which resulted in lowering steam generator water level. Additionally, an automatic safeguards actuation occurred due to the cooldown of the reactor coolant system. The trip was not complex, with all safety systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed by the passive residual heat removal heat exchanger. Units 1, 2, and 4 are not affected. Due to the core makeup tank actuation, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). The reactor protection system actuation while critical is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, this event is reportable per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid containment isolation actuation and a valid passive residual heat removal heat exchanger actuation. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the main feedwater pump 'A' miniflow valve failing open was unknown and under investigation at the time of the notification of this event to the NRC.
ENS 572148 July 2024 19:21:00Watts Bar10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Protection System
Auxiliary Feedwater
Main Condenser
The following information was provided by the licensee via phone and email: At 1521 EDT on July 8, 2024, with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main turbine trip. The (reactor) trip was not complex with all systems responding normally post trip. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the steam dump system and the auxiliary feedwater (AFW) system. Unit 2 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the AFW system (an engineered safety feature) is being reported as an eight-hour report under 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The specific cause of the turbine trip is under investigation by the licensee.
ENS 5719527 June 2024 12:04:00Cook10 CFR 50.72(b)(3)(iv)(A), System ActuationSteam Generator
Reactor Coolant System
Auxiliary Feedwater
Main Condenser
Control Rod
The following information was provided by the licensee email: On June 27, 2024, at 0804 (EDT), D.C. Cook Unit 2 had an automatic start of the turbine driven auxiliary feedwater pump (TDAFP) following a controlled down power and manual reactor trip at approximately 17 percent power. The automatic start of the TDAFP was due to a steam generator water level 'low low' signal following the reactor trip. The down power and trip were performed in accordance with normal shutdown procedures to comply with the required action C.1 of technical specification 3.4.13, 'reactor coolant system operational leakage.' Reference event notification number EN57194. An automatic start of the TDAFP is an eight hour report per 10CFR 50.72(b)(3)(iv)(A). Unit 2 is being supplied by offsite power. All control rods fully inserted. Steam generators are being fed by both motor driven auxiliary feedwater pumps. Decay heat is being removed via the steam dump system to the main condenser. Preliminary evaluation indicates plant systems functioned normally following the reactor trip. D.C. Cook Unit 2 remains in Mode 3 to repair the previously reported reactor coolant system leakage through valve 2-QRV-251, 'CVCS (chemical and volume control system) charging pumps discharge flow control' valve packing. The NRC Resident Inspector has been notified.
ENS 5718722 June 2024 11:28:00Vogtle10 CFR 50.72(b)(3)(iv)(A), System ActuationReactor Protection SystemThe following information was provided by the licensee via email: At 0728 EDT on 06/22/2024, with Unit 2 in Mode 3 at zero percent power and the reactor trip breakers closed, a manual actuation of the RPS was initiated during the withdrawal of the shutdown rods in preparation for Mode 2. This was procedurally directed due to a shutdown rod being misaligned from the other rods in the bank due to a malfunction. Units 1, 3 and 4 were not affected. Due to the manual actuation of the RPS, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5717516 June 2024 17:33:00Waterford10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Feedwater
Reactor Protection System
Decay Heat Removal
Main Condenser
Control Rod
The following information was provided by the licensee via email: On June 16, 2024, at 1233 CDT, Waterford Steam Electric Station Unit 3 was operating at 93 percent power when an automatic reactor trip occurred. Immediately following the reactor trip, emergency feedwater (EFW) actuated automatically. The unit is currently in Mode 3. All control rods fully inserted. Decay heat removal is via the main condenser. Preliminary evaluation indicates that all plant systems functioned normally after the reactor trip, except steam generator (SG) feedwater pump 'A' tripped and SG '1' main feed regulatory controller went to manual. Steam generator water levels are being controlled with the SG feedwater pump 'B'. The cause of the trip is currently being investigated. This event is being reported as a 4-hour non-emergency notification in accordance with 10 CFR 50.72(b)(2)(iv)(B) as an actuation of the reactor protection system when the reactor is critical and as an 8-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as a valid actuation of the EFW system. The NRC Resident Inspector has been notified.
ENS 571593 June 2024 04:51:00Oconee10 CFR 50.72(b)(3)(iv)(A), System ActuationSteam Generator
Reactor Coolant System
Feedwater
Main Steam
Emergency Feedwater System
The following information was provided by the licensee via phone and email: At 0051 EDT on June 3, 2024, with Unit 3 in Mode 3 at 0 percent power, an actuation of the emergency feedwater system (EFW) occurred as main steam pressure was being lowered as part of reactor coolant system (RCS) cooldown for a planned shutdown. The reason for the EFW auto-start was lowering levels in the 3A and 3B steam generators following loss of the operating main feedwater pump. The main feedwater pump automatically tripped when main steam pressure was lowered below the automatic feedwater isolation system (AFIS) actuation setpoint before AFIS channels were taken to bypass. The 3A and 3B motor driven emergency feedwater pumps automatically started as designed when the low steam generator level signal was received for the 3A and 3B steam generators. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the EFW system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5714829 May 2024 10:24:00North Anna10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Protection System
Auxiliary Feedwater
Control Rod
The following information was provided by the licensee via email and phone: On May 29, 2024, at 0624 EDT, Unit 1 automatically tripped from 100 percent power due to a negative rate trip. The unit has been stabilized in mode 3 at normal operating temperature and pressure. The reactor trip was uncomplicated and all control rods fully inserted into the core. This reactor protection system actuation is reportable per 10 CFR 50.72(b)(2)(iv)(B). The auxiliary feedwater pumps actuated as designed because of the reactor trip and is reportable per 10 CFR 50.72(b)(3)(iv)(A) for a valid engineered safety feature (ESF) actuation. Decay heat is being removed by the condenser steam dump system and Unit 1 is in a normal shutdown electrical lineup. Unit 2 was not affected by this event. The NRC Resident has been notified.
ENS 5714123 May 2024 16:46:00Quad Cities10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Protection System
Main Condenser
The following information was provided by the licensee via email: At 2223 CDT on May 23, 2024, with Quad Cities Unit 2 at 38 percent power, the reactor automatically tripped due to a turbine trip signal resulting in main stop valve closure, creating a valid reactor protection system signal. Reactor vessel level reached the low-level set-point following the scram, resulting in valid Group II and Group III containment actuation signals. The trip was not complex with all systems responding as expected post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for the Group II and Group III isolation. Operations responded using their emergency operating procedures and stabilized the plant in mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 remains at 100 percent power. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 2 was at a reduced power for maintenance.
ENS 5713219 May 2024 04:30:00Beaver Valley10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Feedwater
Reactor Protection System
Auxiliary Feedwater
Main Condenser
Control Rod
The following information was provided by the licensee via email: At 0030 (EDT) on 5/19/24, with Beaver Valley Unit 1 in mode 1 at 14 percent power, the reactor was manually tripped due to inability to control the A steam generator water level. The trip was not complex, with all systems responding normally post-trip. The turbine driven auxiliary feedwater pump automatically started on a valid actuation signal. All control rods inserted into the core. Operations responded and stabilized the plant. Decay heat is being removed by the feedwater system and the main condenser. Beaver Valley Unit 2 is unaffected. Due to the reactor protection system system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the emergency safety feature system actuation (automatic start of the turbine driven auxiliary feedwater pump) while critical, this event is being reported as an eight-hour, non-emergency notification per 10CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been verbally notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 1 is stable on off-site power, normal configuration. All emergency systems are available.
ENS 5712815 May 2024 08:27:00Cook10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Reactor Protection System
Auxiliary Feedwater
Main Turbine
The following information was provided by the licensee via email: On May 15, 2024 at 0427 EDT, DC Cooks Unit 2 reactor was manually tripped due to difficulty maintaining steam generator water levels. DC Cook Unit 2 had removed the main turbine from service at approximately 0354 EDT during a planned down-power to repair a steam leak on the high pressure turbine right outer steam/stop control valve upstream drip pot. Stable steam generator water levels were unable to be maintained. As a result, DC Cook Unit 2 was manually tripped with reactor power stabilizing at approximately 20 percent. This notification is being made in accordance with 10 CFR 50.72(b)(2)(iv)(B), Reactor Protection System actuation as a four hour report, and under 10 CFR 50.72(b)(3)(iv)(A), specified system actuation of the Auxiliary Feedwater System, as an eight hour report. The reactor trip was not complicated and all plant systems functioned normally. The DC Cook NRC Resident Inspector was notified.
ENS 5712412 May 2024 21:41:00South Texas10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Reactor Protection System
Emergency Diesel Generator
Main Turbine
Control Rod

The following information was provided by the licensee via email and phone: At 1641 CDT on May 12, 2024, with Unit 2 in Mode 1 at 15 percent power, the reactor automatically tripped due to a unit auxiliary transformer lockout. During the trip, all control rods fully inserted. The cause of the transformer lockout is currently unknown. Emergency diesel generator (EDG) 21 and 23 actuated and all three engineered safety feature (ESF) busses were energized. All equipment responded as expected except for steam generator power operated relief valve (PORV) 2C which failed to open when required in automatic, and the load center (LC) E2A output breaker which failed to close automatically but was closed manually. Steam generator PORV 2C did open when placed in manual, although it subsequently failed to full open and was then closed. Primary system temperature and pressure are currently being maintained at 567 degrees/2235 psig following start of reactor coolant pumps 2A and 2D. Due to the reactor protection system actuation (RPS) while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the emergency diesel generators. There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: South Texas Project Unit 2 was in Mode 1 at 15 percent power due to performance of testing and analysis on the main turbine prior to the RPS actuation.

  • * * UPDATE FROM ROBERT DEWOODY TO BRIAN P. SMITH ON MAY 22, 2024 AT 1805 EDT * * *

The following information was provided by the licensee via email and phone: South Texas Project is submitting the following correction to the event notification: The steam generator (SG) power operated relief valve (PORV) 2C did not fail to open automatically. System pressure during this event did not reach the automatic setpoint for the PORV (1225 psi), and there was no demand for it to open automatically. During the event, SG PORV 2C was taken to manual and it went full open when the up button was pushed slightly. It went closed when the down button was pressed to close it manually. In addition, the load center E2A output breaker initially failed to close automatically, however, after operations placed it in pull-to-lock and returned the hand switch to automatic, it closed automatically. Notified R4DO (Dixon).

ENS 5712211 May 2024 21:55:00Waterford10 CFR 50.72(b)(3)(iv)(A), System ActuationSteam Generator
Feedwater
Reactor Protection System
Control Rod
The following information was provided by the licensee via phone and email: At 1655 CDT, Waterford Steam Electric Station, Unit 3 was in Mode 3 with all control rod element assemblies (CEA) fully inserted with reactor trip circuit breakers closed and individual CEA disconnects open for plant startup. During the performance of emergency feedwater surveillance testing, reactor protection system (RPS) trip set point and emergency feedwater actuation system (EFAS) initiation set point for steam generator level low was exceeded for steam generator 1. Preliminary evaluation indicates that all plant systems functioned normally. The unit is currently stable in Mode 3. All control rods remain fully inserted. This event is being reported as a eight-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as valid actuation of the RPS and emergency feedwater systems. The NRC Resident Inspector has been notified.
ENS 571075 May 2024 08:38:00Braidwood10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Reactor Protection System
Auxiliary Feedwater
Main Condenser

The following information was provided by the licensee via email and phone: At 0338 CDT, with the unit 1 in mode 1 at 6 percent power, the reactor automatically tripped due to lowering steam generator water level. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for an actuation of the auxiliary feedwater system. Operations responded using procedure 1BwEP-0 and stabilized the plant in mode 3. Decay heat is removed by steam dumps via the main condenser. 1A and 1B auxiliary feedwater pumps were actuated manually prior to the reactor trip in an attempt to restore steam generator water level. Unit 2 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 07/05/2024 AT 0450 EDT FROM MATTHEW WHITE TO TENISHA MEADOWS * * *

The following information was provided by the licensee via email and phone: At 0338 CDT, with the unit 1 in mode 2 at 3 percent power, the reactor automatically tripped due to lowering steam generator water level. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and 10CFR50.72(b)(3)(iv)(A) for an actuation of the auxiliary feedwater system, eight-hour notification. Operations responded using procedure 1BwEP-0 and stabilized the plant in mode 3. Decay heat is being removed by steam dumps via the main condenser. 1A and 1B auxiliary feedwater pumps were actuated manually prior to reactor trip in an attempt to restore steam generator water level. Unit 2 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Notified R3DO (Hartman)

ENS 5709025 April 2024 03:15:00Browns Ferry10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Reactor Coolant System
Feedwater
High Pressure Coolant Injection
Reactor Protection System
Main Steam Isolation Valve
Primary Containment Isolation System
Reactor Core Isolation Cooling
Emergency Core Cooling System
The following information was provided by the licensee via email: On 4/24/2024 at 2215 CDT, Browns Ferry Unit 1 experienced an automatic reactor scram. The cause of the scram is currently under investigation. The main steam isolation valves (MSIVs) remain open with the main turbine bypass valves controlling reactor pressure. The reactor feedwater pumps are in service to control reactor water level. Primary containment isolation systems (PCIS) Groups 2, 3, 6, and 8 isolation signals were received. Upon receipt of these signals, all components actuated as required. Following the reactor scram, due to reactor water level reaching minus 45 inches, both high pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) initiation signals were received, and both initiated as designed. All safety systems operated as expected. This event requires a 4-hour report per 10 CFR 50.72(b)(2)(iv)(A), `Any event that results or should have resulted in emergency core cooling system (ECCS) discharge into the reactor coolant system as a result of a valid signal except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation. This event requires a 4-hour report per 10 CFR 50.72(b)(2)(iv)(B), `Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation. This event requires an 8-hour report per 10 CFR 50.72(b)(3)(iv)(A), `Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B): 1) Reactor protection system (RPS) including: reactor scram or reactor trip. 2) General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs). 4) ECCS for boiling water reactors (BWRs) - high-pressure coolant injection (HPCI). 5) BWR reactor core isolation cooling system (RCIC). All safety systems operated as expected. At no time was public health and safety at risk. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Units 2 and 3 were not affected.
ENS 5708320 April 2024 12:04:00LaSalle10 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel GeneratorThe following information was provided by the licensee via phone and email: At 0704 CDT on 4/20/24 with Unit 1 in Mode 1 at 100 percent power, an actuation of the emergency AC power system, specifically the Division 1 and Division 3 emergency diesel generators (EDGs) occurred during an unexpected loss of the Unit 1 system auxiliary transformer (SAT). The cause of the emergency AC power system auto-start was an unexpected loss of the Unit 1 SAT during switchyard maintenance. Bus 141Y did not fast transfer as designed resulting in the actuation of the Division 1 EDG. Division 3 EDG actuation is expected for this condition. The Division 1 and Division 3 EDGs automatically started as designed when the emergency AC power system valid actuation signal was received. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the emergency AC power system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified." The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Division 1 and Division 3 EDGs will remain in operation and loaded until the Unit 1 SAT is restored. This event resulted in the plant entering an unplanned 72 hour limiting condition for operation (LCO) in accordance with technical specification 3.8.1. The licensee is investigating the cause of the unexpected loss of the Unit 1 SAT and the failure of the bus 141Y fast transfer.
ENS 5707513 April 2024 04:35:00Beaver Valley10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Feedwater
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Main Condenser
Control Rod
The following information was provided by the licensee via phone and email: At 0035 EDT on April 13, 2024, with Unit 1 at 97 percent power, the reactor automatically tripped due to 1 of 3 reactor coolant pump (RCP) low flow reactor trip (signal) associated with a loss of the A and B 4160 volt normal buses. Auxiliary feedwater and the 1-1 emergency diesel generator (EDG) automatically started on valid actuation signals. The 1-1 EDG sequenced on to supply all required loads per plant design. All control rods fully inserted and the trip was not complex with all systems responding normally post-trip. Operators have responded and stabilized the unit in Mode 3 (Hot Standby). Decay heat is being removed by discharging steam to the main condenser via the condenser steam dump system with steam generators being supplied by the main feedwater system. Unit 2 is not affected by the event. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the valid actuations of auxiliary feedwater and the 1-1 EDG, this event is reportable in accordance with 10 CFR 50.72(b)(3)(iv)(A). There was no impact to the health and safety of the public or plant personnel. The NRC senior resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Power for the A-E Bus is on the 1-1 EDG. The D-F Bus is on offsite power. One electrical train of offsite power is down.
ENS 5705828 March 2024 01:46:00Quad Cities10 CFR 50.72(b)(3)(iv)(A), System ActuationReactor Protection System
Control Rod
The following information was provided by the licensee via email: At 2046 (CDT) on 3/27/24 with the unit 2 in Mode 5 at 0% power, an actuation of the Reactor Protection System occurred during testing of the scram discharge volume. The cause of the Reactor Protection System actuation was leakage of water into the scram discharge volume causing a high level condition while drains were isolated for testing. The Reactor Protection System automatically actuated as designed when the high scram discharge volume signal was received. All rods were previously fully inserted and the Control Rod Drive system was shutdown. No rod movement occurred due to the actuation. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Reactor Protection System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5705326 March 2024 16:15:00Grand Gulf10 CFR 50.72(b)(3)(iv)(A), System ActuationReactor Coolant System
Reactor Protection System
The following information was provided by the licensee via phone and email: On March 26, 2024 at 1115 CDT, Grand Gulf Nuclear Station experienced an actuation of the reactor protection system (RPS) due to high reactor coolant system pressure. The plant was in Mode 4 at zero percent power and performing scram time testing. All rods were fully inserted at the time of the RPS actuation, and all required equipment responded as designed. This actuation is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A). The cause of the event is under investigation. The NRC resident inspector has been notified.
ENS 5704724 March 2024 23:34:00Palo Verde10 CFR 50.72(b)(3)(iv)(A), System ActuationSteam Generator
Feedwater
Emergency Diesel Generator
Auxiliary Feedwater
The following information was provided by the licensee via email: At 1634 MST on March 24, 2024, an engineered safety features (ESF) service transformer deenergized resulting in a loss of power to the Unit 2 Train B 4.16 kV Class 1E Bus. The Unit 2 Train B emergency diesel generator (EDG) automatically started and energized the Unit 2 Train B 4.16 kV Class 1E Bus. As a result of the loss of power on the Unit 2 Train B 4.16 kV Class 1E Bus and subsequent load sequencing after the Unit 2 Train B EDG started, the Unit 2 Train B auxiliary feedwater (AFW) pump automatically started as designed. The Train B AFW pump was not needed for steam generator level control and no auxiliary feedwater valves repositioned. The Train B AFW Pump did not supply feedwater to the steam generators. All systems operated as designed. Per the emergency plan, no classification was required due to the event. Units 1, 2, and 3 remain in Mode 1 at 100 percent power. The 4.16 kV Class 1E Buses in Units 1 and 3 were not affected by the deenergization of the ESF service transformer. The cause of the ESF service transformer being deenergized is under investigation. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of emergency AC electrical power systems and auxiliary feedwater system. The NRC Resident Inspectors have been informed.
ENS 5704623 March 2024 04:04:00Fermi10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Protection System
Primary containment
Reactor Pressure Vessel
Main Condenser
Control Rod
Main Steam

The following information was provided by the licensee via email: At 0004 EDT on March 23, 2024, with the unit in Mode 1 at 23 percent power, the reactor automatically scrammed due to high reactor pressure vessel pressure when the turbine bypass valves unexpectedly closed while attempting to lower generator MW to 55 MWe to support shutdown for a refueling outage. The scram was not complex, with systems responding normally post-scram, with the exception of the pressure control system. The transient occurred while lowering on turbine speed/load demand which caused a rise in pressure and power until the reactor protection system setpoint for reactor pressure high was exceeded and resulted in an automatic reactor scram. The plant was preparing to shut down for a refueling outage when the trip occurred. Operations responded and stabilized the plant. Reactor water level is being maintained at normal level. Decay heat is being removed by the main steam system to the main condenser using manual operation of the turbine bypass valves. All control rods inserted into the core. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CPR 50.72(b)(2)(iv)(B). Additionally, received expected (primary containment) isolations for Level 3: Group 13 drywell sumps, Group 15 (traverse in-core probe) TlPs (which was already isolated) and Group 4 (residual heat removal - shutdown cooling) RHR-SDC (which was already isolated). The primary containment isolation event is being reported under 10 CFR 50.72(b)(3)(iv)(A). Also, due to the main turbine bypass valves unexpectedly closing, this is also being reported under 10 CFR 50.72(b)(3)(v)(D). There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 4/22/24 AT 1448 EDT FROM WHITNEY HEMINGWAY TO ADAM KOZIOL * * *

The purpose of this notification is to retract the 10 CFR 50.72(b)(3)(v)(D) reporting criteria of event notification 57046 reported on March 23,2024. Based on further evaluation, Fermi 2 has concluded that there was no event or condition that could have prevented fulfillment of a safety function that was needed to mitigate the consequence of an accident. Although discussed in Chapter 15 of the UFSAR, the turbine bypass valves do not provide a safety related function and are not credited safety related components for accident mitigation. Therefore, Fermi 2 is retracting the 10 CFR 50.72(b)(3)(v)(D) reporting criteria that was included on the March 23, 2024 event notification. Notified R3DO (Betancourt-Roldan)

ENS 5704222 March 2024 04:37:00Waterford10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Feedwater
Reactor Protection System
Emergency Diesel Generator
Main Transformer
Emergency Core Cooling System
Decay Heat Removal
Main Condenser
Control Rod

The following information was provided by the licensee: A Notification of Unusual Event, HU4.4 (see note below) was declared based a fire in the protected area requiring off site assistance to extinguish. The fire was in the main transformer yard. The fire was detected at 2328 CDT on March 21, 2024, and the fire was declared out at 0009 CDT on at March 22, 2024. An automatic reactor trip was initiated due to a loss of offsite power to the "B" train and a failure to automatically transfer from unit auxiliary transformer "B" to startup transformer "B. The licensee notified State and local authorities and the NRC Resident Inspector. The NRC remained in Normal. Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email). NOTE: Due to a typographical error initiating condition HU4.1 was initially recorded for the event. The correct initiating condition is HU4.4 as now shown.

  • * * UPDATE AT 0345 EDT ON 03/22/24 FROM LARRY GONSALES TO BILL GOTT * * *

The licensee terminated the Notification of Unusual Event at 0221 CDT on 3/22/24. The licensee notified the NRC Resident Inspector. Notified R4DO (Gepford), IR-MOC (Grant), NRR-EO (Felts), DHS-SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email).

  • * * UPDATE AT 0420EDT ON 03/22/24 FROM JOHN LEWIS TO BILL GOTT * * *

RPS ACTUATION The following information was provided by the licensee via email: On March 21, 2024, at 2328 CDT, Waterford 3 Steam Electric Station, Unit 3 was operating at 98 percent power when an automatic reactor trip was initiated due to a loss of offsite power to the B train and a failure to automatically transfer from unit auxiliary transformer B to startup transformer B. Emergency feedwater actuation signal 2 (EFAS), safety injection actuation signal (ECCS), containment isolation actuation signal and emergency diesel generators automatically actuated. The unit is currently stable in Mode 3. All control rods fully inserted and all other plant equipment functioned as expected. Forced circulation remains with one reactor coolant pump per loop running. Decay heat removal is via the main condenser. A train safety bus is being supplied by off-site power, and B train safety bus is being supplied by emergency diesel generator B. Following the loss of offsite power to the B train, it was reported that main transformer B and startup transformer B were both on fire. The Emergency Director declared an Unusual Event at time 2337 CDT. The fire was reported extinguished at 0009 CDT on March 22, 2024, and the Unusual Event was terminated at 0221 CDT on March 22, 2024. Offsite assistance was requested. The local fire department responded to the site but the fire was extinguished by the on-shift fire brigade. NRC Region IV management was contacted regarding the emergency plan entry at 0030 CDT on March 22, 2024. This event is being reported as a 4-hour non-emergency notification in accordance with 10 CFR 50.72(b)(2)(iv)(B) as an actuation of the reactor protection system (RPS) when the reactor is critical and as an 8-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as valid actuation of the EFW system, ECCS, Containment Isolation and Emergency Diesel Generators. The NRC Resident Inspector has been notified. Notified R4DO (Gepford)

  • * * RETRACTION OF NOTICE OF UNUSUAL EVENT FROM ON 03/26/24 AT 1721 FROM L. BROWN TO K. COTTON * * *

The initial notification in event notice #57042 by Waterford Steam Electric Station, Unit 3, reported a Notice Of Unusual Event (NOUE) emergency declaration due to a fire in the protected area requiring off site support to extinguish. The basis for retraction of the initial emergency notification is that this event did not meet the definition of a fire in the protected area that requires off site support to extinguish. Guidance provided in Nuclear Energy Institute (NEI) 99-01, Rev. 6 and implemented in Waterfords Emergency Plan procedure, initiating Condition HU4.4 states, The dispatch of an offsite firefighting agency to the site requires an emergency declaration only if it is needed to actively support firefighting efforts because the fire is beyond the capability of the Fire Brigade to extinguish. (NOTE: The Initial Notification Form sent from the Control Room at 2341 CDT on March 21, 2024, requested by and provided to the NRC Headquarter Operations Center via e-mail at 0302 CDT on March 22, 2024, stated that the Emergency Classification had been made on Initiating Condition HU4.4 rather than HU4.1)" When the event occurred on March 21, 2024, the Emergency Director declared an Unusual Event at 2337 CDT and requested offsite support based on the information available at that time including the initial assessment by the fire brigade leader and expected need for offsite support to extinguish the fire. As reported in the 0420 EDT update on March 22, 2024, the fire was reported extinguished at 0009 CDT on March 22, 2024, by the Waterford Fire Brigade without the need of offsite support." Notified R4DO (Kellar).

  • * * UPDATE AT 1209 EDT ON 03/27/24 FROM JOHN LEWIS TO KAREN COTTON * * *

The initial notification in EN 57042 by Waterford Steam Electric Station, Unit 3, reported an emergency declaration of an Unusual Event due to a fire in the protected area requiring off site support to extinguish. The basis for the update to the initial notification is that this event did not meet the definition of a Fire in the Protected Area that requires offsite support to extinguish. As provided in NEI 99-01, Rev. 6 and implemented in Waterfords emergency plan procedure, initiating condition HU4.4 states, The dispatch of an offsite firefighting agency to the site requires an emergency declaration only if it is needed to actively support firefighting efforts because the fire is beyond the capability of the Fire Brigade to extinguish. Additionally, EAL 4.1 for a fire not extinguished within 15 minutes of detection in any Table H-1 fire area was not applicable because the fire did not occur in a Table H-1 fire area. When the event occurred on March 21, 2024, the Emergency Director declared an Unusual Event at 2337 CDT and requested offsite support based on the information available at that time including the initial assessment by the fire brigade leader and expected need for offsite support to extinguish the fire. As reported in the 0420 EDT update on March 22, 2024, the fire was reported extinguished at 0009 CDT on March 22, 2024, by the Waterford Fire Brigade without the need of offsite support. (NOTE: The Initial Notification Form sent from the Control Room at 2341 CDT on March 21, 2024, requested by and provided to the Headquarters Operation Center via e-mail at 0302 CDT on March 22, 2024, stated that the emergency classification had been made on initiating condition HU4.4 rather than HU4.1) In accordance with NRC Approved guidance in FAQ 21-02 (ML21117A104), Waterford 3 is retracting the initial event notification made at 0117 EDT on March 22, 2024. The remaining events that were reported in EN 57042 as a 4-hour non-emergency notification in accordance with 10 CFR 50.72(b)(2)(iv)(B) as an actuation of the reactor protection system (RPS) when the reactor is critical and as an 8-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as valid actuation of the EFW (emergency feedwater) system, ECCS (emergency core cooling system), containment isolation and emergency diesel generators are still applicable and require no additional update at this time. The licensee also provided a site map. Notified R4DO (Kellar)

ENS 5704322 March 2024 01:56:00Callaway10 CFR 50.72(b)(3)(iv)(A), System ActuationAuxiliary Feedwater

The following information was provided by the licensee via email: At 2056 on 3/21/24, Callaway Plant was in Mode 1 at approximately 100 percent power when an automatic start of the turbine driven auxiliary feedwater pump occurred. The event occurred while restoring inverter NN12 from maintenance. NN12 is the normal in-service inverter for the group 2 120-VAC instrument bus (NN02). The actuation occurred while swapping from the swing inverter (NN18) to the normal in-service inverter (NN12). All safety systems responded as expected. At 2334, the turbine driven auxiliary feedwater pump was secured. The plant is being maintained in a stable condition, in mode 1. The NRC Resident Inspector was notified The licensee is investigating the cause of the automatic start.

  • * * RETRACTION ON 4/25/2024 AT 1432 EDT FROM GREG CIZIN TO ERNEST WEST * * *

Event Notification (EN) 57043, made on 03/21/2024 pursuant to 10 CFR 50.72(b)(3)(iv)(A), is being retracted based upon further investigation into the cause of the turbine driven auxiliary feedwater pump (TDAFP) actuation. The TDAFP received an invalid manual initiation signal caused by a voltage transient that was generated on the NK02 125-VDC bus upon closure of downstream breaker NK0211 (while restoring inverter NN12 from maintenance). This actuation signal was due to degradation of a 48-VDC power supply (PS1) within engineered safety features actuation system (ESFAS) logic cabinet SA036C. This degradation likely prevented the power supply from sufficiently filtering the transient that occurred on the 125-VDC bus associated with the NN12 inverter. Notified R4DO (Warnick)

ENS 5703317 March 2024 20:15:00Comanche Peak10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Feedwater
Auxiliary Feedwater
Main Condenser
The following information was provided by the licensee via phone and email: On March 17, 2024, at 1515 CDT, the Comanche Peak Unit 2 reactor was manually tripped due to an anticipated automatic trip due to lo-lo steam generator (SG) water levels. Prior to the trip, main feedwater pump '2B' tripped and an auto runback to 700 MW (60 percent power) was in progress. Both motor driven auxiliary feedwater pumps and the turbine driven auxiliary feedwater pump started due to lo-lo level in all SGs. Unit 2 is being maintained in hot standby (Mode 3) in accordance with integrated plant operating procedures IPO-007B. The emergency response guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the '2B' main feed pump trip was due to loss of primary and redundant power to the servo control valve. The loss of power to the servo control valve is under investigation.
ENS 5703216 March 2024 19:49:00Waterford10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Feedwater
Reactor Protection System
Main Steam Isolation Valve
Control Rod
Main Steam
The following information was provided by the licensee via phone and email: At 1449 CDT, Waterford 3 Steam Electric Station was operating at 100 percent power when a manual reactor trip was initiated due to main feed isolation valve (FW-184B) and main steam isolation valve (MS-124B) going closed unexpectedly. Emergency feedwater (EFW) was automatically actuated. Preliminary evaluation indicates that all plant systems functioned normally after the reactor trip. The unit is currently stable in Mode 3. All control rods fully inserted as expected. This event is being reported as a 4-hour non-emergency notification in accordance with 10 CFR 50.72(b)(2)(iv)(B) as an actuation of the reactor protection system (RPS) when the reactor is critical and as an 8-hour nonemergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as valid actuation of the EFW system. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Decay heat is being removed through the turbine bypass valves and the atmospheric dump valve on loop '2'. There is no primary to secondary system leakage. The cause of the isolations is still being investigated.
ENS 5702613 March 2024 01:11:00Catawba10 CFR 50.72(b)(3)(iv)(A), System Actuation

The following information was provided by the licensee via phone and email: On March 12, 2024, at 2111 EDT, a valid containment ventilation isolation train 'A' and 'B' signal was received due to a spurious loss of power to 1EMF-38 (containment particulate radiation monitor) and 1EMF-39 (containment gas radiation monitor). The power to 1EMF-38 and 1EMF-39 was restored. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: There were no plant evolutions ongoing at the time of the event and the cause of the loss of power is under investigation. There was no impact to Unit 2.

  • * * RETRACTION ON 3/13/2024 AT 1436 EDT FROM JASON MOORE TO SAM COLVARD * * *

After further review of the event, it was determined the actuation of the associated containment ventilation isolation train 'A' and 'B' was not valid. This is due to the loss of power being associated with the control room modules for 1EMF-38 and 1EMF-39, and not a result of an actual sensed parameter or plant condition. Therefore, this event notification is being retracted. The NRC Resident Inspector has been notified. Notified R2DO (Miller)

ENS 5702412 March 2024 13:16:00Comanche Peak10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Feedwater
Auxiliary Feedwater
Main Condenser
The following information was provided by the licensee via phone and email: On March 12, 2024, at 0816 CDT, Comanche Peak Unit 2 reactor automatically tripped on lo-lo level in the 2-03 steam generator (SG). Prior to the trip, main feedwater pump (MFP) 2A speed reduced and a manual runback to 700 MW (60 percent) was in progress. Both motor driven auxiliary feedwater pumps and the turbine driven auxiliary feedwater pump started due to lo-lo level in all SGs. Concurrent with the loss of speed on MFP 2A, a servo filter swap was in progress on MFP 2A. Unit 2 is being maintained in hot standby (Mode 3) in accordance with integrated plant operating procedure IPO-007A. The emergency response guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the loss of the MFP is under investigation. Unit 1 was unaffected.
ENS 5702111 March 2024 17:37:00Hatch10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Reactor Protection System
Emergency Diesel Generator
Reactor Core Isolation Cooling
Emergency Core Cooling System
Main Condenser
The following information was provided by the licensee via phone and email: On March 11, 2024, at 1337 EDT, with Unit 1 in Mode 1 at 35 percent power performing power ascension activities, the reactor was manually tripped due to the 'A' reactor feed pump (RFP) tripping on low suction pressure. Due to the power level at the time, the 'B' RFP had not been placed in service. Closure of containment isolation valves (CIVs) in multiple systems and actuation of high-pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) occurred as a result of reaching the actuation setpoint on reactor water level as designed. The trip was not complex, with all safety systems responding normally post-trip. Operations responded and stabilized the plant. The 'B' RFP was placed in service and is controlling reactor water level. Decay heat is being removed by discharging steam to the main condenser using turbine bypass valves. Unit 2 is not affected. Due to the emergency core cooling system (ECCS) discharging into the reactor, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). Also, the Reactor Protection System actuation while critical is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, it is reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of CIVs, RCIC and HPCI. There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the 'A' RFP is under investigation. The reactor electric plant remains in a normal lineup with both emergency diesel generators available. There were no temperature or pressure technical specification limits approached.
ENS 570065 March 2024 06:32:00Watts Bar10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Feedwater
Reactor Protection System
Auxiliary Feedwater
Control Rod
The following information was provided by the licensee via email: At 0132 EST, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main feedwater isolation signal which resulted in steam generator lo-level reactor trip. The reactor trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed using the auxiliary feedwater and steam dump systems. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the auxiliary feedwater system (an engineered safety feature) is being reported as an eight hour report under 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All control rods are fully inserted. The cause of the main feedwater isolation is being investigated.
ENS 570044 March 2024 00:42:00Nine Mile Point10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Shutdown Cooling
Decay Heat Removal
Control Rod
The following information was provided by the licensee via email: On 3/3/24 at 1942 EST, while performing a plant shutdown in preparation for a refuel outage, Nine Mile Point Unit 2 experienced a reactor scram due to a main turbine trip on low condenser vacuum. The plant was at approximately 55 percent power at the time of the reactor scram. Additionally, following the scram a low RPV (reactor pressure vessel) level scram and containment isolation signal on level 3 was received, as expected. The containment isolation signal impacted RHR (residual heat removal) shutdown cooling, RHR letdown to radwaste, and RHR sampling. All impacted valves were closed at the time the isolation occurred. All control rods were fully inserted. Plant response was as expected. Post scram, the main turbine bypass valves are being used to control decay heat, and normal post scram level control is via the feed / condensate system. This is being report under 10 CFR 50.72(b)(2)(iv)(B), 'RPS Actuation', and 10 CFR 50.72(b)(3)(iv)(A), 'Specified System Actuation'. Unit 1 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the low condenser vacuum was a momentary loss of sealing steam. The condenser remained viable for decay heat removal. All safety equipment is available. The grid is stable with the plant in its normal shutdown electrical configuration.
ENS 570033 March 2024 17:42:00Prairie Island10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Feedwater
Auxiliary Feedwater
The following information was provided by the licensee via email: At 1142 CST on 3/3/2024, with Unit 2 in Mode 1 at 29 percent power, the reactor automatically tripped due to a turbine trip caused by a loss of suction to the 22 main feedwater pump. All systems responded normally post trip. Decay heat is being removed via the auxiliary feedwater water system. Secondary steam control mechanism is the steam generator PORVs (power operated relief valves). Unit 1 remains at 100 percent power and is unaffected. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The resident NRC inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The trip occurred while the licensee was returning to power operations after a refueling outage. During the trip, all rods inserted into the core. The plant is in a normal shutdown electrical lineup with offsite power available. The plant will be maintained at normal operating temperature and pressure. There is no known primary to secondary leakage. The cause of the loss of 22 main feedwater pump suction is under investigation.
ENS 5699728 February 2024 18:50:00Calvert Cliffs10 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel GeneratorThe following information was provided by the licensee via phone and email: At 1350 EST on 2/28/2024, with Calvert Cliffs Unit 1 in Mode 5 at 0 percent power and Unit 2 in Mode 1 at 65 percent power, an actuation of the '1A' and '2A' emergency diesel generators' auto-start occurred due to an undervoltage condition on the number 11 and number 21 4kV buses which are fed from the number 11 13kV bus. The '1A' and '2A' emergency diesel generators automatically started as designed when the 4kV buses' undervoltage signals were received. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the '1A' and '2A' emergency diesel generators. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The undervoltage condition was caused by the feeder breaker to the number 11 13 kV bus opening during electrical maintenance.
ENS 5699528 February 2024 14:39:00Monticello10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Protection System
Main Condenser
The following information was provided by the licensee via fax and email: At approximately 0839 (CST) with Unit 1 in Mode 1 at 100 percent power, the reactor automatically scrammed due to the depressurization of the SCRAM air header caused by an invalid signal that (occurred) during system testing. The SCRAM was uncomplicated with all systems responding as expected. The cause and details of the event are under investigation. Containment isolation valves actuated and closed on a valid Group 2 signal. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B), and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for the Group 2 isolation signal. Operations responded using the emergency operating procedure and stabilized the plant in Mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. State as well as Wright and Sherburne Counties will be notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The Anticipated Transient Without Scram (ATWS) circuit was being tested when an invalid signal was sent to depressurize the SCRAM air header.
ENS 5699124 February 2024 20:46:00Calvert Cliffs10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Reactor Protection System
Auxiliary Feedwater
Main Condenser
The following information was provided by the licensee via email: At 1546 EST, with unit 2 at 100 percent power, the reactor was manually tripped due to the '22' steam generator feed pump tripping. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Operations responded using emergency operation procedure EOP-0, Post Trip Immediate Actions and EOP-1, Uncomplicated Reactor Trip and stabilized the plant in mode 3. Decay heat is removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 is not affected. ESFAS (engineered safety features actuation systems) actuation (auxiliary feedwater manual actuation) is reportable under 10 CFR 50.72(b)(3)(iv)(A) 8-hour report. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5699024 February 2024 08:19:00Browns Ferry10 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel GeneratorThe following information was provided by the licensee via phone and email: At 0219 CST on February 24, 2024, Browns Ferry Unit 3 was shut down in a refueling outage, while closing 4 kV shutdown board breaker 3EB-9, the 4 kV shutdown board normal feeder breaker tripped open resulting in a valid 4 kV bus under-voltage condition. Due to the under-voltage condition, the 3B emergency diesel generator (EDG) auto started and tied to the board. The cause of the breaker tripping open is unknown and an investigation is in progress. All systems responded as expected for the loss of voltage. This event requires an 8-hour report per 10 CFR 50.72(b)(3)(iv)(A). There was no impact to the health and safety of the public or plant personnel. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: No other safety related equipment was affected. The 3B EDG continues to supply the shutdown board pending further investigation.
ENS 5697819 February 2024 07:36:00Summer10 CFR 50.72(b)(3)(iv)(A), System ActuationFeedwater
Emergency Diesel Generator

The following information was provided by the licensee via phone and email: On February 19, 2024, at 0236 EST, with VC Summer Unit 1 in Mode 1 at 100 percent power, an actuation of the `B emergency diesel generator (EDG) occurred. The reason for the `B EDG auto-start was the trip of 1 `DB normal incoming breaker. The `B EDG automatically started as designed when the undervoltage signal was received. The `B emergency feedwater pump started due to the undervoltage signal and ran for approximately 1 minute and was secured by operations per procedure. Other plant equipment and systems also responded as expected. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the `B EDG and a valid actuation of the `B emergency feedwater pump. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The `A Emergency Diesel Generator was tagged out for maintenance earlier in the shift, but maintenance has not started. The plan is to restore the `A emergency diesel generator to an operable status and investigate the cause of the 1 `DB normal incoming breaker trip. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: This event resulted in the plant entering a 12 hour limiting condition for operation (LCO) in accordance with technical specification (TS) 3.8.1.1.C. due to having one operable EDG and a loss of offsite power.

      • RETRACTION ON 06/06/2024 AT 1356 EDT FROM JUSTIN BOUKNIGHT TO NATALIE STARFISH ***

VC Summer is retracting event notification (EN) 56978 regarding the unexpected actuations of the B emergency diesel generator and B emergency feedwater pump on 02/19/2024. Both were previously reported as valid actuations under 10 CFR 50.72(b)(3)(iv)(A). Subsequent evaluation has determined that the actuations were the result of an invalid signal caused by equipment failure on the 1 DB bus undervoltage control circuit. The event, its cause, and corrective actions were reported in VC Summer licensee event report 2024-001-00 (ML24108A143) on 04/17/2024, pursuant to the requirements of 10 CFR 50.73(a)(2)(iv)(A). There was no impact on the health and safety of the public or plant personnel as a result of the actuations. The NRC Senior Resident Inspector has been notified. Notified R2DO (Franke)

ENS 5697719 February 2024 04:25:00Brunswick10 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel Generator
Primary Containment Isolation System
Residual Heat Removal
The following information was provided by the licensee via phone and email: At approximately 2325 EST on February 18, 2024, with Unit 1 in Mode 5 at 0 percent power and Unit 2 in Mode 1 at 100 percent power, emergency diesel generator 2 automatically started due to the unexpected loss of AC power to emergency bus E2 during a planned transfer of E2 DC control power from normal to alternate for the 1B-1 battery. In addition, the unexpected loss of AC power to E2 resulted in Unit 1 primary containment isolation system (PCIS) partial Group 2 (i.e., drywell equipment and floor drain, residual heat removal (RHR), discharge to radioactive waste, and RHR process sample), Group 6 (i.e., containment atmosphere control/dilution, containment atmosphere monitoring, and post accident sampling systems), and partial Group 10 (i.e., air isolation to the drywell) isolations. Emergency diesel generator 2 automatically started and re-energized the E2 bus as designed when the loss of E2 signal was received. The PCIS actuations were as expected for the outage plant line up on Unit 1 at the time. The cause of the loss of electrical power to emergency bus E2 is under investigation at this time. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of emergency diesel generator 2 and PCIS. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: This event will be entered into the plant's corrective action program.
ENS 5697116 February 2024 11:34:00Farley10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Reactor Protection System
Auxiliary Feedwater
The following information was provided by the licensee via email: At 0048 CST on February 16, 2024, with Unit 2 in mode 1 at 100 percent power, the reactor was manually tripped due to a loss of 2A 125V DC distribution panel. The trip was complex due to the loss of components associated with A-train DC power. Operations responded and stabilized the plant. Decay heat is being removed by the atmospheric relief valves. Unit 1 is not affected. An automatic actuation of the auxiliary feedwater system (AFW) occurred due to low-low steam generator levels. The AFW auto-start is an expected response with low-low steam generator levels from the reactor trip. AFW is still currently controlling steam generator levels. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the AFW System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5697016 February 2024 03:24:00Watts Bar10 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel Generator

The following information was provided by the licensee via email: At 2224 EST on February 15, 2024, with both units 1 and 2 in mode 1 at 100 percent power, an actuation of the emergency diesel generator (EDG) system on 1A-A, 1B-B, and 2B-B EDGs occurred while removing clearances. The 2A-A EDG did not start because it was still under a clearance. The reason for the emergency diesel generator system auto-start was clearance removal sequencing errors. The emergency diesel generator system automatically started as designed when the common emergency start signal was received. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the emergency diesel generator system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 2/21/2024 AT 1549 EST FROM TYSON JONES TO KAREN COTTON * * *

The following information was provided by the licensee via email: In accordance with NUREG-1022, Section 2.8 and Section 4.2.3, Watts Barr is retracting the previous report EN 56970 pursuant to 10 CFR 50.72(b)(3)(iv)(A). The start signal for the 1A-A, 1B-B, and 2B-B emergency diesel generators (EDG)s was from activation of the common emergency start of the 2A-A EDG. The actuation was not from a loss of offsite power (LOOP) to any shutdown board or from any parameters that would initiate a safety injection (SI) signal, for which the EDG is designed to provide a design basis safety function. Also, the starts were not from intentional manual actuation. Starting the EDGs did not make them inoperable and each EDG was able to perform its design safety function. The common emergency start relay for each diesel is not safety related. It is an anticipatory and redundant circuit to start other EDGs in the event of a LOOP or SI related to the specific EDG. With the 2A-A EDG out of service, the associated common emergency circuit would not be required to perform any function. The starts were not initiated in response to actual plant conditions or parameters satisfying the requirements for initiation of the system. Since the starts were not initiated via an automatic signal from a LOOP, SI, or traditional operator action, the signal is not a valid actuation in accordance with 10 CFR 50.72(b)(3)(iv)(A). Therefore, EN 56970 is being retracted. The NRC Resident Inspector has been notified of this retraction. Notified R2DO (Miller)

ENS 5696815 February 2024 08:47:00Callaway10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Feedwater
Auxiliary Feedwater
Control Rod
The following information was provided by the licensee via email: At 0247 CST on 2/15/2024, Callaway Plant was in mode 1 at approximately 100 percent power when a turbine trip and reactor trip occurred. All safety systems responded as expected with the exception of an indication issue on the feedwater isolation valves, which were confirmed closed. A valid feedwater isolation signal and auxiliary feedwater actuation signal were also received as a result of the reactor trip. The plant is being maintained stable in mode 3. All control rods fully inserted from the reactor trip signal and decay heat is being removed via the auxiliary feedwater system and steam dumps. The NRC Resident Inspector was notified.
ENS 5693629 January 2024 17:02:00Peach Bottom10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
High Pressure Coolant Injection
Primary Containment Isolation System
Reactor Core Isolation Cooling
Residual Heat Removal
Main Condenser
Control Rod

The following information was provided by the licensee via email: At approximately 1202 EST on 01/29/24, unit 2 experienced a reactor scram caused by a main turbine trip. Investigation is still ongoing. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All control rods were fully inserted. The licensee indicated that the turbine trip may have been caused by a power load imbalance, however the cause of the incident is under investigation. The scram was not complex. Decay heat is currently being removed thru bypass valves dumping to the main condenser. Initially unit 2 lost the use of the bypass valves due to lack of condenser vacuum. Unit 2 used the high pressure coolant injection (HPCI) system in the condenser storage tank (CST) to CST mode to remove decay heat. Residual heat removal was used to keep the torus cool. Condenser vacuum was regained and unit 2 is back to removing decay heat with the turbine bypass valves. There was no impact to unit 3. The licensee confirmed there was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * *UPDATE ON 01/29/24 AT 1935 EST FROM PAUL BOKUS TO NATALIE STARFISH* * *

The following information was provided by the licensee via email: Licensee adds 8-hour non-emergency 10 CFR 50.72(b)(3)(iv)(A) specified system actuation report to original 4-hour non-emergency 10 CFR 50.72(b)(2)(iv)(B) RPS Actuation report. At approximately 1202 EST on 01/29/24, unit 2 experienced a reactor scram by a main turbine trip. All control rods inserted. Reactor core isolation cooling system (RCIC) was manually initiated for level control. HPCI was manually initiated for pressure control. Primary containment isolation system (PCIS) Group II and III isolations occurred (specified system actuation). Investigation is ongoing. The NRC Resident Inspector has been notified.

ENS 5693528 January 2024 02:41:00Watts Bar10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Protection System
Auxiliary Feedwater
Control Rod
The following information was provided by the licensee via email: At 2141 EDT, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main turbine trip. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed using the auxiliary feedwater and steam dump systems. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the auxiliary feedwater system (an engineered safety feature) is being reported as an eight hour report under 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All control rods are fully inserted. The cause of the turbine trip is being investigated. The licensee notified the NRC Resident Inspector.
ENS 5689416 December 2023 09:50:00Grand Gulf10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Feedwater
Reactor Protection System
Control Rod
The following information was provided by the licensee via email: On December 16, 2023, at 0350 CST, Grand Gulf Nuclear Station was operating in mode 1 at 81 percent power when an automatic scram occurred due to a turbine trip signal. Before the scram the unit was performing a rod sequence exchange, and no critical work was underway. The cause of the turbine trip signal is not known at this time and is being investigated. All control rods fully inserted, there were no complications, and all plant systems responded as designed. Reactor water level is being maintained by main feedwater and condensate. Reactor pressure is being maintained with main turbine bypass valves. No radiological releases have occurred due to this event. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A), as any event or condition that results in actuation of the reactor protection system when the reactor is critical and specified system actuation due to expected reactor water level 3 isolation signals on a reactor scram. The NRC Senior Resident Inspector has been notified of this event. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Group 2 and Group 3 isolations occurred on the Level 3 isolation signal.
ENS 5688713 December 2023 07:02:00River Bend10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Feedwater
Reactor Protection System
Reactor Core Isolation Cooling
The following information was provided by the licensee via phone and email: At 0102 CST, while operating at 100 percent (reactor) power, River Bend Station experienced an automatic reactor scram caused by a turbine trip signal. The cause of the turbine trip signal is not known at this time and is being investigated. At 0108, reactor core isolation cooling (RCIC) was initiated due to a loss of reactor feed pumps following feedwater heater string isolation. At 0114, reactor water level control was transferred back to feedwater and RCIC was secured. Reactor water level is being maintained by feedwater pumps and reactor pressure is being maintained by turbine bypass valves. The scram was uncomplicated and all other plant systems responded as designed. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical and 10 CFR 50.72(b)(3)(iv)(A) specified system actuation as result of expected post scram (reactor water) level 3 isolations and manual initiation of RCIC. No radiological releases have occurred due to this event from the unit. The NRC Senior Resident Inspector has been notified of this event. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the turbine trip, while still under investigation, was likely due to an electrical transient involving the main generator. Walkdowns in the switchyard post-scram identified damage to one of the output breaker disconnects.
ENS 568772 December 2023 12:10:00South Texas10 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel GeneratorThe following information was provided by the licensee via email: At 0610 CST on 12/2/2023, with Unit 2 in Mode 1 at 100 percent power, the South Texas Project switchyard south electrical bus was de-energized. Emergency diesel generator (EDG) '22' automatically started in response to the loss of offsite power on the train 'B' engineered safety feature (ESF) electrical bus. This event is reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in the valid actuation of an emergency AC electrical power system (50.72(b)(3)(iv)(B)(8)). All required loads were successfully started. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The initial loss of the south electrical bus, partial loss of off-site power, put the plant in a 24 hour limiting condition for operation (LCO) in accordance with (IAW) technical specification (TS) 3.8.1.1.E. Power was restored to the train 'B' ESF bus via an alternate offsite power source and the EDG was returned to its automatic standby condition. Currently, the plant is in a 72 hour LCO IAW TS 3.8.1.1.A.
ENS 5686318 November 2023 05:55:00River Bend10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Feedwater
Reactor Protection System
Emergency Diesel Generator
Control Rod
The following information was provided by the licensee via phone and email: On November 17, 2023, at 2215 CST, River Bend Station (RBS) was operating at 30 percent reactor power performing plant startup activities when an isolation of low-pressure feedwater string `A' occurred. The team entered applicable alternate operating procedures and inserted control rods to exit the restricted region of the power to flow map. Feedwater temperature continued to lower until it challenged the prohibited region of the AOP-0007 graph requiring a reactor scram. The team inserted a manual reactor scram at 2355 from 24 percent reactor power. All control rods fully inserted and there were no complications. All systems responded as designed. Currently RBS Unit 1 is stable with reactor level being maintained 10 to 51 inches with feed and condensate, and pressure being maintained 500 to 1090 psig using steam drains. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the Reactor Protection System (RPS) when the reactor is critical and 10 CFR 50.72(b)(3)(iv)(A) Specified System Actuation as result of Group 3 isolations. The NRC Senior Resident inspector has been notified. No radiological releases have occurred due to this event from the unit. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The electric plant is in a normal lineup for current plant conditions with all emergency diesel generators available. The cause of the initial isolation of low-pressure feedwater string "A" is still under investigation.
ENS 5685616 November 2023 07:27:00Calvert Cliffs10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Feedwater
Reactor Protection System
Auxiliary Feedwater
Main Condenser

The following information was provided by the licensee via email: At 0227 EST on 11/16/23, Calvert Cliffs Unit 2 experienced an automatic trip from the reactor protection system (RPS) based on reactor trip bus undervoltage (UV). At that time, a loss of U-4000-22 (13 kV to 4 kV transformer) caused a loss of 22, 23, and 24 4 kV busses. This resulted in a loss of both motor generator (MG) sets causing the reactor trip bus UV. The loss of 22 and 23 4 kV non-safety related busses resulted in a loss of main feedwater. Auxiliary feedwater (AFW) was manually initiated and is feeding both steam generators. The 2B diesel generator (DG) started and restored the 24 4 kV safety related bus. Heat removal is via the normal turbine bypass valves to the main condenser. RPS actuation is reportable under 10 CFR 50.72(b)(2)(iv)(B) - 4 hour report ESFAS (engineering safety features actuation system) actuation (2B DG start on UV) is reportable under 10 CFR 50.72(b)(3)(iv)(A) - 8 hour report AFW operation is reportable under 10 CFR 50.73(a)(2)(iv)(A) - 60 day report The NRC Senior Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All rods fully inserted. There was no impact on Unit 1 operations. Unit 2 is stable in mode 3.

  • * * UPDATE ON AT 0940 EST FROM KERRY HUMMER TO ADAM KOZIOL * * *

ESFAS actuation (AFW manual initiation) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8 hour report Notified R1DO (Defrancisco).

ENS 5685214 November 2023 16:41:00Farley10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Steam Generator
Feedwater
Reactor Protection System
Auxiliary Feedwater
The following information was provided by the licensee via phone and email: At 1041 CST on 11/14/23 with Farley Unit 2 in Mode 1 at 10 percent power, the reactor was manually tripped due to rising steam generator levels. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Auxiliary feedwater (AFW) was manually initiated in accordance with plant procedures and is feeding the steam generators. Heat removal is being provided via the atmospheric relief valves. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). This event is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the auxiliary feedwater system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All rods fully inserted. The licensee attempted to take manual control of the feedwater control valves to lower steam generator level but, due to reaching a steam generator level that requires a manual trip, the licensee manually tripped the reactor.
ENS 5684610 November 2023 08:14:00Susquehanna10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Feedwater
Reactor Protection System
Main Condenser
The following information was provided by the licensee via email: At 0118 EST, with Unit 1 in Mode 1 at 100 percent power, the reactor was manually scrammed due to degrading main condenser vacuum. The scram was not complex, with all systems responding normally post-scram. The main turbine bypass valves opened automatically to maintain reactor pressure. Operations responded and stabilized the plant. Reactor water level is being maintained via feedwater pumps. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 2 is not impacted. Due to Reactor Protection System actuation while critical, this event is being reported as a four-hour and eight-hour non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). Unit 1 reactor is currently stable in mode 3. An investigation is in progress into the cause of the degrading condenser vacuum. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.