ENS 57107
ENS Event | |
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08:38 May 5, 2024 | |
Title | Automatic Reactor Trip Due to Lowering Steam Generator Water Level |
Event Description | The following information was provided by the licensee via email and phone:
At 0338 CDT, with the unit 1 in mode 1 at 6 percent power, the reactor automatically tripped due to lowering steam generator water level. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for an actuation of the auxiliary feedwater system. Operations responded using procedure 1BwEP-0 and stabilized the plant in mode 3. Decay heat is removed by steam dumps via the main condenser. 1A and 1B auxiliary feedwater pumps were actuated manually prior to the reactor trip in an attempt to restore steam generator water level. Unit 2 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
The following information was provided by the licensee via email and phone: At 0338 CDT, with the unit 1 in mode 2 at 3 percent power, the reactor automatically tripped due to lowering steam generator water level. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and 10CFR50.72(b)(3)(iv)(A) for an actuation of the auxiliary feedwater system, eight-hour notification. Operations responded using procedure 1BwEP-0 and stabilized the plant in mode 3. Decay heat is being removed by steam dumps via the main condenser. 1A and 1B auxiliary feedwater pumps were actuated manually prior to reactor trip in an attempt to restore steam generator water level. Unit 2 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Notified R3DO (Hartman) |
Where | |
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Braidwood Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000456/LER-2024-001 Trip on Low Steam Generator Level Ddue to Failure to Verify Isolation Valves Were Open |
Time - Person (Reporting Time:+-0.45 h-0.0188 days <br />-0.00268 weeks <br />-6.1641e-4 months <br />) | |
Opened: | Azeam Anjum 08:11 May 5, 2024 |
NRC Officer: | Tenisha Meadows |
Last Updated: | Jul 5, 2024 |
57107 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (6 %) |
After | Hot Standby (0 %) |
Braidwood with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 571072024-05-05T08:38:0005 May 2024 08:38:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Lowering Steam Generator Water Level ENS 553202021-06-21T05:51:00021 June 2021 05:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip on Generator Lockout Relay Trip ENS 542892019-09-23T16:06:00023 September 2019 16:06:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Lowering Steam Generator Levels ENS 534432018-06-04T14:20:0004 June 2018 14:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip on Lowering Steam Generator Water Level ENS 533712018-04-30T16:24:00030 April 2018 16:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following Turbine Trip ENS 533582018-04-22T21:46:00022 April 2018 21:46:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Undervoltage Actuation of the Engineered Safety Feature Bus ENS 533472018-04-19T16:52:00019 April 2018 16:52:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Undervoltage Actuation of the Engineered Safety Feature Bus ENS 514502015-10-05T06:05:0005 October 2015 06:05:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuations ENS 462622010-09-20T22:04:00020 September 2010 22:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 461782010-08-16T07:06:00016 August 2010 07:06:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trips at Both Units ENS 452382009-07-31T02:08:00031 July 2009 02:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to a Loss of Offsite Power for Greater than 15 Minutes ENS 450172009-04-24T16:41:00024 April 2009 16:41:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip During Instrument Calibration ENS 447432008-12-27T20:18:00027 December 2008 20:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip as a Result of a Generator Trip ENS 435902007-08-23T20:30:00023 August 2007 20:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness Manual Reactor Trip Because of Lowering Condenser Vacuum ENS 434492007-06-27T14:21:00027 June 2007 14:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Off-Site Power Fluctuation ENS 415352005-03-28T18:46:00028 March 2005 18:46:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Generator Protection Circuitry ENS 412802004-12-22T19:07:00022 December 2004 19:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rps Actuation Due to Steam Generator Low Level Signal ENS 403702003-12-03T09:36:0003 December 2003 09:36:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Plant Had an Auto Reactor Trip from 100% Power Due to Steam Generator Low Level ENS 402982003-11-05T03:32:0005 November 2003 03:32:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Braidwood 2 Afw Support System Actuation During Outage 2024-05-05T08:38:00 | |