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ML20046C3665 August 1993Special Rept:On 930629,seven Blockout Type Penetration Fire Barriers & on 930713,six Sleeve Type Penetration Fire Barriers Determined to Be Nonfunctional.Repairs Completed & Fire Barriers Restored to Functional StatusFire Barrier
Fire Watch
ML20044H3651 June 1993Special Rept:On 930427,EDG Failed to Auto Start During Performance of Main Dam Auxiliary Power Diesel Periodic Test.Corroded Wires & Lugs Appeared to Be Loose.Control Wire Connections Cleaned & Aged Wires Replaced
ML20024H64731 May 1991Special Rept:On 910227,svc Water MOVs Associated W/ Recirculation Spray Heat Exchangers Exceeded Torgue Limits & Stopped in Mid Position While Being Opened During Test.Event Reported on Voluntary Basis to Provide Info to NRC
ML20005E16022 December 1989Special Rept:On 891218,heat Trace Sys for Kaman Vent Stack a Radiation Monitor RI-VG-179 Declared Inoperable.Sys Removed from Svc & Tech Spec 3.3.3.1 Action Statememt Entered.Sys Will Be Repaired & Returned to Svc by 900130
ML19332G04711 December 1989Special Rept:On 891202,Kaman Process Vent Radiation Monitor Exceeded Action Statement of Tech Spec 3.3.3.1 Since Monitor Not Returned to Operable Status within 7 Days.On 891125, Monitor Alarmed in Control Room Every 15 to 30 Minutes
ML20023D21810 May 1983Ro:On 830509,w/unit at 100% Power,Severe Hydrogen Leak Discovered on Hydrogen inner-cooled Turbine Generator.Unit Rampdown Ordered & Hydrogen Vented to Atmosphere.Emergency Terminated When Pressure Reached Less than 10 Psig
ML20009F97526 March 1981Ro:On 810325,station Personnel Discharged 22,000 Gallons of Condensate Water Over 14-h Period.Samples Taken at Beginning & End of Discharge.Results Listed
ML19329F88111 July 1980RO 80-55/O1T-0:during Review of FSAR Safety Analyses for Boron Dilution Accident Potential,Nonconservatism in Cold Shutdown Analysis Determined.Cause Unknown.Accident Analysis Review Initiated
ML19329F97027 June 1980RO-80-029/01T-0:on 800627,pressurizer Power Operated Relief Valve PCV-2456 Inadvertently Opened in Mode 3 Following Valve Maint Activities.Corrective Action Will Be Taken Pending Completion of Investigation
ML18139A2996 June 1980Ro:Several Lines in Low Head & High Safety Injection Sys Were Not Analyzed for Effects of Fluid Temp Below 70 F. Review of New Nozzle Loads Showed Load on Pump Exceeded Vendor Allowable Load.Multiphase Program Proposed
ML19312E5905 June 1980RO 80-10/01T-0:on 800605,during Review of ECCS Piping, Loading on Low Head Safety Injection Pump Nozzles Was Discovered to Exceed Design Stress Allowable.Caused by Deficiency in Piping Sys Stress Analysis
ML19290C6834 February 1980RO 80-02/01T-0:during Review Required by IE Bulletin 79-14, Stress Discovered Over Design Allowable on Pipe Hangers & Snubbers.Caused by Incorrect Valve Weights Used in Design Calculations.Hangers & Snubbers Will Be Modified
ML19270K26425 January 1980RO-80-19:on 800124,during Equipment Qualification Review for IE Bulletin 79-01,qualification Discrepancy Discovered in Svc Water Radiation Pumps for Recirculation Spray Heat Exchangers.Cause Unknown
ML19290C68421 January 1980RO-80-01/01T-0:on 800121,excess Letdown Lines Had Several Pipe Stress Points Above Normal or Upset Allowables.Caused by Incorrect Use of Valve Weight for HCV-1201 Pipe Stress Calculations.Snubber Will Be Added to Line
ML19270H79414 December 1979Followup Suppl to Ler/Ro 79-15.Higher Pipe Stress Code Allowable Should Have Been Used by Teledyne.Pipe Stress on Kubes 1.5 inches-RC-105-1502-01 Not Over Code Allowable
ML19257A34512 December 1979RO 79-158/01T-0:during Review Required by IE Circular 78-08, S&W Discovered Pressure Differential Switches PDS-HV1228A & B Not Seismically Qualified.Cause Unknown.Problem Being Reviewed
ML19257A34312 December 1979RO 79-157/01T-0:during Review of Seismic Analyses Per IE Bulletin 79-14,nonconformance in Pipe Support Design Was Discovered by S&W.Caused by Incorrect Valve Weights Used in Support Calculations
ML19268C17127 November 1979Supplements RO 79-141/01T-0:while Reviewing Operation of Secondary Ventilation Sys,Sys Discovered to Operate in Manner Not in Keeping W/Accident Analyses.Cause Unknown. Matter Under Review
ML19268C17019 November 1979Supplements RO 79-141/1T-0:on 791114,determined,upon Review of Fsar,That Previously Reported Deficiency Re Nonautomatic Restart of Casing Cooling Pumps on Restoration of Onsite Emergency Power Is Not Deficiency
ML19268C17419 November 1979Followup to RO 79-152/01T-0:on 791118,Westinghouse Notified Util of Potential Reduction in Conservatism Re Error Allowances Assumed in Analysis for Power Range Neutron Flux High Negative Rate.Setpoints Will Be Changed
ML19268C17216 November 1979Supplements RO 79-141/01T-0:while Reviewing Operation, Recirculation Cooling Fans & Control Rod Drive Fans Found to Operate in Manner Not in Keeping W/Accident Analyses. Cause Unknown.Problem Being Reviewed by Engineering Svcs
ML19268C17314 November 1979Supplements RO 79-141/01T-0:while Reviewing Operation of Svc Water Sys,Casting Cooling Subsys & Recirculation Spray Sys, Sys Found to Operate Not in Keeping W/Accident Analyses. Cause Unknown.Discrepancies Under Review
ML19308B11314 November 1979Submits 24-h Reportable Event Written Followup Re Undetecable Failure of P-4 Contacts in Engineered Safety Features Actuation Sys.Caused by Westinghouse Design Error. Procedures for Testing P-4 Contacts Being Evaluated
ML19268C1696 November 1979RO-79-151/01T-0:during Review of Valve Weights in Conjunction W/Ie Bulletin 79-14,discovered That Incorrect Seismic Response Spectrum Was Used in Pipe Stress Analysis. Cause Not Known.Investigation in Progress
ML19254F27018 October 1979RO 79-142/01T-0:on 791018,during Pressurization of Steam Generator C,Channel IV Pressure Indications for Generators a & C Observed to Be Swapped.Caused by Piping Being Connected to Wrong Transmitters.Piping Will Be Changed
ML19249E11414 September 1979Ro:On 790914,ambient Temp Ranges Could Have Existed in Excess of Capability of Diesel Generator Fan Cooling Sys. Caused by Fan Blades Not Having Proper Pitch Setting to Provide Necessary Cooling at All Temps.Evaluation Underway
ML19249E10012 September 1979RO on 790912:while Performing Evaluation to Determine When to Secure Quench Spray Pumps After Loca,Error Discovered in Emergency Procedure 1-EP-2 Requiring Pumps Be Secured at Level of 28.1%.Error Corrected;Cause to Be Determined
ML19208C43212 September 1979Ro:On 790912,noted That Station Curve for Refueling Water Tank Was Incorrect,Resulting in Tech Spec Upper Tank Level Limit Being Exceeded.Cause Unknown.Tank Level Lowered.Change to Station Curve Being DraftedCoast down
ML19242A66526 July 1979RO 79-091/01T-0 on 790725:followup Rept on Discovery That Component W-104 Dual Peripheral Driver in 7,300 Series Signal Comparator Cartds Could Fail,Causing Associated Bistable to Fail in Unsafe Mode
ML19225C94723 July 1979RO 79-089/01T:discovered Possiblity of Failure of Process Cards,Causing Adverse Effects on Associated Loop Actions. Process Card Failure Analysis Performed
ML19270G65325 April 1979RO 79-057/01T-0 on 790424:potential Overload exists;4,160 Volt Transfer Bus & Feeder Breakers Are Not Capable of Continually Carrying Full Load Current.Caused by Improper Sizing of Transfer Bus Equipment
ML19263C9595 February 1979Telcon Rept:Util Informed Region 2 of Potential Hydraulic Transient (Water Hammer) in Recirculation Spray Coolers During Operation in Post LOCA Environ.Magnitude of Transient & Applicability to Unit 1 Have Not Been Determined
ML19294A52814 November 1978RO 78-100 on 780803:rept Submitted Re Deficiency in Seismic Analysis of Reactor Vessel Insulation.Mod Made,But Was Not Seismically Analyzed